Cracking at a Superheater Header Connection
Examination of the header of the third superheater of a boiler producing 150 t/h of steam at 525 deg C and 118 kPa, disclosed extensive internal cracking at the connection to the tube joining this to a safety valve. Cracking was observed within the tube and in the thickness of the shell wall itself. The boiler had been in operation for approximately 160,000 h and was shut down for inspection when the cracking was detected. The material involved was 2.25 Cr, 1 Mo steel, and the unit had been subjected to 115 shutdowns. Initiation of the cracks was attributed...
T.L. da Silveira, I. Le May, Cracking at a Superheater Header Connection, ASM Failure Analysis Case Histories: Power Generating Equipment, ASM International, 2019, https://doi.org/10.31399/asm.fach.power.c9001001
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