An API type 2 steel clamp located on the riser of a semisubmersible drilling rig between the lower ball joint and riser blowout preventer (BOP) conductor failed after 7 years of service. Failure analysis revealed the cause of failure to be the low toughness of the clamp material. Contributing factors included the presence of a hard, brittle, heat-affected zone and weld defects at the handling pad eye. It was recommended that the replacement clamp be made from a material with good toughness and that any installation of attachments by welding be done according to qualified procedures.
Salah E. Mahmoud, Brittle Fracture of a Marine Riser Clamp, Handbook of Case Histories in Failure Analysis, Vol 1, Edited By Khlefa A. Esaklul, ASM International, 1992, p 385–388, https://doi.org/10.31399/asm.fach.v01.c9001114
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