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Several components from the tail boom of a helicopter were found fractured at a crash site, including gusset plates, the hat section near the lower yoke, and a cable that controls the pitch of the tail rotor. The components were recovered from the wreckage and taken to a lab for closer examination. Based on their observations and the results of SEM fractography, failure analysts concluded that the gusset plates failed due to a downward bending overload in tension and that the tail rotor control cable snapped due to tensile overload. There were no indications of delayed failure in any of the areas examined.

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