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Alejandro Toro Betancur
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Proceedings Papers
Pablo Andrés Gómez Flórez, Alejandro Toro Betancur, John Edison Morales Galeano, Jeisson Mejía Velásquez
AM-EPRI2024, Advances in Materials, Manufacturing, and Repair for Power Plants: Proceedings from the Tenth International Conference, 247-258, October 15–18, 2024,
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This work describes the repair procedure conducted on the High Pressure/Intermediate Pressure (HP/IP) and generator rotors of a 180 MW steam turbine General Electric (GE) - STAG207FA type D11 installed at La Sierra Thermoelectric Power Plant in Puerto Nare, Colombia. A lubricant supply failure at base load caused severe adhesive damage to the shafts in the bearing support areas and a permanent 3.5 mm bow at the HP/IP rotor mid span section, which required a complex intervention. The repair process began with the identification of the rotors manufacturing material through in-situ metallographic replicas, handheld XRF analysis and surface hardness measurements. Volumetric manual Gas Tungsten Arc Welding (GTAW) welding reconstruction of cracked areas followed by a surface overlay using GTAW and Plasma Arc Welding (PAW) welding processes were applied with a modular mechanized system, where a stress relief treatment through vibration was implemented with the help of computational simulations carried out to determine the fundamental frequencies of the rotors. Geometric correction of the HP/IP rotor mid span section was achieved thanks to the excitation of the rotor at some fundamental frequencies defined by the dynamic modeling and the use of heat treatment blankets at specific locations as well. Finally, after machining and polishing procedures, the power unit resumed operation eleven months after the failure and remains in service to the present date.