ASM Failure Analysis Case Histories: Air and Spacecraft
Fatigue Fracture of a 4337 Steel Articulated Rod Originating at an Electroetched Numeral
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Published:2019
Abstract
An articulated rod (made from 4337 steel (AMS 6412) forging, quenched and tempered to 36 to 40 HRC) used in an overhauled aircraft engine was fractured after being in operation for 138 h. Visual examination revealed that the rod was broken into two pieces 6.4 cm from the center of the piston-pin-bushing bore. The fracture was nucleated at an electroetched numeral 5 on one of the flange surfaces. A notch, caused by arc erosion during electroetching, was revealed by metallographic examination of a polished-and-etched section through the fracture origin. A remelted zone and a layer of untempered martensite constituted...
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Member Sign InFatigue Fracture of a 4337 Steel Articulated Rod Originating at an Electroetched Numeral, ASM Failure Analysis Case Histories: Air and Spacecraft, ASM International, 2019, https://doi.org/10.31399/asm.fach.aero.c0047835
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