Damage in a Gas Turbine Hot Gas Casing
The hot gas casing of a gas turbine used for peak load power production had developed extensive cracking during operation. The operating time was 18,000 h, and it had been subjected to 1,600 operating cycles. The gas temperature on the hot side was 985 deg C, on the cold side 204 deg C, the material being AISI 321 stainless steel. The purpose of the present study was to determine optimum repair welding procedures on the premise that the material was basically sound and undamaged by creep. The cracking was the result of thermal fatigue, and such cracks can propagate...
T.L. da Silveira, I. Le May, Damage in a Gas Turbine Hot Gas Casing, ASM Failure Analysis Case Histories: Power Generating Equipment, ASM International, 2019, https://doi.org/10.31399/asm.fach.power.c9001737
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