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torsion testing

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Image
Published: 01 January 2002
Fig. 55 Macroscale fracture surface of torsion-test specimen, where testing was done so as to avoid axial stresses during testing. Source: Ref 42 More
Image
Published: 15 January 2021
Fig. 55 Macroscale fracture surface of torsion-test specimen, where testing was done to avoid axial stresses during testing. Source: Ref 43 More
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001759
EISBN: 978-1-62708-241-9
... to withstand push-out load of 885 kg. Push-Out Load Test Results for Nitrided Samples The bearing cup tested by push-out load test and was found to withstand push-out load of 1015 kg. Endurance Test To check the torsional fatigue strength of drive shaft assembly and to compare the performances...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001733
EISBN: 978-1-62708-225-9
... Abstract Drive cables from a rubber processing machine were failing in less than 8 h of operation, the expected service life being much greater than 100 h. Comparison cables were tested to failure under known stress conditions, including tensile overload, torsional loading, reversed bending...
Image
Published: 01 January 2002
Fig. 31 Fracture surfaces of a torsional fatigue-test specimen. Courtesy of Greg Fett, Dana Corporation More
Image
Published: 01 June 2019
Fig. 5 Region showing torsional shear in the exemplar test specimen subjected to steady torsional loads. More
Image
Published: 15 January 2021
Fig. 40 Fracture surfaces of a torsional fatigue test specimen. Courtesy of G. Fett, Dana Corporation More
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001810
EISBN: 978-1-62708-241-9
... Abstract Several torsion bars had failed in a projectile weaving machine and were analyzed to determine the cause. Specimens prepared from the damaged components were subjected to visual inspection, hardness testing, chemical analysis, and metallurgical evaluations. The failed torsion bars had...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001468
EISBN: 978-1-62708-221-1
... torsional fatigue. Because it occurred on two different planes at 45 deg to the axis of the shaft it was due to reversals of torsional stress rather than fluctuations of unidirectional torque. Following this failure, the shafts of six other similar cranes were tested ultrasonically. Cracks to varying degree...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001230
EISBN: 978-1-62708-236-5
... Abstract A crankshaft was overloaded on a test stand and suffered an incipient crack in the crank pin. The crack run generally parallel to the longitudinal axis and branched off at the entrance into the two fillets at the transition to the crank arm. It consisted of many small cracks, all...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001596
EISBN: 978-1-62708-225-9
... deflection, greatly increasing the torsional stresses on the spring. To understand the fatigue limits under these test conditions, a bench test was used to establish the fatigue strength of the springs. The bench tests showed that the failed springs had an unacceptable surface texture that reduced...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001091
EISBN: 978-1-62708-214-3
.... These fracture initiation sites are inclined to the main fracture surface and have a helicoidal surface. This surface is the tension plane due to torsion on the bar. The texture of fracture at these origins is typical of fatigue. Testing Procedure and Results Surface Examination Scanning Electron...
Image
Published: 01 December 2019
Fig. 2 Testing apparatus, 60,000 lb Tinius Olsen testing machine. Load applied to the drive wrench fastened to a shaft fixture. The load initiates a static torsional load to the test wrench. The product of peak load and drive wrench determine ultimate torque More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0048117
EISBN: 978-1-62708-235-8
... Abstract Two outer valve springs made from air-melted 6150 pretempered steel wire broke during production engine testing. The springs were 50 mm in OD and 64 mm in free length, had five coils and squared-and-ground ends, and were made of 5.5 mm diam wire. It was revealed that fracture...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0046195
EISBN: 978-1-62708-225-9
... Abstract A pilot-valve bushing fractured after only a few hours of service. In operation, the bushing was subjected to torsional stresses with possible slight bending stresses. A slight misalignment occurred in the assembly before fracture. The bushing was made of 8617 steel and was case...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001220
EISBN: 978-1-62708-225-9
... Abstract A helical compression spring with ten turns made of 1.8 mm thick wire which was under high pressure during tension applied to a rocker arm broke on the test stand in the third turn. The fracture was a torsion fracture that initiated in the highly loaded inner fiber and showed in its...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091096
EISBN: 978-1-62708-234-1
... to an expensive gear mechanism. The rotor was subjected to severe chatter, which was an abnormal condition resulting from a series of continuous small overloads occurring at a frequency of around three per second. Investigation (visual inspection, hardness testing, and hot acid etch images) supported...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001192
EISBN: 978-1-62708-234-1
.... No cause for the crank fracture could be established from material testing. Probably the load was too high for the strength of the crank. Tensile strength could have been increased for the same material by tempering at lower temperature. Additionally, the resistance against high bend fatigue stresses...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046870
EISBN: 978-1-62708-217-4
... of the hollow shaft was exposed to hydraulic oil at temperatures of 0 to 80 deg C (30 to 180 deg F). Analysis (visual inspection, 15-30x low magnification examination, 4x light fractograph, chemical analysis, hardness testing) supported the conclusions that the shaft cracked in a region subjected to severe...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001368
EISBN: 978-1-62708-215-0
... Abstract A forged 4140 steel shaft that connected two runners in a hydroturbine failed catastrophically after approximately 5900 h of service. The runner and the mating section of the broken shaft were examined and tested by various methods. The results of the analyses indicated that the shaft...