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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001905
EISBN: 978-1-62708-217-4
... will also oversee the procedures of the manufacturer and perform first article testing to ensure this type of situation does not occur again. Acknowledgments The author would like to thank Valentin Frunza and Dennis Klaszewski of NAWCWD for their editorial and technical contributions. ...
Abstract
A bomb retaining ring fabricated from type 302 stainless steel unwrapped during a practice flight, causing the bomb fins to deploy. The retaining ring was able to unwrap itself because it was thinner and softer than required. Hardness testing, metallography, and tensile testing confirmed that the component was in the annealed condition and not in the required work-hardened 1/4-hard condition.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001909
EISBN: 978-1-62708-235-8
... The author would like to thank Valentin Frunza and Dennis Klaszewski of NAWCWD for their editorial and technical contributions. Reference Reference 1. Anon .: in Welding Handbook , 8th ed. , vol. 1 , Welding Technology, Connor L.P. , ed., American Welding Society , Miami, FL , 1987 , p...
Abstract
Welded low-carbon steel bomb fins were rejected because of poor weld practice. Visual and metallographic examination revealed that the resistance plug welds that attach the outer skin to the inner spar displayed inadequate weld penetration. Recommended changes to the resistance welding parameters resulted in acceptable welds.
Book Chapter
Use of XRD to Assess Residual Stresses in Steel Springs
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0090626
EISBN: 978-1-62708-218-1
... for this component. Fig. 1 Stress versus depth profiles for different steel coil springs Acknowledgments The authors would like to thank Debbie Aliya, Clayton O. Ruud, Stan Berkley, Robert Drake, and Fred Tonch for their helpful insight and careful review of the ideas presented in the source article...
Abstract
A steel spring used in an automotive application suddenly began to fail in the field, although “nothing had changed” in the fabrication process. Fatigue tests using springs fabricated prior to field failures lasted 500,000 cycles to failure, whereas fatigue tests performed on springs fabricated after field failures lasted only 50,000 cycles to failure. It was discovered that the percent coverage of shot peening prior and subsequent to the increase in failure incidence was much less than 100%, with a shot peening time of 12 min. The residual-stress state of “as fabricated” springs in three conditions were evaluated using XRD: springs manufactured prior to failure incidence increase, 12 min peen; springs manufactured following failure incidence increase, 12 min peen; and 60 min peen. The conclusion was that the failure occurred because low peening time significantly decreased the compressive residual-stress levels in the springs. Recommendation was made to increase the time the spring was shot peened from 12 to 60 min.
Book Chapter
Failure of Die Cast Aluminum Cluster Bomb Tailcone Assemblies
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001908
EISBN: 978-1-62708-235-8
... of the parts was also unacceptable. Extended analysis indicated that the problem was rather widespread. It was concluded that the serviceability of the casting was adversely affected. Acknowledgment The author would like to thank Valentin Frunza and Dennis Klaszewski of NAWCWD for their editorial...
Abstract
Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.
Book Chapter
Cracking in Gas Turbine Blades
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090181
EISBN: 978-1-62708-229-7
... of the problem was considered more generic, and the primary failure mechanism was identified as LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first. Acknowledgments The author wishes to thank Mohan Hebbar of Siemens...
Abstract
Cracking in gas turbine blades was found to initiate from a mechanism of low-cycle fatigue (LCF). LCF is induced during thermal loading cycles in gas turbines. However, metallography of two cracked blades revealed a change in microstructure at as-cast surfaces for depths up to 0.41 mm (0.016 in.). Evaluation by SEM confirmed the difference in structure was associated with a lack of formation of coarse gamma prime structure in the matrix. Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere during the HIP process, resulting in the weakened structure. Because subsequent failures were found in blades that did not come from the suspect HIP lot, the scope of the problem was considered generic, and the conclusion was that the primary failure mechanism was LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first.
Book Chapter
Use of XRD to Evaluate Cracks in Steel Cargo Tiedown Sockets
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0090639
EISBN: 978-1-62708-227-3
... stress-relief heat treatment process. X-ray diffraction residual-stress measurements were then performed on heat treated tiedown sockets to verify the effectiveness of the localized heat treatment process applied. Acknowledgments The authors would like to thank Debbie Aliya, Clayton O. Ruud, Stan...
Abstract
Cracks initiating from the tip of the cloverleaf pattern in steel cargo tiedown sockets were observed by the builder following installation aboard several cargo vessels in various stages of construction. Testing of finite element models and measurements performed in the field on cargo ships with the cracking problem supported the conclusion that the failure was caused by overload. Additional testing showed that the overload failure and the transition from ductile to brittle fracture were facilitated by a combination of high brittleness due to flame cutting, increased hardness due to the cold-working coining process, and high residual stresses created by welding. Recommendations included the removal of the brittle, carbon-rich transformed martensite layer introduced by flame cutting and the application of a localized stress-relief heat treatment process. X-ray diffraction residual-stress measurements were then performed on heat treated tiedown sockets to verify the effectiveness of the localized heat treatment process applied.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001906
EISBN: 978-1-62708-217-4
... office invoked the warranty clause. Acknowledgment The author would like to thank Valentin Frunza and Dennis Klaszewski of NAWCWD for their editorial and technical contributions. References References 1. Anon. : in Product Design Guide for Forging , Forging Industry Association...
Abstract
Suspension lugs fabricated from AISI 4340 steel used to facilitate loading of bombs onto the underside of military aircraft could not sustain required loads during routine proof load testing. Three failed lugs underwent visual examination, chemical analysis, metallography, hardness testing, scanning electron microscopy, and energy-dispersive x-ray spectroscopy. It was determined that the failures were due to forging defects. Both forging laps and seams acted as stress concentrators when the lugs were loaded during proof testing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001907
EISBN: 978-1-62708-217-4
... ductility, increased fracture toughness, and increased resistance to HASCC. Acknowledgment The author would like to thank Valentin Frunza and Dennis Klaszewski of NAWCWD for their editorial and technical contributions. Reference Reference 1. Anon. : in Product Design Guide for Forging...
Abstract
Aircraft missile launcher attachment bolts fabricated from cadmium-coated Hy-tuf steel were found broken. Subsequent analysis of the broken bolts indicated three causes of failure. First, the bolts had been carburized, which was not in conformance with the heat treating requirements. Second, macroetching showed that the bolts has been machined from stock rather than forged, and the threads cut rather than rolled. It was also determined that hydrogen-assisted stress-corrosion cracking also played a part in the failure of the high-strength bolts.
Book Chapter
Evaluation of the Vent Header Crack at Edwin I. Hatch Unit #2 Nuclear Power Station
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001146
EISBN: 978-1-62708-229-7
... header. Acknowledgments The author wishes to thank U.S. NRC Region II (FIN A3500) for funding this work. Additional thanks to L. Gerlach, A. Cendrowski, D. Horne and O. Betancourt for their help, and Dr. J. R. Weeks for his constant support. ...
Abstract
A metallurgical failure analysis was performed on pieces of the cracked vent header pipe from the Edwin I. Hatch Unit 2 Nuclear power plant. The analysis consisted of optical microscopy, chemical analysis, mechanical Charpy impact testing, and fractography. It was found that the material of the vent header met the mechanical and chemical properties of ASTM A516 Grade 70 carbon-manganese steel material and microstructures were consistent with this material. Fracture faces of the cracked pipe were predominantly brittle in appearance with no evidence of fatigue contribution. The NDTT (Nil ductility Transition Temperature) for this material was approximately -51 deg C (-60 deg F). The fact that the material's NDTT was significantly out of the normal operating range of the pipe suggested an impingement of low temperature nitrogen (caused by a faulty torus inerting system) induced a thermal shock in the pipe which, when cooled below its NDTT, cracked in a brittle manner.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001263
EISBN: 978-1-62708-224-2
... become brittle as a result of ageing. Since the embrittlement of such eye bolts can lead to serious accidents, the notched bar impact strength of the eye bolts in the store and in use in the factory should be subjected to spot checks. We would like to thank Dr. T. Geiger, Forschunqslaboratorium...
Abstract
After several years' use, an eyebolt suffered brittle fracture in the first turn of the thread. The fracture started at the notch at the root of the thread. Neither localized material defect nor an old crack were present. The investigation showed that instead of the specified steel quality St 37-2 N, a steel with about 0.5% C had been used. The microstructure with the coarse ferrite network indicated that the forged eye bolt had been normalized either at too high a temperature or not at all. In any case the anneal at 900 deg C produced a considerably more finely grained structure. In addition, the nature of the fracture and the results of the notched bar impact tests showed that in spite of the high C-content, the eye bolt had become brittle as a result of aging.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001910
EISBN: 978-1-62708-217-4
... (receiving activity). Acknowledgment The author would like to thank Valentin Frunza and Dennis Klaszewski of NAWCWD for their editorial and technical contributions. References References 1. Decker R.F. , Eash J.T. , and Goldman A.J. : 18% Nickel Maraging Steel, Source Book...
Abstract
Breech bolt assemblies from the Gatling guns used on fighter aircraft failed during firing tests. Metallography of the failed components revealed considerable decarburization which resulted in a loss of surface hardness. It was also determined that the maraging steel components were not in the nitrided condition as was required. This resulted in lower wear and fatigue resistance. These components also had a silicon content nearly double of that specified. The high silicon content lowered the notch tensile strength and toughness of the components.
Book Chapter
RMS Titanic: A Metallurgical Problem
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001591
EISBN: 978-1-62708-227-3
... by Charpy Impact Tests. These factors were contributing causes of the rapid sinking of the Titanic. Omitted in this study have been design faults and poor seamanship, which were basic to the loss of the RMS Titanic. Acknowledgments The authors wish to thank Mr. George Tullock, RMS Titanic, Inc...
Abstract
On 14 April 1912, at 11:40 p.m., Greenland Time, the Royal Mail Ship Titanic on its maiden voyage was proceeding westward at 21.5 knots (40 km/h) when the lookouts on the foremast sighted a massive iceberg estimated to have weighed between 150,000 to 300,000 tons at a distance of 500 m ahead. Immediately, the ship’s engines were reversed and the ship was turned to port (left) in an attempt to avoid the iceberg. In about 40 sec, the ship struck the iceberg below the waterline on its starboard (right) side near the bow. The iceberg raked the hull of the ship for 100 m, destroying the integrity of the six forward watertight compartments. Within 2 h 40 min the RMS Titanic sank. Metallurgical examination and chemical analysis of the steel taken from the Titanic revealed important clues that allow an understanding of the severity of the damage inflicted on the hull. Although the steel was probably as good as was available at the time the ship was constructed, it was very inferior when compared with modern steel. The notch toughness showed a very low value (4 J) for the steel at the water temperature (-2 deg C) in the North Atlantic at the time of the accident.
Book Chapter
Catastrophic Failure of a Fan in a Diesel Engine Cooler
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001612
EISBN: 978-1-62708-218-1
... by the authors. Authors are also thankful to the director of TCIRD for permission to publish the work. Selected References Selected References • Failures Related to Welding , Failure Analysis and Prevention , Vol 11 , ASM Handbook , ASM International , 2002 , p 156 – 191 10.31399/asm.hb.v11...
Abstract
The fan used to cool a diesel engine fractured catastrophically after approximately 100 h of operation. The fan failed at a spider, which was resistance spot welded to a shim placed between two circular spiders of 3 mm thickness. The detailed analysis of the fracture indicated that the premature failure of the fan was due to inadequate bonding between the sheets at the weld nugget. The fracture was initiated from the nugget-plate interface. The inadequate penetration and lack of fusion between the steel sheets during resistance spot welding led to poor weld strength and the fracture during operation. The propensity to crack initiation and failure was accentuated by improper cleaning of the surfaces prior to welding and to inadequate nugget-to-sheet edge distance.
Book Chapter
Intergranular Fracture of Steam Generator Tubes
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090881
EISBN: 978-1-62708-229-7
...–163 The author would also like to thank William Becker and Gordon Powell for their review of the source article. Selected Reference Selected Reference • Becker W.T. and Lampman S. , Fracture Appearance and Mechanisms of Deformation and Fracture , Failure Analysis...
Abstract
A power plant using two steam generators (vertical U-tube and shell heat exchangers, approximately 21 m (68 ft) high with a steam drum diameter of 6 m (20 ft)) experienced a steam generator tube rupture. Each steam generator contained 11,012 Inconel alloy 600 (nickel-base alloy) tubes measuring 19 mm OD, nominal wall thickness of 1.0 mm (0.042 in.), and average length of 18 m (57.75 ft). The original operating temperature of the reactor coolant was 328 deg C (621 deg F). A tube removal effort was conducted following the tube rupture event. Investigation (visual inspection, SEM fractographs, and micrographs) showed evidence of IGSCC initiating at the OD and IGA under ridgelike deposits that were analyzed and found to be slightly alkaline to very alkaline (caustic) in nature. Crack oxide analysis indicated sulfate levels in excess of expected values. The analysis supported the conclusion that that the deposits formed at locations that experienced steam blanketing or dryout at the higher levels of the steam generators. Recommendations included steam generator water-chemistry controls, chemical cleaning, and reduction of the primary reactor coolant system temperature.
Book Chapter
Failure of Trailer Kingpins Caused by Overheating During Forging
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001302
EISBN: 978-1-62708-215-0
.... Acknowledgments The authors wish to thank Mr. J.R. Kattus of AMC-Vulcan, Inc., Birmingham, Alabama, for permission to reproduce Fig. 5 . Thanks are also due to Prof. T. Gladman of the University of Leeds, U.K, for permission to reproduce Fig. 6 and 7 . Selected References Selected References...
Abstract
To forged AISI 4140 steel trailer kingpins fractured after 4 to 6 months of service. Fractographic and metallographic examination revealed that cracks were present in the spool-flange shoulder region of the defective kingpins prior to installation on the trailers. The cracks grew and coalesced during service. Consideration of the manufacturing process suggested that the cracks were the result of overheating of the kingpin blanks prior to forging, which was exacerbated during forging by deformation heating in the highly-strained region. This view was supported by results of two types of tensile tests conducted near the incipient melting temperature at the grain boundaries. All kingpins made by the supplier of the fractured ones were ultrasonically inspected and six more anticipated to fail were found. It was recommended that the heating of forging blanks be more carefully controlled, especially with respect to the accuracy of the optical pyrometer temperature readout. Also, procedures must be developed such that forging blanks that trigger the over-temperature alarm are reliably and permanently removed from the production line.
Book Chapter
Hydrogen Induced Cracking of a Tappet Adjusting Screw
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001613
EISBN: 978-1-62708-235-8
... to reduce the hardness after carburizing, completely eliminated the problem. Acknowledgments The cooperation and help rendered by the staff of the Materials Science & Technology Division, TCIRD during the investigation is greatly acknowledged by the author. The author is also thankful...
Abstract
The electroplated tappet adjusting screws used in diesel engines failed during initial bend testing. The analysis of the failure showed that the fracture was nucleated from the subsurface of the screw. The fracture surface was intergranular at the ID and OD region and microvoid coalescence in the center. The improper baking after electroplating of the screw led to H2-induced blistering/cracking. The high strength of the threaded region of the adjusting screw increased the failure propensity.
Book Chapter
Failure of a Sprocket Drive Wheel in a Tracked All-Terrain Vehicle
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001303
EISBN: 978-1-62708-215-0
.... The residual compression offsets tension service stress and thereby tends to increase resistance to fatigue failure. Acknowledgments Sincere thanks to Samuel R. Callaway for his comments and constructive suggestions. Selected Reference Selected Reference • Miller B.A. , Overload Failures...
Abstract
A sand-cast LM6M aluminum alloy sprocket drive wheel in an all-terrain vehicle failed. Extensive cracking had occurred around each of the six bolt holes in the wheel. Evidence of considerable deformation in this area was also noted. Examination indicated that the part failed because of gross overload. Use of an alloy with a much higher yield strength and improvement in design were recommended.
Book Chapter
Failure Analysis of Spline Shaft in Beco Lathe
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001786
EISBN: 978-1-62708-241-9
.... Acknowledgments I am immensely thankful to Director, IGCAR and Director, ESG for their guidance and support. I also thank the members of CWD, MJS, QAD, CG of IGCAR for the technical support in conducting the failure analysis. References References 1. BECO Lathe Machine Manual ( 1991 ) 2...
Abstract
A heavy duty facing lathe failed when the tool post caught one of the jaws on the rotating chuck, causing the spline shaft that drives the main spindle to fracture. A detailed analysis of the fracture surfaces (including fractography, metallography, and analytical stress calculations) revealed areas of damage due to rubbing with evidence of cleavage fracture on the unaffected surfaces. The results of stress analysis indicated that repeated reversals of the spindle produced stresses exceeding the fatigue limit of the shaft material. These stresses led to the formation of microcracks in a retaining ring groove that were accelerated to sudden failure when the tool post and chuck collided.
Book Chapter
Improper Fabrication Rotating Blades Results in Premature Failure
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001150
EISBN: 978-1-62708-235-8
... direction, as had the bent bars, the premature fractures would not have occurred. Acknowledgments The author wishes to thank Mark H. Gilkey of Factory Mutual Research Corporation for his extensive assistance in the analysis of these flight arm failures. Reference Reference 1. Bluhm J. I...
Abstract
A number of rotating blades in a diffuser at a sugar beet processing plant fabricated from rectangular bars cut from rolled carbon-manganese steel plate fractured brittlely. However, apparently identical blades underwent significant plastic deformation without fracture. Inspection of both fractured and bent blades revealed similar preexisting cracks at the toes of bar attachment welds. Metallographic examination of the bent and the fractured bars revealed they had been cut parallel and transverse, respectively, to the rolling direction of the steel plate. Due to the combined effects of the low fracture toughness of the plate on planes parallel in the rolling direction, the presence of the preexisting cracks, and the relatively large section thickness of the bars, the bars whose lengths were transverse to the rolling direction fractured brittlely when subjected to impact loads. Had the poor transverse properties of thick-section plate been recognized, and all the bars properly cut with respect to the rolling direction, the premature fractures would not have occurred.
Book Chapter
Fatigue and Corrosion Fatigue Failure Surfaces of Concrete Reinforcement
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001656
EISBN: 978-1-62708-219-8
... obtained from the International Lead Zinc Research Organization and Argonne National Laboratories as portion of their OTEC research. The Electron Microscope Unit staff of the University of Sydney are thanked for their cooperation in these studies. References References 1. Roper H...
Abstract
Some corrosion processes in the presence of chlorides, for steel embedded in concrete, are described and illustrated with the aid of scanning electron microscope EDXA data. Observations made of failure surfaces of reinforcements removed from the concrete beams after being subjected to sinusoidal load fluctuations at 6.7 Hz in air, 3% NaCl solution, and natural sea water are described. Reinforcement types studied included: hot-rolled mild steel bar, hot-rolled alloyed high strength bar, cold-worked high strength bar, galvanized bar of all these three types, nickel-clad bar and epoxy-coated bar.
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