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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047566
EISBN: 978-1-62708-235-8
... Abstract Handles welded to the top cover plate of a chemical-plant downcomer broke at the welds when the handles were used to lift the cover. The handles were fabricated of low-carbon steel rod; the cover was of type 502 stainless steel plate. The attachment welds were made with type 347...
Abstract
Handles welded to the top cover plate of a chemical-plant downcomer broke at the welds when the handles were used to lift the cover. The handles were fabricated of low-carbon steel rod; the cover was of type 502 stainless steel plate. The attachment welds were made with type 347 stainless steel filler metal to form a fillet between the handle and the cover. The structure was found to contain a zone of brittle martensite in the portion of the weld adjacent to the low-carbon steel handle; fracture had occurred in this zone. The brittle martensite layer in the weld was the result of using too large a welding rod and too much heat input, melting of the low-carbon steel handle, which diluted the austenitic stainless steel filler metal and formed martensitic steel in the weld zone. Because it was impractical to preheat and postheat the type 502 stainless steel cover plate, the low-carbon steel handle was welded to low-carbon steel plate, using low-carbon steel electrodes. This plate was then welded to the type 502 stainless steel plate with type 310 stainless steel electrodes. This design produced a large weld section over which the load was distributed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048808
EISBN: 978-1-62708-228-0
... Abstract The welds joining the liner and shell of a fluid catalytic cracking unit failed. The shell was made of ASTM A515 carbon steel welded with E7018 filler metal. The liner was made of type 405 stainless steel and was plug welded to the shell using ER309 and ER310 stainless steel filler...
Abstract
The welds joining the liner and shell of a fluid catalytic cracking unit failed. The shell was made of ASTM A515 carbon steel welded with E7018 filler metal. The liner was made of type 405 stainless steel and was plug welded to the shell using ER309 and ER310 stainless steel filler metal. Fine cracks starting inside the weld zone and spreading outward through the weld and toward the surface were observed during examination. Decarburization and graphitization of the carbon steel at the interface was noted. The high carbon level was found to allow martensite to form eventually. The structure was found to be austenitic in the area where the grain-boundary precipitates appeared heaviest. The composition of the precipitates was analyzed using an electron microprobe to reveal presence of sulfur. Microstructural changes in the weld alloy at the interface were interpreted to be caused by dilution of the alloy and the presence of sulfur caused hot shortness. The necessary internal stress to produce extensive cracking was produced by the differential thermal expansion of the carbon and stainless steels. Periodic careful gouging of the affected areas followed by repair welding was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001645
EISBN: 978-1-62708-232-7
... Abstract An extensive metallurgical investigation was carried out on samples of a failed roller bearing from the support and tilting system of a basic oxygen furnace converter used in the steel melting shop of an integrated steel plant. The converter bearing was fabricated from low-carbon...
Abstract
An extensive metallurgical investigation was carried out on samples of a failed roller bearing from the support and tilting system of a basic oxygen furnace converter used in the steel melting shop of an integrated steel plant. The converter bearing was fabricated from low-carbon, carburizing grade steel and had failed in service within a year of fitting to a repaired shaft. Microscopic observations of both the broken roller and inner-race samples revealed subsurface cracking and preponderance of brittle oxide and other macroinclusions. Electron probe microanalysis studies confirmed that the brittle oxides that formed stringers were alumina, and the other macroinclusions were complex silicates. Both the alumina and silicate inclusions were deleterious to contact-fatigue properties. Microstructurally, the carburized regions of the broken roller and of inner-race samples contained high-carbon tempered martensite. Microhardness measurements revealed that. Although the core hardness of the roller and the inner-race samples were similar, the surface hardness of the roller was approximately 8.5 HRC units harder than that of the inner-race. SEM observations of the roller fracture surface revealed striations indicative of fatigue, and EDS analyses corroborated a high incidence of silicate inclusions at crack sites. The study suggests that the failure of the bearing occurred because the hardness difference between the roller bearing and the inner-race surfaces resulted in wear of the inner-race. The wear led to shaft misalignment and play during service. The misalignment, coupled with the presence of inclusions, caused fatigue failure of the roller bearing.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047879
EISBN: 978-1-62708-234-1
..., grade 2 steel, and the larger-diam section was covered with a type 316 stainless steel end cap. The cap was welded to each end using type ER316 stainless steel filler metal. The forged steel shaft was revealed to have fractured at approximately 90 deg to the shaft axis in the weld metal...
Abstract
The stub-shaft assembly which was part of the agitator shaft in a polyvinyl chloride reactor, fractured in service after a nut that retained a loose sleeve around the smaller-diam section of the shaft had been tightened several times to reduce leakage. The shaft was made of ASTM A105, grade 2 steel, and the larger-diam section was covered with a type 316 stainless steel end cap. The cap was welded to each end using type ER316 stainless steel filler metal. The forged steel shaft was revealed to have fractured at approximately 90 deg to the shaft axis in the weld metal and not in the heat-affected zone of the forged steel shaft. Microscopic investigation and chemical analysis of the steel shaft revealed presence of martensite (offered a path of easy crack propagation) around the fusion line and dilution of the weld metal by the carbon steel shaft. The microstructure was found to be martensitic as the fusion line was approached. The forged steel shaft was concluded to have failed by ductile fracture and possible reasons were discussed. Corrective measures adopted in the replacement shaft were specified.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001532
EISBN: 978-1-62708-232-7
... variations in roll life. The paper provides an insight into the microstructural characteristics of spalled ICED HSM work rolls, which underwent failure under similar mill operating environment in an integrated steel plant under the Steel Authority of India Limited. Microstructural features influencing ICDP...
Abstract
Work rolls made of indefinite chill double-poured (ICDP) iron are commonly used in the finishing trains of hot-strip mills (HSMs). In actual service, spalling, apart from other surface degeneration modes, constitutes a major mechanism of premature roll failures. Although spalling can be a culmination of roll material quality and/or mill abuse, the microstructure of a broken roll can often unveil intrinsic inadequacies in roll material quality that possibly accentuate failure. This is particularly relevant in circumstances when rolls, despite operation under similar mill environment, exhibit variations in roll life. The paper provides an insight into the microstructural characteristics of spalled ICED HSM work rolls, which underwent failure under similar mill operating environment in an integrated steel plant under the Steel Authority of India Limited. Microstructural features influencing ICDP roll quality, viz. characteristics of graphite, carbides, martensite, etc., have been extensively studied through optical microscopy, quantitative image analysis (QIA), and electron-probe microanalysis (EPMA). These are discussed in the context of spalling propensity and roll life.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001535
EISBN: 978-1-62708-232-7
... environment, the failure involves a particular roll or a specific batch of rolls. This paper provides a microstructural insight into the cause of premature breakage of a second-intermediate Sendzimir mill drive roll used at a stainless steel sheet rolling plant under the Steel Authority of India Limited...
Abstract
Although a precise understanding of roll failure genesis is complex, the microstructure of a broken roll can often unravel intrinsic deficiencies in material quality responsible for its failure. This is especially relevant in circumstances when, even under a similar mill-operating environment, the failure involves a particular roll or a specific batch of rolls. This paper provides a microstructural insight into the cause of premature breakage of a second-intermediate Sendzimir mill drive roll used at a stainless steel sheet rolling plant under the Steel Authority of India Limited. Microstructural issues influencing roll quality, such as characteristics of carbides, tempered martensite, retained austenite, etc., have been extensively studied through optical and scanning electron microscopy, electron-probe microanalysis, image analysis, and x-ray diffractometry. These are discussed to elucidate specific microstructural inadequacies that accentuated the failure. The study reveals that even through retained austenite content is low (6.29 vol%) and martensite is non-acicular, the roll breakage is a consequence of intergranular cracking caused by improper carbide morphology and distribution.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0048674
EISBN: 978-1-62708-222-8
... Abstract Fasteners, made in high-production progressive dies from 0.7 mm thick cold-rolled 1060 steel, were used to secure plastic fabric or webbing to the aluminum framework of outdoor furniture. It was found that approximately 30% of the fasteners cracked and fractured as they were compressed...
Abstract
Fasteners, made in high-production progressive dies from 0.7 mm thick cold-rolled 1060 steel, were used to secure plastic fabric or webbing to the aluminum framework of outdoor furniture. It was found that approximately 30% of the fasteners cracked and fractured as they were compressed to clamp onto the framework prior to springback. The heat treatment cycle of the fasteners consisted of austenitizing, quenching, tempering to obtain a tempered martensite microstructure, acid cleaning, zinc electroplating, coating with a clear dichromate and thereafter baking to remove the nascent hydrogen. It was revealed that fasteners treated in this manner were brittle due to hydrogen embrittlement as the baking process was found to not be able to remove all the nascent hydrogen which had induced during acid cleaning and electroplating. The heat treatment cycle was modified to produce a bainitic structure and the method of plating the fastener with zinc was changed from electroplating to a mechanical deposition process to thus avoid hydrogen embrittlement.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001627
EISBN: 978-1-62708-222-8
... Abstract A section from a stainless steel kitchen sink showed a round red stain on its surface after a short time in storage. Several of these sinks were stacked together and separated by felt pads while in storage, and the mating sink showed a nearly identical stain in the same area, while...
Abstract
A section from a stainless steel kitchen sink showed a round red stain on its surface after a short time in storage. Several of these sinks were stacked together and separated by felt pads while in storage, and the mating sink showed a nearly identical stain in the same area, while no stains were noted on any of the other sinks in the stack. The stain was located near one of the pads; however, no discoloration was noted at the pad location. EDS analysis showed the base metal to be austenitic stainless steel, such as type 304. FTIR analysis of the stain revealed carboxylic salts and salts of organic acids, in addition to hydroxyl functionality. The discoloration was caused by localized rusting of the sink from prolonged exposure to a chloride containing substance. The appearance suggests that the substance may actually have been a drop of perspiration (sweat) from a factory worker. Based on these findings, one of the recommendations was to use thicker pads between the sinks to allow any such liquids to dry before causing corrosion damage.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048413
EISBN: 978-1-62708-226-6
... Abstract A type 316L stainless steel angled plate failed. The fatigue fracture was found to have occurred at a plate hole. Symmetric cyclic bending forces were revealed by the fatigue damage at the fracture edge at the top surface of the plate. Fatigue striations and slip bands produced...
Abstract
A type 316L stainless steel angled plate failed. The fatigue fracture was found to have occurred at a plate hole. Symmetric cyclic bending forces were revealed by the fatigue damage at the fracture edge at the top surface of the plate. Fatigue striations and slip bands produced on the surface during cyclic loading were observed. The material was showed by the deformation structure to be in the cold-worked condition and was termed to not be the cause of the implant failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048403
EISBN: 978-1-62708-226-6
... Abstract During the internal fixation, the type 316LR stainless steel cortical bone screw failed. Extensive spiral deformation was revealed by the fracture surface. Dimple structure characteristic of a ductile failure mode was observed with dimples oriented uniformly in the deformation...
Abstract
During the internal fixation, the type 316LR stainless steel cortical bone screw failed. Extensive spiral deformation was revealed by the fracture surface. Dimple structure characteristic of a ductile failure mode was observed with dimples oriented uniformly in the deformation direction. A zone of heavily deformed grains at the fracture edge was revealed by longitudinal metallographic examination. The shearing fractures of a commercially pure titanium screw and a cast cobalt-chromium-molybdenum alloy were discussed for purpose of comparison.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048420
EISBN: 978-1-62708-226-6
... Abstract Fretting and fretting corrosion at the contact area between the screw hole of a type 316LR stainless steel bone plate and the corresponding screw head was studied. The attack on the 316LR stainless steel was only shallow. Mechanical grinding and polishing structures were exhibited...
Abstract
Fretting and fretting corrosion at the contact area between the screw hole of a type 316LR stainless steel bone plate and the corresponding screw head was studied. The attack on the 316LR stainless steel was only shallow. Mechanical grinding and polishing structures were exhibited by a large portion of the contact area. Fine corrosion pits in the periphery were observed and intense mechanical material transfer that can take place during fretting was revealed. Smearing of material layers over each other during wear was observed and attack by pitting corrosion was interpreted to be possible.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c9001579
EISBN: 978-1-62708-226-6
... Abstract Stainless steel is frequently used for bone fracture fixation in spite of its sensitivity to pitting and cracking in chloride containing environments (such as organic fluids) and its susceptibility to fatigue and corrosion fatigue. A 316L stainless steel plate implant used for fixation...
Abstract
Stainless steel is frequently used for bone fracture fixation in spite of its sensitivity to pitting and cracking in chloride containing environments (such as organic fluids) and its susceptibility to fatigue and corrosion fatigue. A 316L stainless steel plate implant used for fixation of a femoral fracture failed after only 16 days of service and before bone callus formation had occurred. The steel used for the implant met the requirements of ASTM Standard F138 but did contain a silica-alumina inclusion that served as the initiation point for a fatigue/corrosion fatigue fracture. The fracture originated as a consequence of stress intensification at the edge of a screw hole located just above the bone fracture; several fatigue cracks were also observed on the opposite side of the screw hole edge. The crack propagated in a brittle-like fashion after a limited number of cycles under unilateral bending. The bending loads were presumably a consequence of leg oscillation during assisted perambulation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048397
EISBN: 978-1-62708-226-6
... Abstract A large portion of the four-hole Lane plate disintegrated and consisted mainly of corrosion products after remaining in the body for 26 years. Transformation structures and carbides were exhibited by the plate which was made from chromium steel. Minimal corrosion was exhibited...
Abstract
A large portion of the four-hole Lane plate disintegrated and consisted mainly of corrosion products after remaining in the body for 26 years. Transformation structures and carbides were exhibited by the plate which was made from chromium steel. Minimal corrosion was exhibited by the soft austenitic 304 stainless steel used to make the screws. The corrosion products of the plate were revealed by microprobe analysis to impregnate the surrounding tissues. Improper material selection was concluded to be the reason for the general corrosion behavior.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048405
EISBN: 978-1-62708-226-6
... Abstract Type 316LR stainless steel screws that failed by fatigue were studied. It was found that fatigue fracture can occur on different thread levels, depending on the loading situation. The initiation of secondary fatigue cracks was occasionally found parallel to the fracture plane...
Abstract
Type 316LR stainless steel screws that failed by fatigue were studied. It was found that fatigue fracture can occur on different thread levels, depending on the loading situation. The initiation of secondary fatigue cracks was occasionally found parallel to the fracture plane. The screws were used with a relatively rigid plate to treat a fracture complication in the upper end of the femur. The fatigue failures were explained by signs of unstable fixation revealed by radiographs.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048400
EISBN: 978-1-62708-226-6
... not to be in compliance with standards (type 304 stainless steel without molybdenum). The screws and washers were found to be made of remelted implant-quality type 316L stainless steel and were intact. Signs of sensitization, characterized by chromium carbide precipitates at the grain boundaries, were revealed...
Abstract
Cerclage wire, which was used with two screws and washers for a tension band in a corrective internal fixation, was found broken at several points and corroded after nine months in service. The material was examined using energy-dispersive x-ray analysis and determined not to be in compliance with standards (type 304 stainless steel without molybdenum). The screws and washers were found to be made of remelted implant-quality type 316L stainless steel and were intact. Signs of sensitization, characterized by chromium carbide precipitates at the grain boundaries, were revealed by the microstructure. Intercrystalline corrosion with pitted grains was indicated by SEM fractography. Improper heat treatment of the steel was interpreted to have led to intercrystalline corrosion and implant separation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048419
EISBN: 978-1-62708-226-6
... Abstract Heavy pitting corrosion on type 304 stainless steel bone screw was studied. A screw head that exhibited heavy pitting corrosion attack was observed. Deep tunnels that penetrated the screw head and followed the inclusion lines were revealed. The screw was inserted in a plate made...
Abstract
Heavy pitting corrosion on type 304 stainless steel bone screw was studied. A screw head that exhibited heavy pitting corrosion attack was observed. Deep tunnels that penetrated the screw head and followed the inclusion lines were revealed. The screw was inserted in a plate made of type 316LR stainless steel and some mechanical fretting and very few corrosion pits were revealed. Type 304 stainless steel was deemed not to be satisfactory as an implant material.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048410
EISBN: 978-1-62708-226-6
... Abstract A narrow bone plate made of type 316 stainless steel and used to stabilize an open midshaft femur fracture failed. A crack at a plate hole next to the fracture site had been revealed by a radiograph taken 13 weeks after the operation. The plate was revealed to be slightly bent...
Abstract
A narrow bone plate made of type 316 stainless steel and used to stabilize an open midshaft femur fracture failed. A crack at a plate hole next to the fracture site had been revealed by a radiograph taken 13 weeks after the operation. The plate was revealed to be slightly bent in the horizontal plane, and the fracture gap was considerably open. The screws and plates supplied by different manufacturers were revealed to be different with respect to microcleanliness (primary inclusion content) of the materials and only one of them was found to be according to specifications. The local crack formation was influenced by the presence of larger inclusions. The screw failed was revealed to have failed through a fatigue mechanism by the presence of striations in the scanning electron micrograph. The crack in the plate was revealed to have originated at the upper, outer corner of the plate by the beach marks which indicated the action of asymmetric bending and rotational forces.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c9001606
EISBN: 978-1-62708-226-6
... Abstract Failures of four different 300-series austenitic stainless steel biomedical fixation implants were examined. The device fractures were observed optically, and their surfaces were examined by scanning electron microscopy. Fractography identified fatigue to be the failure mode for all...
Abstract
Failures of four different 300-series austenitic stainless steel biomedical fixation implants were examined. The device fractures were observed optically, and their surfaces were examined by scanning electron microscopy. Fractography identified fatigue to be the failure mode for all four of the implants. In every instance, the fatigue cracks initiated from the attachment screw holes at the reduced cross sections of the implants. Two fixation implant designs were analyzed using finite-element modeling. This analysis confirmed the presence of severe stress concentrations adjacent to the attachment screw holes, the fatigue crack initiation sites. Conclusions were reached regarding the design of these types of implant fixation devices, particularly the location of the attachment screw holes. The use of austenitic stainless steel for these biomedical implant devices is also addressed. Recommendations to improve the fixation implant design are suggested, and the potential benefits of the substitution of titanium or a titanium alloy for the stainless steel are discussed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048830
EISBN: 978-1-62708-228-0
... Abstract A vessel made of ASTM A204, grade C, molybdenum alloy steel and used as a hydrogen reformer was found to have cracked in the weld between the shell and the lower head. Six samples from different sections were investigated. The crack was found to be initiated at the edge of the weld...
Abstract
A vessel made of ASTM A204, grade C, molybdenum alloy steel and used as a hydrogen reformer was found to have cracked in the weld between the shell and the lower head. Six samples from different sections were investigated. The crack was found to be initiated at the edge of the weld in the coarsegrain portion of the HAZ. The microstructure was found to be severely embrittled and severely gassed in an area around the crack. The microstructure of the metal in the head was revealed to be banded and contained spheroidal carbides. The lower head was established by hardness values and microscopic examination to have been overheated for a sufficiently long time to reduce the tensile strength below the minimum required for the steel. It was interpreted that the wide difference in tensile strength between head and weld metal (including HAZ) formed a metallurgical notch that enhanced the diffusion of hydrogen into the metal in the cracked region. The resultant embrittlement and associated fissuring was established to have caused the failure. The hydrogen was diffused out by wrapping the vessel in asbestos and heating followed by cooling as prescribed by ASME code.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0091594
EISBN: 978-1-62708-228-0
... amine service if the temperature is expected to be above 95 deg C (200 deg F). Recommendations included inspecting all welds using shear wave ultrasonic testing and postweld heat treating all welds in lean amine service. Piping Refineries Sulfur recovery units Weldments Welded carbon steel...
Abstract
Two leaks were discovered at a sulfur recovery unit in a refinery. The leaks were at pipe-to-elbow welds in a 152 mm (6 in.) (NPS 6) diam line, operating in lean amine service at 50 deg C (120 deg F) and 2.9 MPa (425 psig). Thickness measurements indicated negligible loss of metal, and the leaks were clamped. A year later, 15 additional leaks were discovered, again at pipe-to-elbow welds in lean amine lines. Further nondestructive testing located other cracks, giving a total of 35. These lines had been in service for approximately eight years. Investigation (visual inspection, hardness testing, and micrographic cross-sections) supported the conclusion that the failure was caused by lean amine SCC. It was considered unlikely that these pipe welds had received such a postweld heat treatment, although it is industry practice to postweld stress relieve piping and pressure vessels in lean amine service if the temperature is expected to be above 95 deg C (200 deg F). Recommendations included inspecting all welds using shear wave ultrasonic testing and postweld heat treating all welds in lean amine service.