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S.J. Suess
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D. G. Chakrapani
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D. G. Chakrapani
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D. G. Chakrapani
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Philip J. Kenny
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D. G. Chakrapani
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Friedrich Karl Naumann, Ferdinand Spies
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Ronald J. Parrington
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Emanuele Mor, Eugenio Traverso, Giovanna Ventura
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047566
EISBN: 978-1-62708-235-8
... Abstract Handles welded to the top cover plate of a chemical-plant downcomer broke at the welds when the handles were used to lift the cover. The handles were fabricated of low-carbon steel rod; the cover was of type 502 stainless steel plate. The attachment welds were made with type 347...
Abstract
Handles welded to the top cover plate of a chemical-plant downcomer broke at the welds when the handles were used to lift the cover. The handles were fabricated of low-carbon steel rod; the cover was of type 502 stainless steel plate. The attachment welds were made with type 347 stainless steel filler metal to form a fillet between the handle and the cover. The structure was found to contain a zone of brittle martensite in the portion of the weld adjacent to the low-carbon steel handle; fracture had occurred in this zone. The brittle martensite layer in the weld was the result of using too large a welding rod and too much heat input, melting of the low-carbon steel handle, which diluted the austenitic stainless steel filler metal and formed martensitic steel in the weld zone. Because it was impractical to preheat and postheat the type 502 stainless steel cover plate, the low-carbon steel handle was welded to low-carbon steel plate, using low-carbon steel electrodes. This plate was then welded to the type 502 stainless steel plate with type 310 stainless steel electrodes. This design produced a large weld section over which the load was distributed.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047745
EISBN: 978-1-62708-235-8
... Abstract A 321 stainless steel radar coolant-system assembly fabricated by torch brazing with AWS type 3A flux, failed at the brazed joint when subjected to mild handling before installation, after being stored for about two years. It was revealed by visual examination of the failed braze...
Abstract
A 321 stainless steel radar coolant-system assembly fabricated by torch brazing with AWS type 3A flux, failed at the brazed joint when subjected to mild handling before installation, after being stored for about two years. It was revealed by visual examination of the failed braze that the filler metal had not covered all mating surfaces. Lack of a metallurgical bond between the brazing alloy and stainless steel and instead mechanical bonding of the filler metal to an oxide layer on the stainless steel surface was revealed by examination of the broken joint at the cup. It was indicated by the thickness of the oxide layer that the steel surface was not protected from oxidation by the flux during torch heating. It was concluded that the failure was caused by lack of a metallurgical bond between the brazing alloy and the stainless steel. Components made of 347 stainless steel (better brazeability) brazed with a larger torch tip (wider heat distribution) and AWS type 3B flux (better filler-metal flow) were recommended for radar coolant-system assembly.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047749
EISBN: 978-1-62708-235-8
... Abstract A type 321 stainless steel (AMS 5570) pressure-tube assembly that contained a brazed reinforcing liner leaked during a pressure test. Fluorescent liquid-penetrant inspection revealed a circumferential crack extended approximately 180 deg around the tube parallel to the fillet...
Abstract
A type 321 stainless steel (AMS 5570) pressure-tube assembly that contained a brazed reinforcing liner leaked during a pressure test. Fluorescent liquid-penetrant inspection revealed a circumferential crack extended approximately 180 deg around the tube parallel to the fillet of the brazed joint. The presence of multiple origin cracks was indicated on the inside surface of a fractured portion of the crack surface. The cracks had originated adjacent to the braze joining the tube and the reinforcing liner and propagated through the wall to the outer surface. The residues on the inner surface of the tube were identified as fluorides from the brazing flux by chemical analysis. The nature of the crack, potential for corrosion due to residual fluorides and residual swaging stress in the tube prior to brazing, confirmed that failure of the tube end was due to stress-corrosion cracking. Stress relief treatment of tube before brazing and immediate cleaning of brazing residual fluorides was recommended to avoid failure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047753
EISBN: 978-1-62708-235-8
... Abstract A pressure probe assembly comprised of type 347 stainless steel housing, brazed with AMS 4772D filler metal to the pressure probe, failed due to detachment of a rectangular segment from the housing. The presence of a large brazing metal devoid region in the pressure probe-housing joint...
Abstract
A pressure probe assembly comprised of type 347 stainless steel housing, brazed with AMS 4772D filler metal to the pressure probe, failed due to detachment of a rectangular segment from the housing. The presence of a large brazing metal devoid region in the pressure probe-housing joint was revealed by visual examination. Fatigue marks, emanating from multiple crack origins on the inside surface of the housing at the brazed joint were revealed by further study of the fracture. A poor metallurgical bond was confirmed by the presence of large irregular voids, flux trapped braze metal and separation between braze and housing.
Book Chapter
Weld Cracking of a Stainless Steel Heat Exchanger
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0091048
EISBN: 978-1-62708-235-8
... Abstract A welded ferritic stainless steel heat exchanger cracked prior to service. The welding filler metal was identified as an austenitic stainless steel and the joining method as gas tungsten arc welding. Investigation (visual inspection, SEM images, 5.9x images, and 8.9x/119x images etched...
Abstract
A welded ferritic stainless steel heat exchanger cracked prior to service. The welding filler metal was identified as an austenitic stainless steel and the joining method as gas tungsten arc welding. Investigation (visual inspection, SEM images, 5.9x images, and 8.9x/119x images etched with Vilella's reagent followed by electrolytic etching in 10% oxalic acid) supported the conclusion that the heat exchanger cracked due to weld cold cracking or postwelding brittle overload that occurred via flexure during fabrication. The brittle nature of the weld was likely due to a combination of high residual stresses, a mixed microstructure, inclusions, and gross grain coarsening. These synergistic factors resulted from extreme heat input during fillet welding. Recommendations included altering the welding variables such as current, voltage, and travel speed to substantially reduce the heat input.
Book Chapter
Embrittlement of Stainless Steel by Liquid Copper From a Welding Fixture
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047602
EISBN: 978-1-62708-235-8
... Abstract Parts of 21Cr-6Ni-9Mn stainless steel that had been forged at about 815 deg C (1500 deg F) were gas tungsten arc welded. During postweld inspection, cracks were found in the HAZs of the welds. Welding had been done using a copper fixture that contacted the steel in the area of the HAZ...
Abstract
Parts of 21Cr-6Ni-9Mn stainless steel that had been forged at about 815 deg C (1500 deg F) were gas tungsten arc welded. During postweld inspection, cracks were found in the HAZs of the welds. Welding had been done using a copper fixture that contacted the steel in the area of the HAZ on each side of the weld but did not extend under the tungsten arc. In SEM examination, the cracks appeared to be intergranular and extended to a depth of approximately 1.3 mm (0.05 in.). The crack appearance suggested that the surface temperature of the HAZ could have melted a film of copper on the fixture surface and that this could have penetrated the stainless steel in the presence of tensile thermal-contraction stresses. The cracks in the weldments were a form of liquid-metal embrittlement caused by contact with superficially melted copper from the fixture and subsequent grain-boundary attack of the stainless steel in an area under residual tensile stress. The copper for the fixtures was replaced by aluminum. No further cracking was encountered.
Book Chapter
Forming Cracks on Stainless Steel Wire
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0090932
EISBN: 978-1-62708-235-8
... Abstract Cold-drawn type 303 stainless steel wire sections, 6.4 mm (0.25 in.) in diameter, failed during a forming operation. All of the wires failed at a gradual 90 deg bend. Investigation (visual inspection and 5.3x/71x/1187x SEM views) supported the conclusion that the wires cracked due...
Abstract
Cold-drawn type 303 stainless steel wire sections, 6.4 mm (0.25 in.) in diameter, failed during a forming operation. All of the wires failed at a gradual 90 deg bend. Investigation (visual inspection and 5.3x/71x/1187x SEM views) supported the conclusion that the wires cracked due to ductile overload. The forming stresses were sufficient to initiate surface ruptures, suggestive of having exceeded the forming limit. Recommendations included examining the forming process, including lubrication and workpiece fixturing.
Book Chapter
Discoloration of a Stainless Steel Tube after Pickling
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001626
EISBN: 978-1-62708-235-8
... Abstract A type 17-4PH stainless steel tube exhibited brown discoloration after a pickling operation. EDS analysis of the extracted substance revealed relatively high levels of iron and chromium, along with lower amounts of aluminum, silicon, sulfur, chlorine, calcium, manganese, and nickel...
Abstract
A type 17-4PH stainless steel tube exhibited brown discoloration after a pickling operation. EDS analysis of the extracted substance revealed relatively high levels of iron and chromium, along with lower amounts of aluminum, silicon, sulfur, chlorine, calcium, manganese, and nickel. The iron, chromium, and nickel are likely in the form of dissolution products from the pickling solution. FTIR analysis revealed the presence of polypropylene and poly(ethylene:propylene). The EDS results showed that the discoloration of the tube was associated with oxidation products of the tube material, as well as adherent organic residue. Analysis by FTIR of the residue revealed detectable levels of two polymeric substances, which were later determined to be construction materials of the pickling tank. It was recommended that more frequent cleaning and/or replacement of the pickling solution be put into place and another type of tank material be considered.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0047615
EISBN: 978-1-62708-230-3
... Liquids Stress concentration Water chemistry Stainless steel Corrosion fatigue After 10 years of satisfactory operation, several economizer-tube failures occurred in a large black liquor recovery boiler for a paper mill. Several other areas of the boiler had experienced problems...
Abstract
After ten years of satisfactory operation, economizer-tube failures occurred in a large black liquor recovery boiler for a paper mill. The economizer contained 1320 finned tubes. Two fins ran longitudinally for most of the tube length and were attached by fillet welding on one side. The economizer tube leaks occurred at the end of the fin near the bottom of the economizer. A sample from a tube that had not failed showed heavy pitting attack on the inside of the tube, probably due to excess oxygen in the feedwater. Penetrant testing revealed numerous longitudinal cracks on the inside in the area of the fin tip. Cracking at the end of the fin-to-tube fillet weld was noted. The results indicate the failures were due to corrosion fatigue whose stresses were primarily thermally induced. A temporary solution included inspecting all tubes with shear-wave ultrasonics. Tubes with the most severe cracking were ground and repair welded. The square corners of the fins were trimmed back with a gradual taper so that expansion strains would be more gradually transferred to the tube surface. Water chemistry was closely evaluated and monitored, especially with regard to oxygen content.
Book Chapter
Failure of a Type 304 Stainless Steel White Liquor Transfer Pipeline
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001565
EISBN: 978-1-62708-230-3
... Abstract A stainless steel pipe transferring hot white liquor solution of sodium hydroxide and sodium sulfite, developed leaks adjacent to the welds within four years of service. The stainless steel pipe was AISI type 304 and welded with E308 weld electrodes. The service temperature was 190 deg...
Abstract
A stainless steel pipe transferring hot white liquor solution of sodium hydroxide and sodium sulfite, developed leaks adjacent to the welds within four years of service. The stainless steel pipe was AISI type 304 and welded with E308 weld electrodes. The service temperature was 190 deg C (375 deg F) and the solution contained approximately 700 ppm chlorides. Liquid penetrant inspection of the pipeline showed the leaks were numerous and confined adjacent to the welds. A metallographic specimen from the circumferential weld showed the cracks initiated at the inside surface. In addition to the base metal, SCC also had initiated at a notch at the weld root due to improper welding procedures. Failure was attributed to chloride-induced SCC with secondary contributory factors, including improper welding procedures. It was recommended that the pipeline be replaced with a material more resistant to SCC. The candidate materials are commercial grade unalloyed titanium or Inconel 600, which have superior resistance to SCC compared to austenitic stainless steels.
Book Chapter
Failure of a Stainless Steel Black Liquor Feed Pipe
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001564
EISBN: 978-1-62708-230-3
... Abstract An 8 in. diam stainless steel black liquor feed pipe to a carbon steel digester had failed within one year of service. The material was type 316 molybdenum-containing austenitic stainless steel. The service environment was alkaline black liquor at 175 deg C (350 deg F). The pipe had...
Abstract
An 8 in. diam stainless steel black liquor feed pipe to a carbon steel digester had failed within one year of service. The material was type 316 molybdenum-containing austenitic stainless steel. The service environment was alkaline black liquor at 175 deg C (350 deg F). The pipe had developed cracks on the inside surface coincident with an external support gusset. The cracks initiated at wide corrosion grooves. The early stages were corrosion-assisted fatigue cracks. The cracks initiated at the corrosion grooves and propagated as transgranular SCC with characteristic branching. Evaluation indicated the cracks were localized in an area of high cyclic stresses as a consequence of geometrical constraints on the piping and unsupported cantilever loads. No cracks were found elsewhere in the pipe. In the absence of highly localized service stresses (exceeding yield strength of the material), the corrosion grooving and subsequent SCC would not have occurred in this service environment. The pipe support system was modified with additional gussets to reduce the magnitude of cyclic stresses at the critical areas. The modification was apparently successful.
Book Chapter
Cracking of Stainless Steel Suction Roll in a Paper Machine
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001568
EISBN: 978-1-62708-230-3
... Abstract Two suction rolls at the first press section of a 25 ft. wide paper machine developed cracks within two years of service. The rolls were austenitic stainless steel castings made of ASTM A 351 Grade CF8M alloy containing molybdenum. The rolls were exposed to slightly acidic white water...
Abstract
Two suction rolls at the first press section of a 25 ft. wide paper machine developed cracks within two years of service. The rolls were austenitic stainless steel castings made of ASTM A 351 Grade CF8M alloy containing molybdenum. The rolls were exposed to slightly acidic white water (pH approximately 4.7) containing chlorides (45 ppm). Visual and liquid penetrant inspections of the rolls revealed extensive cracking at the roll inside surface. The cracks penetrated more than 30 percent of the wall thickness and a few cracks were several inches long. The cracks were preferentially oriented along the roll length and primarily at the roll inside surface. Field metallographic examination showed significant grain boundary chromium-carbide precipitation and intergranular corrosion. The roll failures were attributed to chromium depletion along the grain boundaries (sensitization) resulting from slow cooling of the casting to avoid large residual stresses. The roll manufacturer recommended a proprietary ferritic/austenitic stainless steel as the replacement material for the rolls.
Book Chapter
Stress-Corrosion Cracking of AISI 316 Stainless Steel
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001650
EISBN: 978-1-62708-230-3
... Abstract Several air heat exchangers failed in service in a pulp and paper operation. The tubes were made from AISI 316 stainless steel with an extruded aluminum fin mechanically bonded to the outside. Originally, the failures were blamed on poor tube to header welds. The units were sent back...
Abstract
Several air heat exchangers failed in service in a pulp and paper operation. The tubes were made from AISI 316 stainless steel with an extruded aluminum fin mechanically bonded to the outside. Originally, the failures were blamed on poor tube to header welds. The units were sent back to the manufacturer for repair. Some of the units failed the hydrostatic test after they were repaired. Microscopic examination revealed the presence of branched transgranular cracks characteristic of stress-corrosion cracking. Only some of the tubes failed and these did so by stress-corrosion cracking. The most probable primary cause of the stress-corrosion cracking was local high residual stresses indicated by the areas of high hardness in the tubes. Low halogens in the water and airborne corrodents found normally in a pulp and paper mill were all that were required in the presence of high residual stresses in the tubes to initiate stress-corrosion cracking. Use of a low-carbon grade of stainless steel such as 316L was recommended to facilitate formation of the tube without producing excessive residual stresses. It was recommended also that failed units be segregated until it can be determined if the failure was related to operating pressure or some other unique cause.
Book Chapter
Stress-Corrosion Cracking of Stainless Steel Falling Film Black Liquor Evaporator
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001567
EISBN: 978-1-62708-230-3
... Abstract A falling film black liquor evaporator consisted of flat twin plate heat exchangers and was used to increase black liquor solids content prior to its burning in the recovery boiler. Several plate heat exchangers were fabricated of AISI type 316L stainless steel by electric resistance...
Abstract
A falling film black liquor evaporator consisted of flat twin plate heat exchangers and was used to increase black liquor solids content prior to its burning in the recovery boiler. Several plate heat exchangers were fabricated of AISI type 316L stainless steel by electric resistance welding. Cracks initiated at the inside surface of the welded areas and penetrated through the wall thickness. In several locations, the weld fractured and the plates separated with significant spring back, indicative of high residual stresses attributed to fabrication and weld procedures. The cracks had extended radially from the electric resistant weld into the base metal. Metallographic examination revealed the cracks were transgranular and branching, characteristic of SCC in austenitic stainless steels. The fracture surfaces had a brittle cleavage-like appearance, typical of SCC in austenitic stainless steels. Chlorides in the service environment were a contributory factor. The primary factor causing SCC localized at the electric resistant welds was substantial residual stresses as a result of fabrication procedures. It was recommended that the heat exchanger plates be subjected to stress-relief heat treatment following fabrication and welding.
Book Chapter
Corroded Leaky Stainless Steel Pipes
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001168
EISBN: 978-1-62708-219-8
Abstract
Steel pipes, used for years in a food factory soft water preheater, were found to leak as a result of corrosion. The pipes, made of 18/8 steel, were immersed in steam maintained at 0.5 atm and 150 deg C. They carried desalinated process water, heating it to approximately 100 deg C. Inspection revealed a reddish-brown coating on the outside of the pipe with a few flat pitting holes and incipient cracks. Corrosion was also observed on the inner walls of the pipe, consisting of rust patches with pitting scars, branching out to predominantly transcrystalline cracks. In this case, leaking appears to be the result of a combination of pitting and stress corrosion, most likely due to chlorides. The factory was recommended to use molybdenum-alloyed steels (type 18/10 or 18/12) which are more resistant to local disruption of passivating films and pitting than molybdenum-free types such as 18/8.
Book Chapter
Analysis of Pitting and MIC of Stainless Steel Piping
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091201
EISBN: 978-1-62708-219-8
... Abstract Type 316L (UNS S31603) austenitic stainless steel piping was installed as part of a storm-sewer treatment collection system in a manufacturing facility. Within six months of start-up, leaks were discovered. Investigation (on-site current flow testing, visual inspection, water tests...
Abstract
Type 316L (UNS S31603) austenitic stainless steel piping was installed as part of a storm-sewer treatment collection system in a manufacturing facility. Within six months of start-up, leaks were discovered. Investigation (on-site current flow testing, visual inspection, water tests, and 5x/10x images etched in ASTM 89 reagent) supported the conclusion that the pitting in the austenitic stainless steel pipe was believed to be caused by damage to the passive layer brought about by a combination of MIC, high chloride levels, and high total dissolved solids. The low-flow and stagnant conditions present in the piping were primary contributors to the pit progression. Recommendations included replacing the pipe. Several alloys, nonmetallic materials, and lining materials were proposed for coupon testing to determine which would operate best in an environment with high levels of aerobic bacteria.
Book Chapter
Failure of a Stainless Steel Holding Tank
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001528
EISBN: 978-1-62708-219-8
... Abstract A 5000-gal (20,000-L) hot-water holding tank fractured at a large automotive manufacturing plant. The tank was made from Type 304 austenitic stainless steel. The inner diameter of the tank displayed a macroscopic, web-like network of cracks that deceptively suggested intergranular...
Abstract
A 5000-gal (20,000-L) hot-water holding tank fractured at a large automotive manufacturing plant. The tank was made from Type 304 austenitic stainless steel. The inner diameter of the tank displayed a macroscopic, web-like network of cracks that deceptively suggested intergranular stress-corrosion cracking. The problem, however, originated on the outside surface of the tank where a tensile stress (due to low applied stress and fabrication-induced residual stresses) accelerated the growth of numerous stress corrosion cracks that eventually broke through to the inner surface, causing leakage and ultimately failure.
Book Chapter
Intercrystalline Corrosion of Welded Stainless Steel Pipelines in Marine Environment
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001171
EISBN: 978-1-62708-219-8
... Abstract The defects observed along weldings of stainless steel pipelines employed in marine environments were evidenced by metallographic and electrochemical examination. A compilation of cases on the effect of defective weldings, in addition to improper choice of stainless steel for water...
Abstract
The defects observed along weldings of stainless steel pipelines employed in marine environments were evidenced by metallographic and electrochemical examination. A compilation of cases on the effect of defective weldings, in addition to improper choice of stainless steel for water pipelines, lead to the conclusion that intercrystalline corrosion in steels involved precipitation of a surplus phase at grain boundaries. Intercrystalline corrosion in austenitic stainless steels due to precipitation of chromium carbides during conditions generated due to welding and ways to avoid the precipitation (including reduction of carbon content, appropriate heat treatment, cold work of steel, reduction of austenitic grain size and stabilizing elements) were described. The presence of microcracks due to highly localized heat concentrations with consequent thermal expansion and considerable shrinkages during cooling was investigated. The specimens were taken from various sources including transverse and longitudinal welding seam, sensitized areas and it was concluded appropriate material selection with respect to medium could control some corrosion processes.
Book Chapter
Fatigue Fracture of a Type 316L Stainless Steel Angled Plate
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048413
EISBN: 978-1-62708-226-6
... Abstract A type 316L stainless steel angled plate failed. The fatigue fracture was found to have occurred at a plate hole. Symmetric cyclic bending forces were revealed by the fatigue damage at the fracture edge at the top surface of the plate. Fatigue striations and slip bands produced...
Abstract
A type 316L stainless steel angled plate failed. The fatigue fracture was found to have occurred at a plate hole. Symmetric cyclic bending forces were revealed by the fatigue damage at the fracture edge at the top surface of the plate. Fatigue striations and slip bands produced on the surface during cyclic loading were observed. The material was showed by the deformation structure to be in the cold-worked condition and was termed to not be the cause of the implant failure.
Book Chapter
Shearing Fracture of a Type 316LR Stainless Steel Screw
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048403
EISBN: 978-1-62708-226-6
... Abstract During the internal fixation, the type 316LR stainless steel cortical bone screw failed. Extensive spiral deformation was revealed by the fracture surface. Dimple structure characteristic of a ductile failure mode was observed with dimples oriented uniformly in the deformation...
Abstract
During the internal fixation, the type 316LR stainless steel cortical bone screw failed. Extensive spiral deformation was revealed by the fracture surface. Dimple structure characteristic of a ductile failure mode was observed with dimples oriented uniformly in the deformation direction. A zone of heavily deformed grains at the fracture edge was revealed by longitudinal metallographic examination. The shearing fractures of a commercially pure titanium screw and a cast cobalt-chromium-molybdenum alloy were discussed for purpose of comparison.
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