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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001753
EISBN: 978-1-62708-241-9
Abstract
A failure analysis investigation was conducted on a fractured aluminum tailwheel fork which failed moments after the landing of a privately owned, 1955 twin-engine airplane. Nondestructive evaluation via dye-penetrant inspection revealed no discernible surface cracks. The chemical composition of the sand-cast component was identified via optical emission spectroscopy and is comparable to an aluminum sand-cast alloy, AA 712.0. Metallographic evaluation via optical microscopy and scanning electron microscopy revealed a high degree of porosity in the microstructure as well as the presence of deleterious intermetallic compounds within interdendritic regions. Macrohardness testing produced hardness values which are noticeably higher than standard hardness values for 712.0. The primary fracture surfaces indicate evidence of mixed-mode fracture, via intergranular cracking, cleaved intermetallic particles, and dimpled cellular regions in the matrix. The secondary fracture surface demonstrates similar features of intergranular fracture.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001633
EISBN: 978-1-62708-221-1
Abstract
Failure analysis of a mobile harbor crane wheel hub that included SEM and EDS analyses demonstrated that the mechanism of failure was fatigue. The wheel hub was a ductile cast iron component that had been subjected to cyclic loading during a ten-year service period. The fracture surface of the fatigue failure also contained corrosion deposit, suggesting that cracking occurred over a period of time sufficient to allow corrosion of the cracked surfaces. Replacement and alignment of the failed wheel hub was recommended along with inspection of the nonfailed wheel hubs that remained on the crane.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001614
EISBN: 978-1-62708-225-9
Abstract
The damage to a screw on the head of a 1.8 liter personal car engine was nucleated as the result of common disadvantageous environmental influences and reversed loads leading to corrosion fatigue.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001732
EISBN: 978-1-62708-218-1
Abstract
Statistical techniques provide the design engineer with a powerful tool for the analysis of failure data. By means of an actual case study, steps required to design a test yielding statistically meaningful data and procedures used in graphical analysis of results are presented. The Weibull distribution is the statistical model used as a basis for these techniques. This method of failure analysis provides the engineer with clear, positive design direction.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001588
EISBN: 978-1-62708-221-1
... as to the circumstances, causes, and origins of this failure. FaAA evaluated relevant documentation and all physical evidence. Witnesses, staff, and consultants were interviewed regarding the design and manufacturing of the truss, as well as operation, controls, and maintenance. In order to reconstruct the collapse...
Abstract
On 23 Dec 1997, a portion of the main ore conveyor at a large mine collapsed onto a highway and shut down mine operations. The conveyor structure that collapsed was supported by a steel truss spanning 185 ft. Truss failure occurred just as the conveyor transport rate was increased to 8,260 tph. Under this total loading, which was only slightly above the regular operating condition, a poorly designed and fabricated transition joint in the west lower chord failed, thereby overloading other key structural members and causing the entire truss to collapse. Another contributing cause of the collapse was the transition joint welds, where the fracture originated. They were made with undersized fillet welds, 20% smaller than specified on the original fabrication drawing. Because of the poorly designed joint detail and the deficient welds, both of which concentrated stress and strain in the low ductility direction of the transition joint plate, lamellar tearing of plate material occurred at the boxed I-beam fillet weld attachment. Brittle fracture of this joint precipitated global collapse of the truss structure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001584
EISBN: 978-1-62708-236-5
... staff of Practical Failure Analysis does not want to take sides or favor either side of a case under litigation. Additionally, the PFA staff does not want the publication to be used to enhance or refute the position of either side of a pending case. The positions expressed by Dr. Rau in the inaugural...
Abstract
On 13 Dec 1994, two massive detonations leveled portions of an ammonium nitrate plant near Sioux City, IA. The primary explosion allegedly occurred in defectively-designed titanium sparger piping inside the neutralizer vessel. Investigation however, revealed the explosion occurred because of unsafe plant operations and poor maintenance procedures. Specifically, the ammonium nitrate within the 18,000 gal capacity neutralizer vessel had become contaminated and made highly acidic. The operators then injected superheated steam directly into the ammonium nitrate in the neutralizer vessel.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001431
EISBN: 978-1-62708-221-1
..., it is not yet an economical proposition to examine every welded detail by this means. As these examples show — no matter how good the reputation of the manufacturer, and the excellence and vigilance of his inspection and quality control staff — examples of criminal malpractice which could lead to serious...
Abstract
The sudden collapse of a tower crane on a building site resulted in severe injuries to the driver. Failure took place at the upper portion of the foundation or lowermost section. The mast sections were constructed from four main corner angles welded to end frames also made from angle sections which were gusseted and fitted with additional doubling plates in the corners where the jointing bolts were fitted. It was evident that the collapse was due to failure of the welds attaching the corner angles to an end frame. Many of the welds at the locations where failure occurred were of poor quality. The corner angles appeared to have been cut slightly shorter than the required dimensions. This was compensated in one case by the use of a weld build-up and in the other three by make-up pieces attached by welds of insignificant dimensions.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001612
EISBN: 978-1-62708-218-1
... edge distance and improper cleaning of the mating surfaces before welding may have contributed to the propensity to failure. Acknowledgments The cooperation and help rendered by the staff of the Materials Science & Technology Division, TCIRD during the investigation is greatly acknowledged...
Abstract
The fan used to cool a diesel engine fractured catastrophically after approximately 100 h of operation. The fan failed at a spider, which was resistance spot welded to a shim placed between two circular spiders of 3 mm thickness. The detailed analysis of the fracture indicated that the premature failure of the fan was due to inadequate bonding between the sheets at the weld nugget. The fracture was initiated from the nugget-plate interface. The inadequate penetration and lack of fusion between the steel sheets during resistance spot welding led to poor weld strength and the fracture during operation. The propensity to crack initiation and failure was accentuated by improper cleaning of the surfaces prior to welding and to inadequate nugget-to-sheet edge distance.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001613
EISBN: 978-1-62708-235-8
... to reduce the hardness after carburizing, completely eliminated the problem. Acknowledgments The cooperation and help rendered by the staff of the Materials Science & Technology Division, TCIRD during the investigation is greatly acknowledged by the author. The author is also thankful...
Abstract
The electroplated tappet adjusting screws used in diesel engines failed during initial bend testing. The analysis of the failure showed that the fracture was nucleated from the subsurface of the screw. The fracture surface was intergranular at the ID and OD region and microvoid coalescence in the center. The improper baking after electroplating of the screw led to H2-induced blistering/cracking. The high strength of the threaded region of the adjusting screw increased the failure propensity.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001656
EISBN: 978-1-62708-219-8
... obtained from the International Lead Zinc Research Organization and Argonne National Laboratories as portion of their OTEC research. The Electron Microscope Unit staff of the University of Sydney are thanked for their cooperation in these studies. References References 1. Roper H...
Abstract
Some corrosion processes in the presence of chlorides, for steel embedded in concrete, are described and illustrated with the aid of scanning electron microscope EDXA data. Observations made of failure surfaces of reinforcements removed from the concrete beams after being subjected to sinusoidal load fluctuations at 6.7 Hz in air, 3% NaCl solution, and natural sea water are described. Reinforcement types studied included: hot-rolled mild steel bar, hot-rolled alloyed high strength bar, cold-worked high strength bar, galvanized bar of all these three types, nickel-clad bar and epoxy-coated bar.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001720
EISBN: 978-1-62708-227-3
... of the hull plate and, indirectly, the integrity of the fuel oil tanks. Acknowledgments Assistance by the U.S.S. Arizona Memorial Staff, National Park Service, at Pearl Harbor, Hawaii and the Submerged Cultural Resources Unit, HPS, Santa Fe, New Mexico are gratefully acknowledged. They provided...
Abstract
Metallographic studies found that steel used to fabricate the U.S.S. Arizona battleship during original construction, 1913-1915 and reconstruction, 1929-1931 were consistent with the best materials available during each time period. Due to the force of the forward magazine detonation, the best steel available today would not have had any impact on the outcome. Heavy banding in steels from both periods could adversely affect the corrosion resistance under anaerobic conditions that prevail during a corrosion cycle that has developed under hard biofouling layers for over 58 years. Banding would have no effect on corrosion rate under aerobic conditions that may occur in local areas on the hull. In the part of the ship from which samples for this report were obtained, high temperatures above 1340 deg F did not occur. Hull plate samples from the submerged wreckage are not yet available. These samples will be important to confirm findings to this time and determine the remaining thickness of the hull plate and, indirectly, the integrity of the fuel oil tanks.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001615
EISBN: 978-1-62708-235-8
... of the material during upset forging. Strict control over the inclusion content in the raw material by changing the vendor eliminated the problem. Acknowledgments The cooperation and help rendered by the staff of Materials Science & Technology Division, TCIRD during the investigation is greatly...
Abstract
Carbon steel axle forgings were rejected due to internal cracks observed during final machining. To determine the cause of the cracks, the preforms of the forging were analyzed in detail at each stage of the forging. The analysis revealed a large central burst in the intermediate stage of the forging preform, which subsequently increased in the final stage. A high upset strain during forging, especially in the final stage, accentuated the center burst by high lateral flow of the metal. It was concluded that the center burst of the axle forging resulted from a high concentration of nonmetallic inclusions in the central portion of the raw bar stock rather than the usual problem of improper forging temperature. Strict control over the inclusion content in the raw material by changing the vendor eliminated the problem.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001487
EISBN: 978-1-62708-234-1
... possibilities and following discussions with the owners' engineering staff and the makers of the set, it was concluded that short circuits had developed in the rotor and this view was strengthened when a close cheek of the station records showed that an increase of excitation current for a given load condition...
Abstract
Copper shortening has been found to occur in the rotor windings of turbo alternators and takes the form of a progressive reduction in the length of the coils leading to distortion of the end windings. The trouble results from the high loading which develops between successive layers of the strip conductor due to centrifugal force. This leads to a high frictional binding force between turns and prevents axial expansion under normal heating in service. Rotor trouble which proved to be due to copper shortening was found in a set rated at 27.5 MW. It was manufactured in 1934 at which time silver-bearing copper was not available. The use of hard-drawn silver-bearing copper for a rewind, in conjunction with special attention to blocking up the end windings, is confidently expected to effect a complete cure.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006815
EISBN: 978-1-62708-329-4
... such a thing.” For example, the minimum allowable brake rotor thickness and the minimum allowable brake pad thickness were both specified in the maintenance manual for a passenger transit vehicle. The provider of the equipment assumed that the professional maintenance staff, in charge with the safe upkeep...
Abstract
The intent of this article is to assist the failure analyst in understanding the underlying engineering design process embodied in a failed component or system. It begins with a description of the mode of failure. This is followed by a section providing information on the root cause of failure. Next, the article discusses the steps involved in the engineering design process and explains the importance of considering the engineering design process. Information on failure modes and effects analysis is also provided. The article ends with a discussion on the consequence of management actions on failures.
Series: ASM Handbook
Volume: 11B
Publisher: ASM International
Published: 15 May 2022
DOI: 10.31399/asm.hb.v11B.a0006868
EISBN: 978-1-62708-395-9
..., the quality assurance staff from any or all of these groups, the business development or marketing group, and so on. Each project will require a different composition for this development team. The idea is to gather the stakeholders responsible for each functional piece of the development process...
Abstract
This article presents the benefits of selecting plastics for products to be manufactured. It discusses the four key considerations for plastic part design: material, process, tooling, and design. The article provides a detailed discussion of the development sequence for plastic parts. The basis for the development sequence is twofold: first, to create the best solution for the application, and second, to minimize potential project risks through careful and thoughtful work habits.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001591
EISBN: 978-1-62708-227-3
... the outfitting of the ship, to permit the loading of provisions on board for the voyage, to secure an adequate supply of coal because of a miners strike, and to conclude the hiring of the hotel staff and the ship's crew. The Voyage Shortly before noon on Wednesday, 10 April, the lines holding the RMS...
Abstract
On 14 April 1912, at 11:40 p.m., Greenland Time, the Royal Mail Ship Titanic on its maiden voyage was proceeding westward at 21.5 knots (40 km/h) when the lookouts on the foremast sighted a massive iceberg estimated to have weighed between 150,000 to 300,000 tons at a distance of 500 m ahead. Immediately, the ship’s engines were reversed and the ship was turned to port (left) in an attempt to avoid the iceberg. In about 40 sec, the ship struck the iceberg below the waterline on its starboard (right) side near the bow. The iceberg raked the hull of the ship for 100 m, destroying the integrity of the six forward watertight compartments. Within 2 h 40 min the RMS Titanic sank. Metallurgical examination and chemical analysis of the steel taken from the Titanic revealed important clues that allow an understanding of the severity of the damage inflicted on the hull. Although the steel was probably as good as was available at the time the ship was constructed, it was very inferior when compared with modern steel. The notch toughness showed a very low value (4 J) for the steel at the water temperature (-2 deg C) in the North Atlantic at the time of the accident.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001761
EISBN: 978-1-62708-241-9
... distribution along the crankshaft and could have resulted in overstressing some journal/ pin fillets, thereby enhancing failure. Acknowledgments This study was supported by Kuwait University under grant no. EM 04/06. The authors would like to thank the Faculty of Science for providing their facilities...
Abstract
An investigation of a damaged crankshaft from a horizontal, six-cylinder, in-line diesel engine of a public bus was conducted after several failure cases were reported by the bus company. All crankshafts were made from forged and nitrided steel. Each crankshaft was sent for grinding, after a life of approximately 300,000 km of service, as requested by the engine manufacturer. After grinding and assembling in the engine, some crankshafts lasted barely 15,000 km before serious fractures took place. Few other crankshafts demonstrated higher lives. Several vital components were damaged as a result of crankshaft failures. It was then decided to send the crankshafts for laboratory investigation to determine the cause of failure. The depth of the nitrided layer near fracture locations in the crankshaft, particularly at the fillet region where cracks were initiated, was determined by scanning electron microscope (SEM) equipped with electron-dispersive X-ray analysis (EDAX). Microhardness gradient through the nitrided layer close to fracture, surface hardness, and macrohardness at the journals were all measured. Fractographic analysis indicated that fatigue was the dominant mechanism of failure of the crankshaft. The partial absence of the nitrided layer in the fillet region, due to over-grinding, caused a decrease in the fatigue strength which, in turn, led to crack initiation and propagation, and eventually premature fracture. Signs of crankshaft misalignment during installation were also suspected as a possible cause of failure. In order to prevent fillet fatigue failure, final grinding should be done carefully and the grinding amount must be controlled to avoid substantial removal of the nitrided layer. Crankshaft alignment during assembly and proper bearing selection should be done carefully.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001616
EISBN: 978-1-62708-229-7
... by eliminating settlement of flue gas species. Care has been taken during assembly to avoid deep or severe dents (hammer blows, bending, etc.) on the tubes, which accelerated the corrosion in local regions. Acknowledgments The cooperation and help rendered by the staff of Materials Science...
Abstract
Severe pitting corrosion of a carbon steel tube was observed in the air preheater of a power plant, which runs on rice straw firing. Approximately 1450 tubes were removed from Stage 3 of the preheater (air inlet and flue gas outlet) due to corrosion and local bursting. Samples from Stage 2 (where corrosion was low) and Stage 3 (severe corrosion) were taken and subjected to visual inspection, SEM, x-ray diffraction, microhardness measurement, and chemical and microstructural analysis. It was determined that extended non-operation of the plant resulted in the settlement of corrosive species on the tubes in Stage 3. The complete failure of the tube occurred due to diffusion of these elements into the base metal and precipitation of potassium and chlorine compounds along the grain boundaries, with subsequent dislodging of grains. The nonmetallic inclusions acted as nucleating sites for local pitting bursting. Nonuniform heat transfer in Stage 3 operation accelerated the selective corrosion of front-end tubes. The relatively high heat transfer in this stage resulted in condensation of some corrosive gases and consequent corrosion. Continuous operation of the plant with some precautions during assembly of the tubes reduced the corrosion problem.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001473
EISBN: 978-1-62708-229-7
... sustained by the generator. The main lesson to be learned from the occurrence is that it is obviously desirable to ensure that all operating staff are fully conversant with the proper mode of synchronising and that they are periodically re-trained in what is, after all, an exacting operation. The risk...
Abstract
A combination of adverse factors was present in the disruption of a turbo-alternator gearbox. The major cause was the imposition of a gross overload far in excess of that for which the gearbox was designed. The contributory factors were a rim material (EN9 steel) that was inherently notch-sensitive and liable to rupture in a brittle manner. Discontinuities were present in the rims formed by the drain holes drilled in their abutting faces, and possibly enhanced by the stress-raising effect of microcracks in the smeared metal at their surfaces It is probable that the load reached a value in excess of the yield point within the delay time of the material so when the fracture was initiated, it was preceded by several microcracks giving rise to the propagation of a brittle fracture.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001548
EISBN: 978-1-62708-219-8
... be as independent as possible. Independent consultants generally will have more credibility in court than people from one's own staff who naturally have a vested interest in the outcome. In this case, had the defense retained expert assistance (including the retention of a wood technologist) at an earlier stage...
Abstract
In 1975, a manufacturer was awarded a contract to produce modular air-traffic control towers for the U.S. Navy. The specifications called for painted steel siding, but the manufacturer convinced the Navy to substitute aluminum-bonded-to-plywood panels that were provided by a supplier. In less than one year, the panels began to delaminate and the aluminum began to crack. It was found that the failure was the result of chloride-induced intergranular corrosion caused by chemicals in the adhesive and excessive moisture in the wood introduced during manufacturing.
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