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sintered
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Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001133
EISBN: 978-1-62708-214-3
... Abstract A femoral knee implant was returned to the casting vendor for analysis after exhibiting poor bond strength between the cast substrate and a sintered porous coating. Both the coating and the substrate were manufactured from a cobalt-chromium-molybdenum alloy. Metallographic analysis...
Abstract
A femoral knee implant was returned to the casting vendor for analysis after exhibiting poor bond strength between the cast substrate and a sintered porous coating. Both the coating and the substrate were manufactured from a cobalt-chromium-molybdenum alloy. Metallographic analysis indicated that a decarburized layer existed on all surfaces of the casting, which prevented bonding during the sintering thermal cycle. Bead-to-bead bonding within the coating appeared sufficient, and no decarburized layer was present on the bead surfaces. It was concluded that the decarburization did not occur during the sintering thermal cycle. It was recommended that the prosthetic manufacturer investigate atmosphere controls for all thermal cycles prior to coating.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001104
EISBN: 978-1-62708-214-3
... Abstract A Nicrofer 3718 sinter belt used in a sinter furnace operated at 965 deg C (1770 deg F) for the curing of nickel briquettes stretched and fractured after only 6 months in service. Macrofractographic, metallographic, and chemical analyses of several broken links of the woven belt...
Abstract
A Nicrofer 3718 sinter belt used in a sinter furnace operated at 965 deg C (1770 deg F) for the curing of nickel briquettes stretched and fractured after only 6 months in service. Macrofractographic, metallographic, and chemical analyses of several broken links of the woven belt and an unused section of new wire showed that the fracture resulted from sulfur attack and overheating during service. It was recommended that the sinter belt material be changed to Nicrofer 3220-H (alloy 800H).
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in Fatigue Fracture of Titanium Alloy Knee Prostheses
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1993
Fig. 11 Micrograph of surface of titanium alloy tibial tray where a sintered bead has fractured off. Note incomplete fusing of the bead to the tray.
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in Fatigue Fracture of Titanium Alloy Knee Prostheses
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1993
Fig. 12 Micrograph of sinter neck of titanium bead. Note appearance of fracture lines about the circumference of the bead neck.
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in Failures Related to Metal Additive Manufacturing
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 8 Binder jetting and sintering process. (a) Image of a layer of powder in midprint in the binder jet process. (b) Depowdering after the curing step
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Published: 15 May 2022
Fig. 51 Schematic drawing of the selective laser sintering additive manufacturing process
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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001265
EISBN: 978-1-62708-215-0
.... The sintered porous coating exhibited multiple regions where fatigue fracture of the neck region occurred, as well as indications that the sintering process did not fully incorporate the beads onto the substrate. Better process control during sintering and use of subsequent heat treatments to ensure a bimodal...
Abstract
Total knee prostheses were retrieved from patients after radiographs revealed fracture of the Ti-6A1-4 VELI metal backing of the polyethylene tibial component. The components were analyzed using scanning electron microscopy. Porous coated and uncoated tibial trays were found to have failed by fatigue. Implants with porous coatings showed significant loss of the bead coating and subsequent migration of the beads to the articulating surface between the polyethylene tibial component and the femoral component, resulting in significant third-body wear and degradation of the polyethylene. The sintered porous coating exhibited multiple regions where fatigue fracture of the neck region occurred, as well as indications that the sintering process did not fully incorporate the beads onto the substrate. Better process control during sintering and use of subsequent heat treatments to ensure a bimodal microstructure were recommended.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006838
EISBN: 978-1-62708-329-4
... considerations, and quality assurance. The emphasis is on the design and metallurgical aspects for the two main types of metal AM processes: powder-bed fusion (PBF) and directed-energy deposition (DED). The article also describes the processes involved in binder jet sintering, provides information on the design...
Abstract
This article provides an overview of metal additive manufacturing (AM) processes and describes sources of failures in metal AM parts. It focuses on metal AM product failures and potential solutions related to design considerations, metallurgical characteristics, production considerations, and quality assurance. The emphasis is on the design and metallurgical aspects for the two main types of metal AM processes: powder-bed fusion (PBF) and directed-energy deposition (DED). The article also describes the processes involved in binder jet sintering, provides information on the design and fabrication sources of failure, addresses the key factors in production and quality control, and explains failure analysis of AM parts.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001033
EISBN: 978-1-62708-214-3
... (1600 mu in.) diam type 304 stainless steel wire screening had been torn and pieces were missing. Scanning electron microscope revealed that the fracture had occurred at wire crossover locations by a fatigue mechanism. The problem was solved by sintering the individual screens into a single unit...
Abstract
An investigation of a Stirling engine after an aborted test run revealed that the regenerator screens had suffered substantial damage. During the run, the individual screens oscillated as the helium working fluid was shuttled through the regenerator. In localized areas, the 41 mu m (1600 mu in.) diam type 304 stainless steel wire screening had been torn and pieces were missing. Scanning electron microscope revealed that the fracture had occurred at wire crossover locations by a fatigue mechanism. The problem was solved by sintering the individual screens into a single unit.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0045926
EISBN: 978-1-62708-235-8
... Abstract A batch of bimetal foil/epoxy laminates was rejected because of poor peel strength. The laminates were manufactured by sintering a nickel/phosphorus powder layer to a copper foil, cleaning, then chromate conversion coating the nickel-phosphorus surface, and laminating the nickel...
Abstract
A batch of bimetal foil/epoxy laminates was rejected because of poor peel strength. The laminates were manufactured by sintering a nickel/phosphorus powder layer to a copper foil, cleaning, then chromate conversion coating the nickel-phosphorus surface, and laminating the nickel-phosphorus side of the clad bimetal onto an epoxy film, so that the end product contained nickel-phosphorus sandwiched between copper and epoxy, with a chromate conversion layer on the epoxy side of the nickel-phosphorus. Peel testing showed abnormally low adhesion strength for the bad batch of peel test samples. Comparison with normal-strength samples using XPS indicated an 8.8% Na concentration on the surface of the bad sample; the good example contained less than 1% Na on the surface. After 15 min of argon ion etching, depth profiling showed high concentrations of sodium were still evident, indicating that the sodium was present before the chromate conversion treatment was performed. A review of the manufacturing procedures showed that sodium hydroxide was used as a cleaning agent before the chromate conversion coating. Failure cause was that apparently the sodium hydroxide had not been properly removed during water rinsing. Thus, recommendation was to modify that stage in the processing.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001784
EISBN: 978-1-62708-241-9
... geometric design with sharp corners as stress raisers, and incomplete sintering evidenced by unsintered particles. These were determined to be the primary cause of failure, although inclusions on the fracture surface containing S and Al may have played a role as well. socket fracture stress raisers...
Abstract
A 13/16-in. hex socket failed while in use. Analysis (hardness testing, optical and scanning electron microscopy, and EDS) revealed that the socket was made of low carbon steel formed in a powder metallurgy process. A number of flaws were found including nonuniform wall thickness, poor geometric design with sharp corners as stress raisers, and incomplete sintering evidenced by unsintered particles. These were determined to be the primary cause of failure, although inclusions on the fracture surface containing S and Al may have played a role as well.
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Published: 01 January 2002
Fig. 26 Valve recession as a result of bench tests carried out isolating impact using a cast and a sintered seat insert material (both based on a tool steel matrix)
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Published: 15 January 2021
Fig. 36 Valve recession as a result of bench tests carried out isolating impact using a cast and a sintered seat insert material (both based on a tool steel matrix)
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Published: 15 January 2021
Fig. 13 Comparison between (a) Archard approach and (b) friction energy wear approach to quantify the wear evolution of a sintered steel displaying a significant fluctuation of the friction coefficient, depending on the loading condition. Adapted from Ref 42
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Published: 01 January 2002
Fig. 29 Examples of strength-limiting defects in ceramics. (a) Silicon inclusion in reaction-bonded silicon nitride. (b) Powder agglomerate in sintered silicon carbide. (c) Machining damage in hot pressed silicon nitride. SEM; picture widths (a) ∼150 μm. (b) ∼300 μm, (c) ∼150 μm. Source: Ref
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Published: 01 January 2002
Fig. 18 Impact crater area vs. compressive residual stress for impacts normal to the lay and compressive stresses perpendicular to the grinding direction (○), and for impacts perpendicular to the lay and compressive stresses parallel to the grinding direction (●), using sintered reaction
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Published: 15 January 2021
Fig. 20 Impact crater area versus compressive residual stress for impacts normal to the lay and compressive stresses perpendicular to the grinding direction (■) and for impacts perpendicular to the lay and compressive stresses parallel to the grinding direction (●), using sintered reaction
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Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003551
EISBN: 978-1-62708-180-1
... sintering. Technical ceramics nevertheless possess a fired density as close as possible to theoretical density (with small pores and very little apparent porosity—a major difference when compared to refractories). The refractory materials to be considered can be classified as: Basic refractories...
Abstract
This article provides a discussion on the structural ceramics used in gas turbine components, the automotive and aerospace industries, or as heat exchangers in various segments of the chemical and power generation industries. It covers the fundamental aspects of chemical corrosion and describes the corrosion resistance characteristics of specific classes of refractories and structural ceramics. The article also examines the prevention strategies that minimize corrosion failures of both classes of materials.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001361
EISBN: 978-1-62708-215-0
... the race was also of 17-4PH hardened to 26 to 35 HRc. The ball was constructed of 440C steel hardened to 55 to 62 HRc. The liner was a Teflon impregnated sintered bronze matrix. Visual Examination of General Physical Features Rod and Body The fracture surface was found to contain beach marks...
Abstract
A 17-4 PH steering actuator rod end body broke during normal take-off. Results of failure analysis revealed that the wall thickness of the race was much below the design limits, thus causing the race to rest on the body's swaged edges rather than on the load carrying centerline of the body. This assembly condition generated abnormal high loads on the swaged edges, ultimately resulting in fatigue failure. To prevent a recurrence of similar failure in the future, the dimensions of the race in the spherical bearing were changed, no further failure occurred.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047793
EISBN: 978-1-62708-217-4
.... The microstructure of the metal in the impeller exhibited scattered porosity and carbide particles and appeared to be a sintered powder metallurgy compact. Metallographic examination of a section through the damaged splines and of a section through the adjacent undamaged part of the same splines disclosed...
Abstract
Failure of a case hardened steel shaft incorporated fuel pump in a turbine-powered aircraft resulted in damage to the aircraft. The disassembled pump was found to be dry and free of any contamination. Damage was exhibited on the pressure side of each spline tooth in the impeller and the relatively smooth cavities and undercutting of the flank on this side indicated that the damage was caused by an erosion or abrasion mechanism. A relatively smooth worn area was formed at the center of each tooth due to an abrasive action and an undulating outline with undercutting was observed on the damaged side. Particles of sand, paint, or plastic, fibers from the cartridge, brass, and steel were viewed in the brown residue on the filter cartridge under a low power microscope and later confirmed by chemical analysis. Large amount of iron was identified by application of a magnet. It was concluded that the combined effect of vibration and abrasive wear by sand and metal particles removed from the splines damaged the shaft. Case hardened spline teeth surface was recommended to increase resistance to wear and abrasion.
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