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Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006810
EISBN: 978-1-62708-329-4
... Abstract In addition to failures in shafts, this article discusses failures in connecting rods, which translate rotary motion to linear motion (and conversely), and in piston rods, which translate the action of fluid power to linear motion. It begins by discussing the origins of fracture. Next...
Abstract
In addition to failures in shafts, this article discusses failures in connecting rods, which translate rotary motion to linear motion (and conversely), and in piston rods, which translate the action of fluid power to linear motion. It begins by discussing the origins of fracture. Next, the article describes the background information about the shaft used for examination. Then, it focuses on various failures in shafts, namely bending fatigue, torsional fatigue, axial fatigue, contact fatigue, wear, brittle fracture, and ductile fracture. Further, the article discusses the effects of distortion and corrosion on shafts. Finally, it discusses the types of stress raisers and the influence of changes in shaft diameter.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001620
EISBN: 978-1-62708-229-7
... Abstract Two vertical coal-pulverizer shafts at a coal-fired generation station failed after four to five years in service. One shaft was completely broken, and the other was unbroken but cracked at both ends. shaft material was AISI type 4340 Ni-Cr- Mo alloy steel, with a uniform hardness...
Abstract
Two vertical coal-pulverizer shafts at a coal-fired generation station failed after four to five years in service. One shaft was completely broken, and the other was unbroken but cracked at both ends. shaft material was AISI type 4340 Ni-Cr- Mo alloy steel, with a uniform hardness of approximately HRC 27. Metallographic examination of transverse sections through the surface-damaged areas adjacent to the cracks also showed additional small cracks growing at an angle of approximately 60 deg to the surface. The crack propagation mode appeared to be wholly transgranular. SEM examination revealed finely spaced striations on the crack surfaces, supporting a diagnosis of fatigue cracking. Crack initiation in the pulverizer shafts started as a result of fretting fatigue. Greater attention to lubrication was suggested, combined with asking the manufacturer to consider nitriding the splined shaft. It was suggested that the surfaces be securely clamped together and that an in-service maintenance program be initiated to ensure that the tightness of the clamping bolts was verified regularly.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047865
EISBN: 978-1-62708-225-9
... Abstract Splined rotor shafts (constructed from 1151 steel) used on small electric motors were found to miss one spline each from several shafts before the motors were put into service. Apparent peeling of splines on the induction-hardened end of each rotor shaft was revealed by visual...
Abstract
Splined rotor shafts (constructed from 1151 steel) used on small electric motors were found to miss one spline each from several shafts before the motors were put into service. Apparent peeling of splines on the induction-hardened end of each rotor shaft was revealed by visual and stereo-microscopic examination. One tooth on each shaft was found to be broken off. It was revealed by metallographic examination of an unetched section through the fractured tooth that the fracture surface was concave and had an appearance characteristic of a seam. Partial decarburization of the surface was revealed after etching with 1% nital. The presence of a crack, with typical oxides found in seams at its root, was disclosed by an unetched section through the shaft in an area unaffected by induction heating. The etched samples revealed similar decarburization as was noted on the fracture surface of the tooth. It was concluded that the seam had been present before the shaft was heat treated and these seams acted as stress raisers during induction hardening to cause the shaft failure. It was recommended that the specifications should specify that the shaft material should be free of seams and other surface imperfections.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001254
EISBN: 978-1-62708-225-9
... Abstract The specified elongation of 10% could not be achieved in several hollow pinion gear shafts made of cast Cr-Mo steel GS 35 Cr-Mo 5 3 that were heat treated to a strength of 90 kp/sq mm. The steel was melted in a basic 3 ton arc furnace and deoxidized in the furnace and in the pan...
Abstract
The specified elongation of 10% could not be achieved in several hollow pinion gear shafts made of cast Cr-Mo steel GS 35 Cr-Mo 5 3 that were heat treated to a strength of 90 kp/sq mm. The steel was melted in a basic 3 ton arc furnace and deoxidized in the furnace and in the pan with a total of 7 kg aluminum. Fracture of a tensile specimen occurred with low elongation and, apparently, also with low reduction of area. In some places it was coarse grained conchoidal. It was found that the exceptionally low elongation of the cast specimens was due to excessive deoxidation by aluminum.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001430
EISBN: 978-1-62708-236-5
... Abstract An intermediate shaft (3 in. diam), part of a camshaft drive on a large diesel engine, broke after two weeks of service. Failure occurred at the end of the taper portion adjacent to the screwed thread. The irregular saw-tooth form of fracture was characteristic of failure from...
Abstract
An intermediate shaft (3 in. diam), part of a camshaft drive on a large diesel engine, broke after two weeks of service. Failure occurred at the end of the taper portion adjacent to the screwed thread. The irregular saw-tooth form of fracture was characteristic of failure from torsional fatigue. A second shaft carried as spare gear was fitted and failure took place in a similar manner in about the same period of time. Examination revealed that the tapered portion of the Fe-0.6C carbon steel shaft had been built up by welding prior to final machining. A detailed check by the engine-builder established that the manufacture of these two shafts had been subcontracted. It was ascertained that the taper portions had been machined to an incorrect angle and then subsequently built-up and remachined to the correct taper. The reduction in fatigue endurance following welding was due to heat-affected zone cracking, residual stresses, the lower fatigue strength of the weld deposited metal, and weld defects.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0047823
EISBN: 978-1-62708-236-5
... Abstract High-horsepower electric motors were utilized to drive large compressors (made of 4340 steel shafts and gear-type couplings) required in a manufacturing process. The load was transmitted by two keys 180 deg apart. Six of the eight compressor shafts were found cracked in a keyway...
Abstract
High-horsepower electric motors were utilized to drive large compressors (made of 4340 steel shafts and gear-type couplings) required in a manufacturing process. The load was transmitted by two keys 180 deg apart. Six of the eight compressor shafts were found cracked in a keyway and one of them fractured after a few months of operation. Visual examination of fractured shaft revealed that the cracks originated from one of the keyways and propagated circumferentially around the shaft. The shaft and coupling slippage was indicated by the upset keys and this type of fracture. The shaft surface both near and in the keyways indicated fretting which greatly reduced the fatigue limit of the shaft metal and initiated fatigue cracks. Fatigue marks were observed on the fractured key. Repetitive impact loading was responsible for propagation of the cracks. The high cyclic bending stresses were caused by misalignment between the electric motor and compressor and were transmitted to the shaft through the geared coupling. Flexible-disk couplings capable of transmitting the required horsepower were installed on the shafts as a corrective measure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0047447
EISBN: 978-1-62708-230-3
... Abstract Small paddles used to mix pulp had experienced a high incidence of breakage through the shafts. In some of the shanks, shrinkage was found relatively close to the surface where threads had been cut all the length of the shaft. Chemistries were within normal CF-8M ranges. Metallography...
Abstract
Small paddles used to mix pulp had experienced a high incidence of breakage through the shafts. In some of the shanks, shrinkage was found relatively close to the surface where threads had been cut all the length of the shaft. Chemistries were within normal CF-8M ranges. Metallography showed the parts to be correctly heat treated. Cross sections of several of the parts showed pitting corrosion, and beneath the pits, stress-corrosion cracks in areas where the shafts had been bent during use. All the samples showed deep SCC in the areas where bending had occurred. In several cases, centerline shrinkage from inadequate risering had decreased life by reducing the cross-sectional area. Type CF-8M is not resistant to chloride SCC where the chloride concentration is considerable. The biggest problem was the bending of these parts. Deformed material with high residual stresses would always be susceptible to SCC. Redesign to lower stresses was essential. In addition, change to a high-strength duplex stainless steel with its higher strength and greater resistance to chlorides was recommended. Finally, the part must be adequately risered to produce solid shanks free from shrinkage.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001808
EISBN: 978-1-62708-180-1
... Abstract This article discusses failures in shafts such as connecting rods, which translate rotary motion to linear motion, and in piston rods, which translate the action of fluid power to linear motion. It describes the process of examining a failed shaft to guide the direction of failure...
Abstract
This article discusses failures in shafts such as connecting rods, which translate rotary motion to linear motion, and in piston rods, which translate the action of fluid power to linear motion. It describes the process of examining a failed shaft to guide the direction of failure investigation and corrective action. Fatigue failures in shafts, such as bending fatigue, torsional fatigue, contact fatigue, and axial fatigue, are reviewed. The article provides information on the brittle fracture, ductile fracture, distortion, and corrosion of shafts. Abrasive wear and adhesive wear of metal parts are also discussed. The article concludes with a discussion on the influence of metallurgical factors and fabrication practices on the fatigue properties of materials, as well as the effects of surface coatings.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001764
EISBN: 978-1-62708-241-9
...Results of the Optical Emission Spectroscopy Table 1 Results of the Optical Emission Spectroscopy The material chemistry of the failed Design 6 drive shafts and that of the nonfailed Design 1 and 6 drive shafts is very similar. Element, wt.% Failed Drive Shaft, Design 5/6 Nonfailed...
Abstract
High failure rates in the drive shafts of 40 newly acquired articulated buses was investigated. The drive shafts were fabricated from a low-carbon (0.45%) steel similar to AISI 5046. Investigators examined all 40 buses, discovering six different drive shaft designs across the fleet. All of the failures, a total of 14, were of the same type of design, which according to finite-element analysis, produces a significantly higher level of stress. SEM examination of the fracture surface of one of the failed drive shafts revealed fatigue striations near the OD and ductile dimpling near the ID, evidence of high-cycle fatigue. Based on the failure rate and fatigue life predictions, it was recommended to discontinue the use of drive shafts with the inferior design.
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in Stress-Corrosion Cracking in Mixer Paddle Shafts
> ASM Failure Analysis Case Histories: Pulp and Paper Processing Equipment
Published: 01 June 2019
Fig. 1 Stress-corrosion cracks in cast CF-8M mixer paddle shafts. Cracking was most extensive in deformed area of the shafts
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in Failure of a Coal-Pulverizer Shafts from a Generation Station
> ASM Failure Analysis Case Histories: Power Generating Equipment
Published: 01 June 2019
Fig. 1 Two failed coal-pulverizer shafts. The broken shaft is on the right; the cracked shaft is on the left. The arrow indicates the position of the bowl end crack in the cracked shaft.
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in Broken Structural Bolt
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
Fig. 8 Shafts. Microstructure of bolts, longitudinal sections, etch: Nital. 500 ×
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Published: 01 December 2019
Fig. 1 An on-site inspection and identification of replaced drive shafts identified 6 visually discernable designs among the 28 drive shafts inspected.
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Published: 01 December 2019
Fig. 9 Comparison of cross sections of the Design 1 and 6 drive shafts. The areas marked with circles are of particular concern because they differ in terms of fillet radii and cross-sectional area.
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Published: 01 December 2019
Fig. 10 Geometry used in the finite-element analysis for the Design 1 drive shafts
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Published: 01 December 2019
Fig. 11 Von Mises stress contours present in the Design 1 drive shafts subjected to 1356 N-m (1000 ft-lbf) torque. Maximum stress is 93.7 MPa (13.59 ksi) at the location indicated.
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Published: 01 December 2019
Fig. 12 Von Mises stress contours present in the Design 6 drive shafts subjected to 1356 N-m (1000 ft-lbf) torque. Maximum stress is 132 MPa (19.10 ksi) at the location indicated.
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001436
EISBN: 978-1-62708-235-8
... Abstract A 3 in. diam shaft was found to have suffered excessive wear on one of the journals and was built up by welding. While it was in the lathe prior to turning down the built-up region, a crack was discovered in the root of the oil-seal groove and subsequently the end of the shaft...
Abstract
A 3 in. diam shaft was found to have suffered excessive wear on one of the journals and was built up by welding. While it was in the lathe prior to turning down the built-up region, a crack was discovered in the root of the oil-seal groove and subsequently the end of the shaft was broken off with hammer blows. The fracture surface was duplex in nature, there being an annular region surrounding a central zone, which suggests that the fracture developed in two stages. Microscopic examination confirmed that the fracture was of the brittle type. The shaft material showed a microstructure typical of a medium-carbon steel (carbon approximately 0.4%) in the normalized condition, a material not weldable by ordinary methods. It was concluded that the post-welding crack arose primarily from the thermal contraction which developed in the weld metal on cooling. It is probable that if the built-up zone had extended beyond the oil seal groove, failure in the manner would not have occurred. Experience indicated however, that failure from fatigue cracking would still have been likely to occur.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001689
EISBN: 978-1-62708-233-4
... Abstract The drive shaft on a centrifugal pump fractured after five months of operation. The fracture occurred at a packing gland inside a sleeve against which the packing material sealed. The shaft and sleeve were of duplex stainless steel. In contrast to a previous conclusion that heating had...
Abstract
The drive shaft on a centrifugal pump fractured after five months of operation. The fracture occurred at a packing gland inside a sleeve against which the packing material sealed. The shaft and sleeve were of duplex stainless steel. In contrast to a previous conclusion that heating had caused property deterioration resulting in embrittlement and fracture, it was concluded that the shaft must have fractured (most probably by fatigue cracking originating at the change of section) and that heating had then taken place from friction between the rotating input shaft and the remaining part attached to the pump. High temperature was thus a result, not the cause, of the failure.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001368
EISBN: 978-1-62708-215-0
...Results of chemical analysis Table 1 Results of chemical analysis Element Laboratory shaft Analysis Reported by forge shop SAE 4140 specification Carbon 0.40 0.40 0.38–0.43 Manganese 0.86 0.84 0.75–1.00 Silicon 0.25 0.24 0.20–0.35 Phosphorus 0.016 0.012...
Abstract
A forged 4140 steel shaft that connected two runners in a hydroturbine failed catastrophically after approximately 5900 h of service. The runner and the mating section of the broken shaft were examined and tested by various methods. The results of the analyses indicated that the shaft failed by torsional fatigue starting at subsurface crack initiation sites. The forging contained regions of crack like flaws associated with particles rich in chromium, manganese, and iron. Fracture features indicated that the fatigue cracks propagated under a relatively low stress.
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