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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001441
EISBN: 978-1-62708-220-4
... forces tending to disrupt the joints radially, i.e. to collapse the pipe walls. This sequence of events would be repeated every time the pipes were cooled below freezing-point, sufficient water to refill any cavities that had become enlarged being drawn in when the ice within contracted on melting...
Abstract
Soft-soldered copper pipe joints used in refrigerating plants failed. The solder had not adhered uniformly to the pipe surface. In addition, there were some longitudinal grooves on the pipe surfaces, parts of which were not filled with solder. The unsoldered areas formed cavities within the joints, some of which had been in direct communication with the outsides via the grooves or interconnected cavities. On cooling, moisture condensed on the external surfaces. Some of this was drawn by capillary action into the cavities in open communication with the external surface. On continued cooling to below freezing-point, water that entered the cavities solidified. This was accompanied by a slight increase in volume, which collapsed the pipe walls. In the examples, the pipe ends had not been properly tinned. The solder used was found to be of the tin-antimony type, containing about 5% antimony, which is more difficult to use than the usual tin-lead alloys. The use of this particular type of solder was a contributory factor in the production of unsound joints in the samples examined.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001087
EISBN: 978-1-62708-214-3
...Abstract Abstract The repeated failure of rubber-covered rotors and volute liners in a flue gas desulfurization system after conversion from lime slurry reagent to limestone slurry reagent was investigated. The pump was a horizontal 50 x 65 mm (2 x 2.5 in.) Galiger pump with a split cast iron...
Abstract
The repeated failure of rubber-covered rotors and volute liners in a flue gas desulfurization system after conversion from lime slurry reagent to limestone slurry reagent was investigated. The pump was a horizontal 50 x 65 mm (2 x 2.5 in.) Galiger pump with a split cast iron case and open rotor (impeller). Both the case and the ductile iron rotor core were covered by natural rubber. Analyses conducted included surface examination of wear patterns, chemical analysis of materials, measurement of mechanical properties, and in-place flow tests. It was determined that the proximate cause of failure was cavitation and vortexing between the rotor and the lining. The root cause of the failure was the conversion from lime to limestone slurry without appropriate modification of the pump. Conversion to the limestone slurry resulted in fluid dynamics outside the operational limits of the pump. The recommended remedial action was replacement with a pump appropriately sized for the desired pressures and flow rates for limestone slurry.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0091622
EISBN: 978-1-62708-230-3
...Abstract Abstract A CF-8M (cast type 316) neck liner or manway was removed from the top of a digester vessel. Repeated attempts to repair the part in the field during its life cycle of many years had failed to keep the unit from leaking. The casting was a CF-8M modified with the molybdenum...
Abstract
A CF-8M (cast type 316) neck liner or manway was removed from the top of a digester vessel. Repeated attempts to repair the part in the field during its life cycle of many years had failed to keep the unit from leaking. The casting was a CF-8M modified with the molybdenum level at the top end of the range. The plate was standard 317L material. The filler metal was type 316, although marginal in molybdenum content. Investigation (visual inspection, chemical analysis, micrographs, and metallographic examination) supported the conclusion that the damage to the neck liner was due to Cl-SCC in an area of debris buildup. It appeared the original casting suffered SCC in a low-oxygen area high in chlorides from repeated wet/dry cycles where there was a buildup of debris. Recommendations included redesigning the neck liner to eliminate the abrupt change where there was debris buildup. If redesign was impossible, an alloy more resistant to Cl-SCC, such as a duplex stainless steel or a high-molybdenum (4 to 6%) austenitic stainless steel, should be used.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001472
EISBN: 978-1-62708-221-1
... resulted from fatigue due to the cumulative action of the repeated stresses which it had been subjected to during service. The shaft had been subjected to repeated stress applications sufficient to result in the initiation and development of a fatigue crack at the radial hole. To prevent a repetition...
Abstract
Severe damage to the jib of a dragline excavator resulted from failure of the shaft which carried the derricking sheaves at the apex of the "A" frame. Failure occurred within the hub of the center sheave of the group of three at the right-hand end of the shaft. The shaft was manufactured from a 0.5% carbon, 1% chromium steel heat treated to give a hardness value of 300 VDP. The material was in the hardened and tempered condition and showed no abnormalities which would predispose to early failure. The content of non-metallic matter was only of nominal amount. Failure of the shaft resulted from fatigue due to the cumulative action of the repeated stresses which it had been subjected to during service. The shaft had been subjected to repeated stress applications sufficient to result in the initiation and development of a fatigue crack at the radial hole. To prevent a repetition of the failure it was recommended that the stress-raising effect of the holes be reduced by chamfering or preferably rounding-off the edges. Furthermore, rotation of the shaft should be prevented so that the radial holes were positioned on the opposite side of the shaft.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0089617
EISBN: 978-1-62708-232-7
... the molten metal, flowing through a trough, was poured into the mold beginning at the bell end and ending with the spigot end being poured last. After the pipe had cooled, it was pulled out from the bell end of the mold, and the procedure was repeated. Investigation supported the conclusion that failure...
Abstract
A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten metal, flowing through a trough, was poured into the mold beginning at the bell end and ending with the spigot end being poured last. After the pipe had cooled, it was pulled out from the bell end of the mold, and the procedure was repeated. Investigation supported the conclusion that failure of the mold surface was the result of localized overheating caused by splashing of molten metal on the bore surface near the spigot end. In addition, the mold-wash compound (a bentonite mixture) near the spigot end was too thin to provide the proper degree of insulation and to prevent molten metal from sticking to the bore surface. Recommendations included reducing the pouring temperatures of the molten metal and spraying a thicker insulating coating onto the mold surface.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001901
EISBN: 978-1-62708-218-1
..., and repeated until no effervescence is observed. Automotive components Depolymerization Differential scanning calorimetry Housings Sensors Thermogravimetric analysis Polyoxymethylene (Other, miscellaneous, or unspecified) failure Thermogravimetric analysis (TGA) and differential scanning...
Abstract
Thermogravimetric analysis (TGA) and differential scanning calorimetry (DSC) were used to analyze an automotive polyoxymethylene (POM) sensor housing that was depolymerizing during service. It was found that a combination of heat, oxygen, and sulfuric acid attacked and caused premature failure of the part. POM should not be selected for automotive applications where elevated temperatures and acidic environments can exist. If exposure to acid is suspected, sodium bicarbonate should be applied to neutralize the surrounding environment, followed by copious quantities of water, and repeated until no effervescence is observed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001000
EISBN: 978-1-62708-229-7
..., microcracks, and aligned damage centers which showed up as voids upon repeated polish-etch cycles. Because of the local nature of creep damage that can occur, any inspection that involves in situ metallography must be conducted at exactly the right or critical position or the presence of damage may...
Abstract
Rupture occurred at a bend in a superheated steam transfer line between a header and a desuperheater of a boiler producing 230 t/h of steam at 540 deg C and 118 kPa. The boiler had operated for 77,000 h. Rupture occurred along the outer bend radius of the 168 mm diam tube, this being of 1 Cr, 0.5 Mo steel with a wall thickness of 14 mm. The design temperature of this tube was 490 deg C, but there is evidence that it was operating at a temperature much above 500 deg C. Metallographic analysis disclosed an advanced stage of creep damage accumulation in the form of local cracks, microcracks, and aligned damage centers which showed up as voids upon repeated polish-etch cycles. Because of the local nature of creep damage that can occur, any inspection that involves in situ metallography must be conducted at exactly the right or critical position or the presence of damage may not be detected.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001406
EISBN: 978-1-62708-229-7
... boiler, which failed to respond to repeated expansion. The leakage was traced to circumferential cracking in the portion of Fe-0.11C-0.46Mn-0.018S-0.011P tubes within the expanded region. Microscopic examination indicated that all cracks started from the outer surface of the tubes in the expanded portion...
Abstract
Caustic cracking is the term used to describe one of the forms in which stress-corrosion cracking manifests itself in carbon steels. In the present study, persistent leakage occurred after ten weeks of service from tube expansions in the steam and mud drum of a two-drum D type boiler, which failed to respond to repeated expansion. The leakage was traced to circumferential cracking in the portion of Fe-0.11C-0.46Mn-0.018S-0.011P tubes within the expanded region. Microscopic examination indicated that all cracks started from the outer surface of the tubes in the expanded portion. The form of cracking which was mostly intergranular. Examination at higher magnification disclosed that a selective attack had taken place on the carbide constituents of the pearlite grains. An alkaline deposit on the fireside surface of the tube resulted from the evaporation of boiler water which had found its way past the tube expansions. This indicated that this operation had not resulted in a satisfactorily tight joint.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001047
EISBN: 978-1-62708-214-3
... sheet joint allowed the Nox to condense and subsequently reboil. This, coupled with repeated repair welding in the area, reduced resistance to acid attack. Intergranular corrosion continued until failure. Recommendations included changing operating parameter inlet to prevent HNO3 condensation outside...
Abstract
An E-Brite /Ferralium explosively bonded tube sheet in a nitric acid condenser was removed from service because of corrosion. Visual and metallographic examination of tube sheet samples revealed severe cracking in the heat-affected zone between the outer tubes and the weld joining the tube sheet to the floating skirt. Cracks penetrated deep into the tube sheet, and occasionally into the tube walls. The microstructures of both alloys and of the weld appeared normal. Intergranular corrosion characteristic of end-grain attack was apparent. A low dead spot at the skirt / tube sheet joint allowed the Nox to condense and subsequently reboil. This, coupled with repeated repair welding in the area, reduced resistance to acid attack. Intergranular corrosion continued until failure. Recommendations included changing operating parameter inlet to prevent HNO3 condensation outside the inlet and replacement of the floating skirt with virgin material (i.e., material unaffected by weld repairs).
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001289
EISBN: 978-1-62708-215-0
...Abstract Abstract The repeated occurrence of random cracks in the fillet radius portion of low-alloy steel (38KhA) end frame forgings following heat treatment was investigated. Microstructural analyses were carried out on both the failed part and disks of the rolled bar from which the part...
Abstract
The repeated occurrence of random cracks in the fillet radius portion of low-alloy steel (38KhA) end frame forgings following heat treatment was investigated. Microstructural analyses were carried out on both the failed part and disks of the rolled bar from which the part was made. Subsurface cracks were found to be zigzag and discontinuous as well as intergranular in nature. A mixed mode of fracture involving ductile and brittle flat facets was observed. Micropores and rod-shaped manganese sulfide inclusions were also noted. The material had a hydrogen content of 22 ppm, and cracking was attributed to hydrogen embrittlement. Measurement of hydrogen content in the raw material prior to fabrication was recommended. Careful control of acid pickling procedures for descaling of the hot-rolled bars was also deemed necessary.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001382
EISBN: 978-1-62708-215-0
... testing. The fracture origin was typical of fatigue. The ultimate tensile strength of the bolt was in excess of requirements. Wear patterns indicated that the bolt had been frozen in position for a protracted period and subjected to repeated bending stresses, which resulted in fatigue cracking and final...
Abstract
A trunnion bolt that was part of a coupling in a metropolitan railway system failed in service, causing cars to separate. The bolt had been in service for more than ten years prior to failure. Visual examination showed that the failure resulted from complete fracture at the grease port and surface groove located at midspan. Drillings machined from the bolt underwent chemical analysis, which confirmed that the material was AISI 1045 carbon steel, in accordance with specifications. Two sections cut from the bolt were subjected to metallographic examination and hardness testing. The fracture origin was typical of fatigue. The ultimate tensile strength of the bolt was in excess of requirements. Wear patterns indicated that the bolt had been frozen in position for a protracted period and subjected to repeated bending stresses, which resulted in fatigue cracking and final complete fracture. It was recommended that proper lubrication procedures be maintained to allow free rotation of the bolts while in service.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001055
EISBN: 978-1-62708-214-3
...Abstract Abstract The repeated failure of a welded ASTM A283 grade D pipe that was part of a 6 km (4 mi) line drawing and conducting river water to a water treatment plant was investigated. Failure analysis was conducted on sections of pipe from the third failure. Visual, macrofractographic...
Abstract
The repeated failure of a welded ASTM A283 grade D pipe that was part of a 6 km (4 mi) line drawing and conducting river water to a water treatment plant was investigated. Failure analysis was conducted on sections of pipe from the third failure. Visual, macrofractographic, SEM fractographic, metallographic, chemical, and mechanical property (tension and impact toughness) analyses were conducted. On the basis of the tests and observations, it was concluded that the failure was the combined result of poor notch toughness (impact) properties of the steel, high stresses in the joint area, a possible stress raiser at the intersection of the spiral weld and girth weld, and sudden impact loading, probably due to water hammer. Use of a semi- or fully killed steel with a minimum Charpy V-notch impact value of 20 J (15 ft·lbf) at 0 deg C (32 deg F) was recommended for future water lines. Certified test results from the steel mill, procedure qualification tests of the welding, and design changes to reduce water hammer were also recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001736
EISBN: 978-1-62708-220-4
... between the plates and the pipe. The creep damage failure was attributed to repeated relaxation cycles of very high thermal stresses of resulting from the periodic shutdowns, temperature fluctuations during service, or both. This failure emphasized the information available from an evaluation...
Abstract
Leakage was detected at the welds between stiffening plates and the pipe in a transfer line carrying butane and related petrochemical compounds. The line and reinforcing rings were of AISI 316 stainless steel, the pipe being of 508 mm diam and 6.25 mm wall thickness. The design temperature and pressure were 621 deg C and 2.75 kPa, respectively, while the operating conditions were 579 deg C and 1.03 kPa. The line was insulated. Failure occurred after approximately 90,000 h of operation, shutdowns being approximately two per annum. The cracking occurred at the toe of welds between the plates and the pipe. The creep damage failure was attributed to repeated relaxation cycles of very high thermal stresses of resulting from the periodic shutdowns, temperature fluctuations during service, or both. This failure emphasized the information available from an evaluation of the operative creep mechanism, namely grain boundary sliding, relating to the periodic nature of the loading, with high residual stresses being present.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0089676
EISBN: 978-1-62708-224-2
...Abstract Abstract Chain link, a part of a mechanism for transferring hot or cold steel blooms into and out of a reheating furnace, broke after approximately four months of service. The link was cast from 2% Cr austenitic manganese steel and was subjected to repeated heating to temperatures...
Abstract
Chain link, a part of a mechanism for transferring hot or cold steel blooms into and out of a reheating furnace, broke after approximately four months of service. The link was cast from 2% Cr austenitic manganese steel and was subjected to repeated heating to temperatures of 455 to 595 deg C (850 to 1100 deg F). Examination included visual inspection, macrograph of a nital-etched specimen from an as-received chain link 1.85x, micrographs of a nital-etched specimen from an as-received chain link 100x/600x, normal microstructure of as-cast standard austenitic manganese steel 100x, micrograph of a nital-etched specimen that had been austenitized 20 min at 1095 deg C (2000 deg F) and air cooled 315x, and micrograph of the same specimen after annealing 68 h at 480 deg C (900 deg F) 1000x). Investigation supported the conclusions that the chain link failed in a brittle manner, because the austenitic manganese steel from which it was cast became embrittled after being reheated in the temperature range of 455 to 595 deg C (850 to 1100 deg F) for prolonged periods of time. The alloy was not suitable for this application, because of its metallurgical instability under service conditions.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001018
EISBN: 978-1-62708-217-4
..., fresh, and indicative of a shock type of failure pattern. Closer examination, however, showed a fatigue crack at one corner. At this point, there was definite evidence of progression and oxidation. It was concluded that the corner in question was subjected to repeated brinelling resulting from normal...
Abstract
Initial investigation showed that a landing gear failure was the result of a hard landing with no evidence of contributory factors. The objective of reexamination was to determine whether there was any evidence of metallurgical failure. The landing gear was primarily an AISI type 6150 Cr-V steel flat spring attached at the top end to the fuselage and at the bottom end to the axle. Failure occurred at the clamping point near the top end of this spring. The failure showed evidence of severe brinelling at one corner in the clamping area. The fracture surfaces were clean, fresh, and indicative of a shock type of failure pattern. Closer examination, however, showed a fatigue crack at one corner. At this point, there was definite evidence of progression and oxidation. It was concluded that the corner in question was subjected to repeated brinelling resulting from normal landing loads, probably accentuated by looseness in the clamping device. The resulting residual tensile stress lowered the effective fatigue strength at that point against drag and side loads.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001778
EISBN: 978-1-62708-241-9
... by initiation of fatigue cracks in the decarburized zone under conditions of repeated bending and unbending stresses superimposed on the static tensile load. wire rope brittle fracture decarburization steel grain-boundary cracks electron probe microanalysis tensile strength High-carbon steel (alloy...
Abstract
A locked coil track rope (LCTR) is essentially composed of wires (round and rail-shaped) laid helically in different layers. These wire ropes are sometimes used in conveyors carrying empty and loaded buckets in mining areas. During service, such wire ropes may fail prematurely due to disintegration/failure of individual groups of wires. To understand the genesis of LCTR wire failures, a detailed metallurgical investigation of failed rope wires was made and included visual examination, optical microscopy, scanning electron microscopy (SEM), and electron probe microanalysis (EPMA). Two types of failed wires were investigated; one is from a 40 mm diameter locked coil track rope and the other from a 53 mm locked coil track rope. Optical microscopy of failed round wires in the 53 mm diameter rope clearly revealed fully decarburized layers at the surface and a few grain-boundary cracks. From the location of the failure, it was clear that apart from static tensile loads, the wire ropes had been subjected to bending and unbending loads near the saddle, as fully loaded or empty buckets traveled access the conveyor. The SEM studies confirmed that the fracture had been caused by initiation of fatigue cracks in the decarburized zone under conditions of repeated bending and unbending stresses superimposed on the static tensile load.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001786
EISBN: 978-1-62708-241-9
... calculations) revealed areas of damage due to rubbing with evidence of cleavage fracture on the unaffected surfaces. The results of stress analysis indicated that repeated reversals of the spindle produced stresses exceeding the fatigue limit of the shaft material. These stresses led to the formation...
Abstract
A heavy duty facing lathe failed when the tool post caught one of the jaws on the rotating chuck, causing the spline shaft that drives the main spindle to fracture. A detailed analysis of the fracture surfaces (including fractography, metallography, and analytical stress calculations) revealed areas of damage due to rubbing with evidence of cleavage fracture on the unaffected surfaces. The results of stress analysis indicated that repeated reversals of the spindle produced stresses exceeding the fatigue limit of the shaft material. These stresses led to the formation of microcracks in a retaining ring groove that were accelerated to sudden failure when the tool post and chuck collided.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001349
EISBN: 978-1-62708-215-0
...Abstract Abstract The dished ends of a heavy water/helium storage tank manufactured from 8 mm (0.3 in.) thick type 304 stainless plate leaked during hydrotesting. Repeated attempts at repair welding did not alleviate the problem. Examination of samples from one dished end revealed...
Abstract
The dished ends of a heavy water/helium storage tank manufactured from 8 mm (0.3 in.) thick type 304 stainless plate leaked during hydrotesting. Repeated attempts at repair welding did not alleviate the problem. Examination of samples from one dished end revealed that the cracking was confined to the heat affected zone (HAZ) surrounding circumferential welds and, to a lesser extent, radial welds that were part of the original construction. Most of the cracks initiated and propagated from the inside surface of the dished ends. Microstructures of the base metal, HAZ, and weld metal indicated severe sensitization in the HAZ due to high heat input during welding. An intergranular corrosion test confirmed the observations. The severe sensitization was coupled with residual stresses and exposure of the assembly to a coastal atmosphere during storage prior to installation. This combination of factors resulted in failure by stress-corrosion cracking. Implementation of a new repair procedure was recommended. Repairs were successfully made using the new procedure, and all cracks in the weld repair zones were eliminated.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001352
EISBN: 978-1-62708-215-0
...Abstract Abstract Repeated failures of high-pressure ball valves were reported in a chemical plant. The ball valves were made of AFNOR Z30C13 martensitic stainless steel. Initial examination of the valves showed that failure occurred in a weld at the ball/stem junction end of austenitic...
Abstract
Repeated failures of high-pressure ball valves were reported in a chemical plant. The ball valves were made of AFNOR Z30C13 martensitic stainless steel. Initial examination of the valves showed that failure occurred in a weld at the ball/stem junction end of austenitic stainless steel sleeves that had been welded to the valve stem at both ends. Metallographic examination showed that a crack had been introduced into the weld by improper weld heat treatment. Stress concentration at the weld location resulting from an abrupt change in cross section facilitated easy propagation of the crack during operation. Proper weld heat treatment was recommended, along with avoidance of abrupt change in cross section near the weld. Due penetrant testing at the ball stem junction before and after heat treatment was also suggested.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001305
EISBN: 978-1-62708-215-0
... fracture. No defects were found that could have contributed to failure. The wheel conformed to the chemical, microstructural, and hardness requirements for class A wheels. Failure was attributed to repeated severe heating and cooling of the rim and flange due to brake locking or misapplication of the hand...
Abstract
An ASTM A 504 carbon steel railway car wheel that was used on a train in a metropolitan railway system failed during service, causing derailment. The wheel was completely fractured from rim to hub. Macrofractography of the fracture surface showed road grime, indicating that the crack had existed for a considerable time prior to derailment and initiated in the flange. Failure propagated from the flange across the rim and down the plate to the bore of the hub. Two zones that exhibited definite signs of heating were observed. The fracture initiation site was typical of fatigue fracture. No defects were found that could have contributed to failure. The wheel conformed to the chemical, microstructural, and hardness requirements for class A wheels. Failure was attributed to repeated severe heating and cooling of the rim and flange due to brake locking or misapplication of the hand brake. It was recommended that the brake system on the car be examined and replaced if necessary.