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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001181
EISBN: 978-1-62708-220-4
... Abstract A forged pressure vessel made from high temperature austenitic steel X8Cr-Ni-MoVNb 16 13 K (DIN 1.4988) failed. The widest part of the burst had fine cracks on the internal wall running longitudinally. When the internal wall was cleaned, numerous even finer cracks were exposed...
Abstract
A forged pressure vessel made from high temperature austenitic steel X8Cr-Ni-MoVNb 16 13 K (DIN 1.4988) failed. The widest part of the burst had fine cracks on the internal wall running longitudinally. When the internal wall was cleaned, numerous even finer cracks were exposed. On the fracture surfaces in this region an irregularly formed zone was visible in the direction of the internal wall and a fibrous oriented fracture zone towards the external wall. The fracture was typical of stress-corrosion cracking in austenitic steels. Vanadium trichloride was present and tensile stresses were of necessity set up by the internal pressure. Stress-corrosion cracking does not occur if one of the basic requirements is lacking. Because the chloride agent and tensile stresses were inevitably present, the only possible way to prevent future reoccurrence is to forge the entire pressure vessel from a material immune to stress-corrosion cracking or to use interchangeable linings of such a material. A nickel alloy could be considered.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001053
EISBN: 978-1-62708-214-3
... Abstract A carbon steel (ASTM A515 grade 70) pressure vessel failed by brittle fracture while being hydro tested in the fabricating shop. The fracture origin was a small crack at a welding arc strike associated with the toe of a nozzle weld. A fracture mechanics calculation indicated...
Abstract
A carbon steel (ASTM A515 grade 70) pressure vessel failed by brittle fracture while being hydro tested in the fabricating shop. The fracture origin was a small crack at a welding arc strike associated with the toe of a nozzle weld. A fracture mechanics calculation indicated that this imperfection, although small, initiated fracture because of the local geometry and stress conditions and the low toughness of the steel. It was recommended that (1) the probability of flaws be reduced by welding over or grinding out arc strikes, (2) the local stresses be lowered by post weld stress relief and improved weld toe geometry, and (3) toughness be improved by specifying fine-grain steel and/ or by normalizing.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001059
EISBN: 978-1-62708-214-3
... steel column in diglycol amine vacuum service had visible OD pitting in several areas above the insulation support rings. Circumstances Leading to Failure Although the column was used in diglycol amine vacuum service, previous service included pressurized operation. The pitted areas were...
Abstract
Field metallography and replication were performed on a type 316 stainless steel column in diglycol amine vacuum service to determine the cause of visible OD pitting on the column in several areas above the insulation support rings. The examination revealed transgranular stress-corrosion cracking beneath the pitted areas on the OD. The likely cause of the cracking was chloride stress corrosion, with chlorides deriving from the marine atmosphere and concentrating under the insulation around the support rings. A complete insulation evaluation, including repair or replacement, was recommended to prevent chloride buildup. Painting of the steel surface with an epoxy-phenolic or epoxy-coal tar was also suggested.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001137
EISBN: 978-1-62708-228-0
... Abstract Following a fracture mechanics “fitness-for-purpose” analysis of petroleum industry cold service pressure vessels, using the British Standard PD 6493, it was realized that an analogous approach could be used for the failure analysis of a similar pressure vessel dome which had failed...
Abstract
Following a fracture mechanics “fitness-for-purpose” analysis of petroleum industry cold service pressure vessels, using the British Standard PD 6493, it was realized that an analogous approach could be used for the failure analysis of a similar pressure vessel dome which had failed in service some years previously. The failed pressure vessel, with a diam of 2.5 m and several meters tall, had been made of 12 mm thick IZETT steel plate of the same type and heat treatment as used in the earlier fitness-for-purpose already measured. Examination of the fracture surfaces suggested, from fatigue striations manifested by SEM, that the vessel was subject to significant fatigue cracking, which was probably corrosion assisted. From COD measurements at the operating temperature of -130 deg C (-202 deg F), and a finite stress analysis, a fracture mechanics evaluation using BS PD6493 yielded realistic critical flaw sizes (in the range 51 to 150 mm). These sizes were consistent with the limited fracture surface observations and such flaws could well have been present in the vessel dome prior to catastrophic failure. For similar pressure vessels, an inspection program based on a leak-before-break philosophy was consequently regarded as acceptable.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0048819
EISBN: 978-1-62708-233-4
... Abstract A large pressure vessel that had been in service as a hydrogen sulfide (H2S) absorber developed cracks and began leaking at a nozzle. The vessel contained a 20% aqueous solution of potassium hydroxide (KOH), potassium carbonate (K2CO3), and arsenic. The vessel wall was manufactured...
Abstract
A large pressure vessel that had been in service as a hydrogen sulfide (H2S) absorber developed cracks and began leaking at a nozzle. The vessel contained a 20% aqueous solution of potassium hydroxide (KOH), potassium carbonate (K2CO3), and arsenic. The vessel wall was manufactured of ASTM A516, grade 70, low-carbon steel plate. A steel angle had been formed into a ring was continuously welded to the inside wall of the vessel. The groove formed by the junction of the lower tray-support weld and the top part of the weld around the nozzle was found to have a crack. Pits and scale near the crack origin were revealed by microscopic examination and cracking was found to be transgranular. Periods of corrosion alternated with sudden instances of cleavage, under a tensile load, along preferred slip planes were interpreted during examination with a microscope. It was concluded that the combination of the residual plus operating stresses and the amount of KOH present would have caused stress corrosion as a result of caustic embrittlement. It was recommended that the tray support should be installed higher on the vessel wall to prevent coincidence of the lower tray-support weld with the nozzle weld.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047641
EISBN: 978-1-62708-235-8
... Abstract A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding...
Abstract
A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding for the exterior surface of the weld. A segmented backup ring with a gas channel was used inside the vessel to shield the weld root. The pressure vessel failed due to contamination of the fusion zone by oxygen, which resulted when the gas shielding the root face of the weld was diluted by air that leaked into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region of the segmented backup ring was provided, and a fine-mesh stainless steel screen diffuser was incorporated in the channel section of the backup ring to prevent air from leaking in. A titanium alloy color chart was furnished to permit correlation of weld-zone discoloration with the degree of atmospheric contamination.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047144
EISBN: 978-1-62708-235-8
... Abstract During autofrettage of a thick-wall steel pressure vessel, a crack developed through the wall of the component. Certain forged pressure vessels are subjected to autofrettage during their manufacture to induce residual compressive stresses at locations where fatigue cracks may initiate...
Abstract
During autofrettage of a thick-wall steel pressure vessel, a crack developed through the wall of the component. Certain forged pressure vessels are subjected to autofrettage during their manufacture to induce residual compressive stresses at locations where fatigue cracks may initiate. The results of the autofrettage process, which creates a state of plastic strain in the material, is an increase in the fatigue life of the component. Analysis (visual inspection, 50x/500x unetched micrographs, and electron microprobe analysis) supports the conclusion that the fracture toughness of the steel was exceeded, and failure through the wall occurred because of the following reason: the high level of iron oxide found is highly abnormal in vacuum-degassed steels. Included matter of this nature (exogenous) most likely resulted from scale worked into the surface during forging. Therefore, it is understandable that failure occurred during autofrettage when the section containing these defects was subjected to plastic strains. Because the inclusions were sizable, hard, and extremely irregular, this region would effect substantial stress concentration. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001440
EISBN: 978-1-62708-235-8
.... The vessel was 11.5 in. diameter, 50 in. high, and the ends, 0.12 in. thick were dished outwardly to almost hemispherical form. It was designed for a working pressure of 30 atm. (440 p.s.i.), was of welded construction, and had been in use for ten years. At the centre of the top end it was fitted with a hand...
Abstract
A portable propane container with a name-plate soldered onto it exploded in service. When the vessel was inspected afterwards, it was found to have developed a crack in the top end plate. A portion of the end plate cut out to include the midlength and one termination of the crack was examined microscopically. This revealed that the crack was associated with intergranular penetration by molten metal. The microstructure in general was indicative of a good-quality mild steel. It was evident from that solder that was responsible for the penetration and that fused brass from the hand wheel had not played any part. Tensile stress was present at the time of the failure sufficiently high to enable solder penetration to take place. The use of soft solder as a medium for attaching name-plates directly on to stressed steel parts is not recommended. It would be preferable to use a welded-on patch plate or to employ one of the high-strength, non-metallic adhesives.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0048795
EISBN: 978-1-62708-220-4
... Abstract A large pressure vessel designed for use in an ammonia plant failed during hydrostatic testing. It was fabricated from ten Mn-Cr-Ni-Mo-V steel plates which were rolled and welded to form ten cylindrical shell sections and three forgings of similar composition. The fracture surfaces...
Abstract
A large pressure vessel designed for use in an ammonia plant failed during hydrostatic testing. It was fabricated from ten Mn-Cr-Ni-Mo-V steel plates which were rolled and welded to form ten cylindrical shell sections and three forgings of similar composition. The fracture surfaces were metallographically examined to be typical for brittle steel fracture and associated with the circumferential weld that joined the flange forging to the first shell section. Featureless facets in the HAZ were observed and were revealed to be the fracture-initiation sites. Pronounced banding in the structure of the flange forging was revealed by examination. A greater susceptibility to cracking was interpreted from the higher hardenability found within the bands. Stress relief was concluded to have not been performed at the specified temperature level (by hardness and impact tests) which caused the formation of hard spots. The mode of crack propagation was established by microstructural examination to be transgranular cleavage. It was concluded that failure of the pressure vessel stemmed from the formation of transverse fabrication cracks in the HAZ fostered by the presence of hard spots. It was recommended that normalizing and tempering temperatures be modified and a revised forging practice explored.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0048840
EISBN: 978-1-62708-220-4
...-stress levels after welding. Lamellar tearing Pressure vessels Strain aging Welded joints ASTM A201 Grade B Joining-related failures Brittle fracture A spherical carbon steel fixed-catalyst bed reactor failed after 20 years of service while in a standby condition ( Fig. 1 ). At the time...
Abstract
A spherical carbon steel fixed-catalyst bed reactor, fabricated from French steel A42C-3S, approximately equivalent to ASTM A201 grade B, failed after 20 years of service while in a standby condition. The unit was found to contain primarily hydrogen at the time of failure. The vessel had a type 304 stainless steel shroud around the catalyst bed as protection against the overheating that was possible if the gas bypassed the bed through the refractory material. The failure was observed to have begun at the toe of the shroud-support ring weld. The ring was found to have a number of small cracks at the root of the weld. The cleavage mode of fracture was confirmed by SEM. The presence of extensive secondary cracking and twinning (Neumann bands) where the fracture followed the line of the shroud-support ring was revealed by metallography. It was revealed by refinery maintenance records that the ring had been removed for hydrotest and welded without any postweld heat treatment. The final cause of failure was concluded to be cracking that developed during the installation of the new shroud ring. Stress-relief heat treatments were recommended to be performed to reduce residual-stress levels after welding.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001818
EISBN: 978-1-62708-180-1
... Abstract This article discusses the effect of using unsuitable alloys, metallurgical discontinuities, fabrication practices, and stress raisers on the failure of a pressure vessel. It provides information on pressure vessels made of composite materials and their welding practices. The article...
Abstract
This article discusses the effect of using unsuitable alloys, metallurgical discontinuities, fabrication practices, and stress raisers on the failure of a pressure vessel. It provides information on pressure vessels made of composite materials and their welding practices. The article explains the failure of pressure vessels with emphasis on stress-corrosion cracking, hydrogen embrittlement, brittle and ductile fractures, creep and stress rupture, and fatigue with examples.
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Published: 01 January 2002
Fig. 11 Large thick-wall pressure vessel that failed because of cracking in weld HAZ. (a) Configuration and dimensions (given in inches). (b) Shattered vessel. (c) General appearance of one fracture surface; arrow points to facet at fracture origin. (d) Enlarged view of region at arrow in (c
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Published: 01 January 2002
Fig. 15 Cracks in pressure vessel made of ASTM A515 carbon steel lined with type 405 stainless steel. Failure occurred at plug welds because of dilution of weld metal. (a) Micrograph of specimen through weld area etched in acid cupric chloride showing ASTM A515 carbon steel (top), interface
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Image
Published: 01 January 2002
Fig. 21 Large enclosed cylindrical pressure vessel that failed by SCC because of caustic embrittlement by potassium hydroxide. (a) View of vessel before failure and details of nozzle and tray support. Dimensions given in inches. (b) Micrograph showing corrosion pits at edge of fracture surface
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Published: 01 January 2002
Fig. 28 Fracture path of failed pressure vessel. The arrows indicate the direction of crack propagation as determined from the chevron markings on the fracture faces. The letters identify the individual plates.
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in Embrittlement of a 76 mm (3 in.) Stainless Steel Pipe and Liner From a Hydrogen Plant Quench Pot Vessel
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
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in Hydrotest Failure of a Carbon Steel Pressure Vessel[1]
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
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in Hydrotest Failure of a Carbon Steel Pressure Vessel[1]
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
Fig. 3 Schematic of the failed pressure vessel showing the location of the origin and the path of the propagating fracture. A and B indicate sections of the vessel selected for laboratory examination.
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in Hydrotest Failure of a Carbon Steel Pressure Vessel[1]
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
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in Failures of Pressure Vessels and Process Piping
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 28 (a) Large thick-walled pressure vessel that failed because of cracking in weld heat-affected zone (dimensions given in inches). (b) Shattered vessel. (c) General appearance of one fracture surface; arrow points to facet at fracture origin. (d) Enlarged view of region at arrow in (c
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