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piping system
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048791
EISBN: 978-1-62708-234-1
... Abstract Linear indications on the outer surface of a cross in a piping system were revealed by dye-penetrant examination. The cross was specified to be SA403 type WP 304 stainless steel. The cross had been subjected to induction-heating stress improvement. The linear indications on the cross...
Abstract
Linear indications on the outer surface of a cross in a piping system were revealed by dye-penetrant examination. The cross was specified to be SA403 type WP 304 stainless steel. The cross had been subjected to induction-heating stress improvement. The linear indications on the cross were located in wide bands running circumferentially below the cross-to-cap weld and above the cap-to-discharge-pipe weld. The material was found to conform to the requirements both in terms of hardness and strength. Intergranular cracks filled with oxide were observed on metallographic analysis of a sectioned and oxalic acid etched sample. The grain size was found to exceed the ASTM standard. No indications of sensitization were observed during testing with practice A of ASTM A 262. Definitive evidence of contaminants to support SCC as the failure mechanism was not disclosed during analysis. It was concluded that overheating or burning of the forging, which classically results in large grain size, intergranular fractures, and fine oxide particles dispersed throughout the grains was the possible reason for the failure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046991
EISBN: 978-1-62708-234-1
... Abstract The outlet-piping system of a steam-reformer unit failed by extensive cracking at four weld locations. The welded system consisted of Incoloy 800 (Fe-32Ni-21Cr-0.05C) pipe and fittings. The exterior surfaces of the system were insulated with rock wool that did not contain...
Abstract
The outlet-piping system of a steam-reformer unit failed by extensive cracking at four weld locations. The welded system consisted of Incoloy 800 (Fe-32Ni-21Cr-0.05C) pipe and fittings. The exterior surfaces of the system were insulated with rock wool that did not contain weatherproofing. On-site visual examination and magnetic testing indicated severe external corrosion of most of the piping. The system showed extensive cracking in weld HAZ. One specimen indicated that corrosion extended to a depth of 3.2 mm and cracks were seen at the edge of the cover bead and in the HAZ of the weld. Metallographic examination showed that cracking was intergranular and that adjacent grain boundaries had undergone deep intergranular attack. Examination at higher magnification revealed heavy carbide precipitation, primarily at grain boundaries, indicating that the alloy had been sensitized, which resulted from heating during welding. Electron probe x-ray microanalysis showed the outside surface of the tube did not have the protective chromium oxide scale normally found on Incoloy 800. The inside surface of the tube had a thin chromium oxide protective scale. This evidence supported the conclusions that the deep oxidation greatly decreased the strength of the weld HAZ and cracking followed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001559
EISBN: 978-1-62708-229-7
..., chloride, stress-corrosion cracking. Replacement decisions were based on the presence of SCC attack or heavy corrosion deposits indicative of extended exposure time to chloride-contaminated water. The existing uncracked pipe, about 75 percent of the piping in the system, was retained despite the presence...
Abstract
One inch diam Type 304 stainless steel piping was designed to carry containment atmosphere samples to an analyzer to monitor hydrogen and oxygen levels during operational and the design basis accident conditions that are postulated to occur in a boiling water reactor. Only one of six lines in the system had thru-wall cracks. Shallow incipient cracks were detected at the lowest elevations of one other line. The balance of the system had no signs of SCC attack. Chlorides and corrosion deposits in varying amounts were found throughout the system. The failure mechanism was transgranular, chloride, stress-corrosion cracking. Replacement decisions were based on the presence of SCC attack or heavy corrosion deposits indicative of extended exposure time to chloride-contaminated water. The existing uncracked pipe, about 75 percent of the piping in the system, was retained despite the presence of low level surface chlorides. Controls were implemented to insure that temperatures are kept below 150 deg F, or, walls of the pipe are moisture-free or the cumulative wetted period will never exceed 30 h.
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Published: 01 January 2002
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in Failure of an Incoloy 800 Piping System
> ASM Failure Analysis Case Histories: Failure Modes and Mechanisms
Published: 01 June 2019
Fig. 1 Schematic of Incoloy 800 outlet-piping system for a steam-reformer unit showing the four welds that failed by cracking. Dimensions given in inches
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Published: 15 January 2021
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in Uniform Corrosion of Copper Piping Caused by Microbiological Attack
> ASM Failure Analysis Case Histories: Failure Modes and Mechanisms
Published: 01 June 2019
Fig. 2 Micrograph of 19 mm (0.75 in.) copper piping in a closed-loop water system with MIC and erosion of the weak oxide layer. 20×. Courtesy of MDE Engineers, Inc.
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Published: 01 January 2002
Fig. 12 Micrograph of 19 mm (0.75 in.) copper piping in a closed-loop water system with MIC and erosion of the weak oxide layer. 20×. Courtesy of MDE Engineers, Inc.
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Image
Published: 15 January 2021
Fig. 12 Micrograph of 19 mm (0.75 in.) copper piping in a closed-loop water system with microbiologically induced corrosion and erosion of the weak oxide layer. Original magnification: 20×. Courtesy of MDE Engineers, Inc.
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001699
EISBN: 978-1-62708-234-1
.... The system primarily comprised of steel pipes with threaded connections for the 2-inch (46.32 cms) pipes, and bolted flanged couplings for the larger diameter pipes. The large pipes were up to 18 inches (55.72 cms) in diameter. The heat exchangers within the fan coil units mainly consisted of copper coils...
Abstract
A shopping mall in South Carolina was originally constructed in 1988 and a second phase completed in 1989. The HVAC system inside the mall included an open, recirculating condenser water loop that served various fan coil units located within tenant spaces. The system had a recirculating capacity of about 44,000 gal (166,000 L) of water. It consisted primarily of steel pipes fitted with threaded connectors on the 2 in. (46 cm) pipes and bolted flanged couplings on the larger pipes. Seven years following the completion of the mall, corrosion problems were noted at the outer and inner surfaces of the pipe. Visual observations on the inner diametral surfaces revealed that the pipes were, in almost all cases, filled with corrosion products. A significant amount of base metal loss was documented in all of the samples. The cause of the observed corrosion was determined to be a lack of corrosion monitoring and poor water quality. Pipe replacement and a regular water testing program were recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048361
EISBN: 978-1-62708-234-1
... Abstract Several failures occurred in 64-mm schedule 80 type 304 stainless steel (ASME SA-312, grade TP304) piping in a steam-plant heat-exchanger system near tee fittings at which cool water returning from the heat exchanger was combined with hot water from a bypass. Various portions...
Abstract
Several failures occurred in 64-mm schedule 80 type 304 stainless steel (ASME SA-312, grade TP304) piping in a steam-plant heat-exchanger system near tee fittings at which cool water returning from the heat exchanger was combined with hot water from a bypass. Various portions of the piping were subjected to temperatures ranging from 29 to 288 deg C. Each of the failures were revealed to consist of transgranular cracking in and/or close to the circumferential butt weld joining the tee fitting to the downstream pipe leg, where the hot bypass water mixed with the cool return water. The transgranular cracks suggested that thermal fatigue was a more likely cause of failure than SCC. It was concluded by temperature measurements that circumferential temperature gradients, in combination with inadequate flexibility in the piping system as a whole, had caused the failures. The tee fitting was redesigned to alleviate the thermal stress pattern.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001698
EISBN: 978-1-62708-222-8
... that there were inferior materials used in the plumbing system during construction of the subject homes. Several sections of copper pipe were removed from one residence that had reported severe leaking, and several segments of the copper piping at this location had to be replaced. The samples were analyzed...
Abstract
A residential subdivision near Tampa, FL was constructed in 1984 through 1985. Several sections of copper pipe were removed from one residence that had reported severe leaking. Visual examination revealed extensive pitting corrosion throughout the ID surfaces of the sample. Microscopic evaluation of a cross section of a copper pipe revealed extensive pitting corrosion throughout the inner diametral surfaces of the pipe. Some pits had penetrated through the wall thickness, causing the pin hole leaks. Analysis of a sample of water obtained from the subdivision revealed relatively high hardness levels (210 mg/l), high levels of sulfate ions (55 mg/l), a pH of 7.6 and a sulfate-to-chloride ratio of 3:1. Analysis of corrosion product removed from the ID surfaces of the pipe section revealed that an environment rich in carbonates existed inside the pipe, a result of the hard water supply. It was concluded that pitting corrosion was a result of the corrosive waters supplied by the local water utility. Waters could be rendered non-pitting by increasing their pH to 8 or higher and neutralizing the free carbon dioxide.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001339
EISBN: 978-1-62708-215-0
... Abstract The failure mode of through-wall cracking of a butt weld in a 5083-O aluminum alloy piping system in an ethylene plant was identified as mercury liquid metal embrittlement. As a result of this finding, 226 of the more than 400 butt welds in the system were ultrasonically inspected...
Abstract
The failure mode of through-wall cracking of a butt weld in a 5083-O aluminum alloy piping system in an ethylene plant was identified as mercury liquid metal embrittlement. As a result of this finding, 226 of the more than 400 butt welds in the system were ultrasonically inspected for cracking. One additional weld was found that had been degraded by mercury. A welding team experienced in repairing mercury contaminated piping was recruited to make the repairs. Corrective action included the installation of a sulfur-impregnated charcoal mercury-removal bed and replacement of the aluminum equipment that was in operation prior to the installation of the mercury-removal bed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046414
EISBN: 978-1-62708-234-1
... to the piping system and excluding air from the pump inlet. Impellers Pumps Bronze Cavitation wear Figure 1(a) shows the impeller from one of two water pumps that were taken out of service because of greatly reduced output. Both impellers showed considerable material loss over all the interior...
Abstract
Two water pumps were taken out of service because of reduced output. Visual inspection revealed considerable material loss in both impellers, which were 25.4 cm (10 in.) in diam x 1.3 cm (0.5 in.) wide and made from a cast bronze alloy. Several similar water pumps operating under nearly identical conditions, drawing water from an open tank through a standpipe, had no observable failures. Etched micrographs 100x of samples taken from the impellers showed clean, pockmarked, severely eroded surfaces, characteristic of cavitation damage. Investigation also revealed that considerable quantities of air were being drawn into the system when water in the supply tank dropped below a certain level. It was concluded that cavitation erosion (due to the uptake of air) caused metal removal and microstructural damage in the impellers. Recommendations included adding a water-level control to the piping system and excluding air from the pump inlet.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001701
EISBN: 978-1-62708-219-8
... Abstract A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials...
Abstract
A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials. The fittings were mechanically threaded assemblies. Temperatures ranged from 150 to 155 deg F (65.6 to 68.3 deg C). Leaks in the system had reportedly initiated immediately after the building had been placed in service. The cause of corrosion inside the steel pipes was attributed to tuberculation caused by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091336
EISBN: 978-1-62708-234-1
... Abstract A type 304 austenitic stainless steel tube (0.008 max C, 18.00 to 20.00 Cr, 2.00 max Mn, 8.00 to 10.50 Ni) was found to be corroded. The tube was part of a piping system, not yet placed in service, that was exposed to an outdoor marine environment containing chlorides. As part...
Abstract
A type 304 austenitic stainless steel tube (0.008 max C, 18.00 to 20.00 Cr, 2.00 max Mn, 8.00 to 10.50 Ni) was found to be corroded. The tube was part of a piping system, not yet placed in service, that was exposed to an outdoor marine environment containing chlorides. As part of the assembly, a fabric bag containing palladium oxide was taped to the tube. The palladium served as a “getter.” Investigation (visual inspection and EDS analysis of corrosion debris) supported the conclusion that chlorides and palladium both contributed to corrosion in the crevice created by the tape on the tube, which was periodically exposed to water. Recommendations included taking steps to prevent water from entering and being trapped in this area of the assembly.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001793
EISBN: 978-1-62708-241-9
... representation of wire spacers positioned on the external surface of the concentric pipe In the present case, the operation of a dynamic positioning ship was interrupted due to loss of pressure on the CPP system. Closer analysis revealed that the failure was concentrated at the concentric pipe inside...
Abstract
A controllable pitch propeller (CPP) on a dynamic positioning ship failed after eight months of operation. The CPP design consists of a hollow propeller shaft and a concentrically located pipe that operates inside. The pitch of the propeller blades is controlled hydraulically through the longitudinal displacement of the inner (concentric) pipe. Fractography, microstructural, microhardness, and chemical analyses revealed that the concentric pipe failed due to fatigue. Fatigue cracks initiated along longitudinal welds where wire spacers attach to the external surface of the pipe. The effect of crack-like defects, stress concentration at the weld toe, residual tensile stress, and lack of penetration contributed to a shorter fatigue crack initiation phase and premature failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091201
EISBN: 978-1-62708-219-8
... Abstract Type 316L (UNS S31603) austenitic stainless steel piping was installed as part of a storm-sewer treatment collection system in a manufacturing facility. Within six months of start-up, leaks were discovered. Investigation (on-site current flow testing, visual inspection, water tests...
Abstract
Type 316L (UNS S31603) austenitic stainless steel piping was installed as part of a storm-sewer treatment collection system in a manufacturing facility. Within six months of start-up, leaks were discovered. Investigation (on-site current flow testing, visual inspection, water tests, and 5x/10x images etched in ASTM 89 reagent) supported the conclusion that the pitting in the austenitic stainless steel pipe was believed to be caused by damage to the passive layer brought about by a combination of MIC, high chloride levels, and high total dissolved solids. The low-flow and stagnant conditions present in the piping were primary contributors to the pit progression. Recommendations included replacing the pipe. Several alloys, nonmetallic materials, and lining materials were proposed for coupon testing to determine which would operate best in an environment with high levels of aerobic bacteria.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091394
EISBN: 978-1-62708-227-3
... Abstract An austenitic stainless steel (type 316/316L stainless steel, schedule 40, 64 mm (2.5 in.) diam and larger) piping network used in the fire-sprinkler system in a large saltwater passenger and car ferry failed by rapid leaking. Operating conditions involved stagnant seawater at ambient...
Abstract
An austenitic stainless steel (type 316/316L stainless steel, schedule 40, 64 mm (2.5 in.) diam and larger) piping network used in the fire-sprinkler system in a large saltwater passenger and car ferry failed by rapid leaking. Operating conditions involved stagnant seawater at ambient temperatures. The pipe was in service for four weeks when three leaks appeared. Investigation (visual inspection and photographic images) supported the conclusion that the failure was caused by attack and corrosion damage of Cl ions in conditions that were ideal for three modes of highly accelerated pitting of austenitic stainless steel: the bottom surface, weld or HAZ pits, and crevices. Recommendations included proper material selection for piping, flanges, and weld rods with greater corrosion resistance. Proper filtering to prevent entrained abrasives and timely breakdown inspections were also advised.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001683
EISBN: 978-1-62708-234-1
... optically and with the scanning electron microscope. Cooling systems Heat affected zone Piping Welded joints 304 UNS S30400 Biological corrosion Discovery In mid-1991, a closed-loop cooling water system for a new production facility, which had not begun operation, developed leaks...
Abstract
Corrosion in a closed-loop cooling water system constructed of austenitic stainless steel occurred during an extended lay up of the system with biologically contaminated water. The characteristics of the failure were those of microbiologically influenced corrosion (MIC). The corrosion occurred at welds and consisted of large subsurface void formations with pinhole penetrations of the surfaces. Corrosive attack initiated in the heat affected zones of the welds, usually immediately adjacent to fusion lines. Stepwise grinding, polishing, and etching through the affected areas revealed that voids generally grew in the wrought material by uniform general corrosion. Tunneling or worm-holing was also observed, whereby void extension occurred by initiating daughter voids probably at flaws or other inhomogeneities. Selective attack occurred within the fusion zone, i.e., within the cast two-phase structure of the weld filler itself. The result was a void wall which consisted of a rough and porous ferritic material, a consequence of preferential attack of the austenitic phase and slightly lower rate of corrosive attack of the ferrite phase. The three-dimensional spongy surface was studied optically and with the scanning electron microscope.
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