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piping system

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048791
EISBN: 978-1-62708-234-1
... Abstract Linear indications on the outer surface of a cross in a piping system were revealed by dye-penetrant examination. The cross was specified to be SA403 type WP 304 stainless steel. The cross had been subjected to induction-heating stress improvement. The linear indications on the cross...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046991
EISBN: 978-1-62708-234-1
... Abstract The outlet-piping system of a steam-reformer unit failed by extensive cracking at four weld locations. The welded system consisted of Incoloy 800 (Fe-32Ni-21Cr-0.05C) pipe and fittings. The exterior surfaces of the system were insulated with rock wool that did not contain...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001559
EISBN: 978-1-62708-229-7
..., chloride, stress-corrosion cracking. Replacement decisions were based on the presence of SCC attack or heavy corrosion deposits indicative of extended exposure time to chloride-contaminated water. The existing uncracked pipe, about 75 percent of the piping in the system, was retained despite the presence...
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Published: 01 January 2002
Fig. 42 Microbiologically influenced corrosion in a cooling water piping system More
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Published: 01 June 2019
Fig. 1 Schematic of Incoloy 800 outlet-piping system for a steam-reformer unit showing the four welds that failed by cracking. Dimensions given in inches More
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Published: 15 January 2021
Fig. 36 Microbiologically influenced corrosion in a cooling water piping system More
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Published: 01 June 2019
Fig. 2 Micrograph of 19 mm (0.75 in.) copper piping in a closed-loop water system with MIC and erosion of the weak oxide layer. 20×. Courtesy of MDE Engineers, Inc. More
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Published: 01 January 2002
Fig. 12 Micrograph of 19 mm (0.75 in.) copper piping in a closed-loop water system with MIC and erosion of the weak oxide layer. 20×. Courtesy of MDE Engineers, Inc. More
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Published: 15 January 2021
Fig. 12 Micrograph of 19 mm (0.75 in.) copper piping in a closed-loop water system with microbiologically induced corrosion and erosion of the weak oxide layer. Original magnification: 20×. Courtesy of MDE Engineers, Inc. More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001699
EISBN: 978-1-62708-234-1
.... The system primarily comprised of steel pipes with threaded connections for the 2-inch (46.32 cms) pipes, and bolted flanged couplings for the larger diameter pipes. The large pipes were up to 18 inches (55.72 cms) in diameter. The heat exchangers within the fan coil units mainly consisted of copper coils...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048361
EISBN: 978-1-62708-234-1
... Abstract Several failures occurred in 64-mm schedule 80 type 304 stainless steel (ASME SA-312, grade TP304) piping in a steam-plant heat-exchanger system near tee fittings at which cool water returning from the heat exchanger was combined with hot water from a bypass. Various portions...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001698
EISBN: 978-1-62708-222-8
... that there were inferior materials used in the plumbing system during construction of the subject homes. Several sections of copper pipe were removed from one residence that had reported severe leaking, and several segments of the copper piping at this location had to be replaced. The samples were analyzed...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001339
EISBN: 978-1-62708-215-0
... Abstract The failure mode of through-wall cracking of a butt weld in a 5083-O aluminum alloy piping system in an ethylene plant was identified as mercury liquid metal embrittlement. As a result of this finding, 226 of the more than 400 butt welds in the system were ultrasonically inspected...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046414
EISBN: 978-1-62708-234-1
... to the piping system and excluding air from the pump inlet. Impellers Pumps Bronze Cavitation wear Figure 1(a) shows the impeller from one of two water pumps that were taken out of service because of greatly reduced output. Both impellers showed considerable material loss over all the interior...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001701
EISBN: 978-1-62708-219-8
... Abstract A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091336
EISBN: 978-1-62708-234-1
... Abstract A type 304 austenitic stainless steel tube (0.008 max C, 18.00 to 20.00 Cr, 2.00 max Mn, 8.00 to 10.50 Ni) was found to be corroded. The tube was part of a piping system, not yet placed in service, that was exposed to an outdoor marine environment containing chlorides. As part...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001793
EISBN: 978-1-62708-241-9
... representation of wire spacers positioned on the external surface of the concentric pipe In the present case, the operation of a dynamic positioning ship was interrupted due to loss of pressure on the CPP system. Closer analysis revealed that the failure was concentrated at the concentric pipe inside...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091201
EISBN: 978-1-62708-219-8
... Abstract Type 316L (UNS S31603) austenitic stainless steel piping was installed as part of a storm-sewer treatment collection system in a manufacturing facility. Within six months of start-up, leaks were discovered. Investigation (on-site current flow testing, visual inspection, water tests...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091394
EISBN: 978-1-62708-227-3
... Abstract An austenitic stainless steel (type 316/316L stainless steel, schedule 40, 64 mm (2.5 in.) diam and larger) piping network used in the fire-sprinkler system in a large saltwater passenger and car ferry failed by rapid leaking. Operating conditions involved stagnant seawater at ambient...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001683
EISBN: 978-1-62708-234-1
... optically and with the scanning electron microscope. Cooling systems Heat affected zone Piping Welded joints 304 UNS S30400 Biological corrosion Discovery In mid-1991, a closed-loop cooling water system for a new production facility, which had not begun operation, developed leaks...