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microstructural design

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Published: 01 June 2019
Fig. 5 Case of old design. Thick-walled part. Microstructure of crankcase, etch: Picral. 100 × More
Image
Published: 01 June 2019
Fig. 6 Case of old design. Thin-walled part. Microstructure of crankcase, etch: Picral. 100 × More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0090974
EISBN: 978-1-62708-235-8
...-and-tempered microstructure contained solidification shrinkage, inherently poor ductility, and type II Mn-S inclusions that are known to reduce ductility. The macro and microscale fracture features confirmed that the casting was likely in low-temperature service at the time of failure. The composition...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001793
EISBN: 978-1-62708-241-9
... months of operation. The CPP design consists of a hollow propeller shaft and a concentrically located pipe that operates inside. The pitch of the propeller blades is controlled hydraulically through the longitudinal displacement of the inner (concentric) pipe. Fractography, microstructural, microhardness...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001200
EISBN: 978-1-62708-221-1
... of the thin wall. It has a comparatively low strength. Fig. 5 Case of old design. Thick-walled part. Microstructure of crankcase, etch: Picral. 100 × Fig. 6 Case of old design. Thin-walled part. Microstructure of crankcase, etch: Picral. 100 × The fracture formation in the cylinder...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091761
EISBN: 978-1-62708-229-7
... to 6400 h of operation. Investigation (visual inspection, metallographic examination, and stress analysis) supported the conclusion that the differing microstructure of the airfoil resulted in changes in mechanical properties. Because normal operation includes cycling of loads and temperatures, the shroud...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001592
EISBN: 978-1-62708-228-0
... to “design out” flow disruption in the downhole assembly and apply a corrosion inhibitor program following NACE Standards RP0195 3 and MR0174. 2 4. Conclusion The studied failure cases revealed the importance of the material microstructure on the service life of sucker rods. Other factors...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0047212
EISBN: 978-1-62708-221-1
... to fracture. No evidence of a defective design, improper microstructure, high inclusion count, or other stress-raising condition was observed. No recommendations were made. Earthmoving equipment Plastic deformation Shafts (power) 4340 UNS G43400 Fatigue fracture A steering knuckle used...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001794
EISBN: 978-1-62708-241-9
... radius (the one required by design) and ultimately promoted fatigue initiation. Material characterization showed that the shaft was manufactured from low-alloy steel grade AISI 4340. The shaft was quenched and tempered at a high temperature, to achieve hardness value of 30 HRC. Microstructure...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001741
EISBN: 978-1-62708-234-1
... was designed to handle soft lignite coals but had been used to crush hard deep-mined anthracite coals. Anthracite Crushers Lignite Loads (forces) Taper roller bearings Carburized steel Rolling-contact wear Metallographic evidence of microstructural features in the shape of ‘butterflies’ ( Fig...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001582
EISBN: 978-1-62708-233-4
... in an earlier engine design. The rods were 380 mm long with a pitch diameter of 14.7 mm and were fabricated from drawn and rolled steel rods of AISI 4140 steel. The rods were hardened by austenitizing at 840 to 850 °C for 45 min, oil quenching to room temperature, tempering at 520 °C and air-cooling...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001688
EISBN: 978-1-62708-234-1
... interesting in that the conditions actually experienced may be very different from the design conditions or from those reported to be present. Original microstructures are often unknown but, if original unused samples of the materials can be obtained, they are very useful for the purpose of comparison...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047879
EISBN: 978-1-62708-234-1
... and not in the heat-affected zone of the forged steel shaft. Microscopic investigation and chemical analysis of the steel shaft revealed presence of martensite (offered a path of easy crack propagation) around the fusion line and dilution of the weld metal by the carbon steel shaft. The microstructure was found...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0047109
EISBN: 978-1-62708-233-4
.... That they failed in the threaded portion also suggests a stress-concentration effect. Recommendations included changing the material spec to a higher-strength material with greater impact strength. In this case, it was recommended that the stems, despite any possible design changes, be manufactured from an alloy...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0092155
EISBN: 978-1-62708-221-1
..., of the case as a result of several factors. Recommendations included reducing the high local stresses at the pitch line to an acceptable level with a design modification. Also suggested was specification of a core hardness of 35 to 40 HRC to provide adequate support for the case and to permit attainment...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047105
EISBN: 978-1-62708-225-9
... microscopy, and mechanical-property analysis) supported the conclusions that the alloy steel plate used in this application contained significant brittle microstructural fibering or banding. This condition produced considerable anisotropy in ductility and toughness as revealed by mechanical testing...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047541
EISBN: 978-1-62708-217-4
... with a weak grain-boundary network of ferrite that had not been corrected by postweld heat treatment. The combination of the cracks and this unfavorable microstructure provided a weakened condition that resulted in catastrophic, brittle fracture under normal applied loads. Corrective Measure The design...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006838
EISBN: 978-1-62708-329-4
... , respectively. Fig. 9 Microstructure of a binder jet part showing isotropic grain structure Fig. 10 Microstructure of laser powder-bed fusion build showing distinct nonisotropic weld patterns Design and Fabrication Sources of Failure The overall influence of AM processes on design...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001294
EISBN: 978-1-62708-215-0
...× Abstract A precipitation-hardened stainless steel poppet valve assembly used to shut off the flow of hydrazine fuel to an auxiliary power unit was found to leak. SEM and optical micrographs revealed that the final heat treatment designed for the AM-350 bellows material rendered the AM-355 poppet...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0090971
EISBN: 978-1-62708-222-8
... properties and alloy designation were not specified. Investigation (visual inspection, 187x SEM images, unetched 30x images, hardness testing, and chemical analysis) of both the failed adapter and an exemplar casting from known-good lot supported the conclusion that the casting failed as a result of brittle...