1-20 of 1709 Search Results for

micrograph

Follow your search
Access your saved searches in your account

Would you like to receive an alert when new items match your search?
Close Modal
Sort by
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046737
EISBN: 978-1-62708-229-7
... (manganese bronze). The bolts and nuts were made of copper alloy C46400 (naval brass, uninhibited). The water that was circulated through the tower had high concentrations of oxygen, carbon dioxide, and chloramines. Analysis (visual inspection, bend tests, fractographs, 50x unetched micrographs, 100x...
Image
Published: 01 December 1993
Fig. 3 Scanning electron micrograph of tail rotor blade failure origin. Micrograph shows lead wool ballast in aluminum spar bore cavity and fracture which initiated at bore wall. Approximately 13×. More
Image
Published: 01 December 1993
Fig. 4 Scanning electron micrograph of tail rotor blade failure origin. Micrograph shows multiple pits at origin with associated corrosion product. Beach marks are shown emanating from pits, typical of a fatigue failure mode. Approximately 63×. More
Image
Published: 01 June 2019
Fig. 2 Micrograph of corroded tube: (a) unetched micrograph of copper crystals; (b) copper crystals with nonmetallic inclusions; (c) twin boundaries in the copper crystals, and, (d) colinearity between twin and grain boundaries in the substrate alloy and the grown crystals. More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0089676
EISBN: 978-1-62708-224-2
... deg C (850 to 1100 deg F). Examination included visual inspection, macrograph of a nital-etched specimen from an as-received chain link 1.85x, micrographs of a nital-etched specimen from an as-received chain link 100x/600x, normal microstructure of as-cast standard austenitic manganese steel 100x...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091631
EISBN: 978-1-62708-229-7
.... This and additional investigation (visual inspection, and 250x micrograph etched with aqua regia) supported the conclusion that the tubing failed by chloride SCC. Chlorides in the steam condensate also caused corrosion of the inner surface of the tubing. Stress was produced when the tubing was bent during...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090881
EISBN: 978-1-62708-229-7
... fractographs, and micrographs) showed evidence of IGSCC initiating at the OD and IGA under ridgelike deposits that were analyzed and found to be slightly alkaline to very alkaline (caustic) in nature. Crack oxide analysis indicated sulfate levels in excess of expected values. The analysis supported...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001711
EISBN: 978-1-62708-229-7
... Abstract Failures of 10Cr-Mo9-10 and X 20Cr-Mo-V12-1 superheated pipes during service in steam power generation plants are described. Through micrographic and fractographic analysis, creep and overheating were identified as the cause of failure. The Larson-Miller parameter is computed...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046972
EISBN: 978-1-62708-217-4
... halfway from the leading edge to the trailing edge on the concave surface before ultimate failure occurred in dynamic tension. Analysis (including visual inspection, SEM, and 250x/500x micrographic examination) supported the conclusions that the blades failed due to thermal fatigue. Recommendations...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091674
EISBN: 978-1-62708-217-4
... Abstract Forged aluminum alloy 2014-T6 hinge brackets in naval aircraft rudder and aileron linkages were found cracked in service. The cracks were in the hinge lugs, adjacent to a bushing made of cadmium-plated 4130 steel. Investigation (visual inspection and 250X micrographs) supported...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091678
EISBN: 978-1-62708-217-4
... Abstract During a routine shear-pin check, the end lug on the barrel of the forward canopy actuator on a naval aircraft was found to have fractured. The lug was forged from aluminum alloy 2014-T6. Investigation (visual inspection, 2x views, and 140X micrographs etched with Keller's reagent...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047072
EISBN: 978-1-62708-217-4
... inspection, dye-penetrant inspection, and 10x/150x micrographs of sections etched with Keller's reagent) supports the conclusion that the outer shell of the bullet assembly separated from the stiffener because the four attachment clips fractured through the shell-to-clip spot welds. Fracture occurred...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047125
EISBN: 978-1-62708-217-4
... the roll mileage was reported, but about 300 days had elapsed between the date of manufacture and the date the wheel was removed from service. The analysis (visual inspection, macrographs, micrographs, electron microprobe) supported the conclusions that the wheel half failed by fatigue. The fatigue crack...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047165
EISBN: 978-1-62708-217-4
... inspection, and micrographs with deep etching in aqueous 20% sodium hydroxide) supported the conclusion that failure on both wheel halves was by fatigue caused by a forging defect resulting from abnormal transverse grain flow. The crack in the first wheel half occurred during service, and the surfaces became...
Image
Published: 01 January 2002
Fig. 9 Micrograph of the worn surface for a phenolic resin-aramid fiber composite ( Ref 29 ) showing partial coverage of the polymer pin by transfer film More
Image
Published: 01 January 2002
Fig. 7 Micrograph of a section through a copper-lead alloy bearing that failed by deleading. Light area at the upper surface is the copper matrix that remained after the alloy was depleted of lead. As-polished. 100× More
Image
Published: 01 January 2002
Fig. 23 Microstructural alterations in a 52100 steel bearing ring. (a) Micrograph of picral-etched section through a spalled area showing elongated bandlike microstructural alterations. 200×. At the top is a profile of the bottom of the spalled area. (b) Macrograph of part of the spalled area More
Image
Published: 01 January 2002
Fig. 10 Composite micrograph of a transverse section through a type 303(Se) stainless steel eye terminal for a wire rope showing corroded crack surface and final-fracture region. 75× More
Image
Published: 01 January 2002
Fig. 15 Scanning electron micrograph of fracture surface of fasteners shown in Fig. 14 . 880× More
Image
Published: 01 January 2002
Fig. 41(b) Micrograph showing the poor carbide distribution and morphology in the roll shown in Fig. 41(a) . The grain size, ASTM 6.75, was coarser than desired. Etched with 3% nital. 700× More