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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047125
EISBN: 978-1-62708-217-4
... that was removed from service because it developed a fatigue crack at a material defect. Detail A shows the area where the crack occurred and a view of the fracture surface revealed when the hub was broken open to examine the crack. View B-B, a macrograph of the fracture surface, shows the origin of the fatigue...
Abstract
A commercial aircraft wheel half, machined from an aluminum alloy 2014 forging that had been heat treated to the T6 temper, was removed from service because a crack was discovered in the area of the grease-dam radius during a routine inspection. Neither the total number of landings nor the roll mileage was reported, but about 300 days had elapsed between the date of manufacture and the date the wheel was removed from service. The analysis (visual inspection, macrographs, micrographs, electron microprobe) supported the conclusions that the wheel half failed by fatigue. The fatigue crack originated at a material imperfection and progressed in more than one plane because changes in the direction of wheel rotation altered the direction of the applied stresses. Recommendations included rewriting the inspection specifications to require sound forgings.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001154
EISBN: 978-1-62708-223-5
... which could be recognized as flaky cracks already in the fracture, and which later were united. No material defects could be detected in the cross section parallel to the fracture plane except for these very short cracks. These comparatively insignificant defects were sufficient to cause the fracture...
Abstract
The cause of fracture of two piston rods of hammers of a drop forge was determined. The first rod of 180 mm diam consisted of an unalloyed steel with 0.37% C and 0.67% Mn and had a strength of 56 kp/sq mm at 26% elongation. Fatigue fractures propagated from several points which could be recognized as flaky cracks already in the fracture, and which later were united. No material defects could be detected in the cross section parallel to the fracture plane except for these very short cracks. These comparatively insignificant defects were sufficient to cause the fracture during high impact fatigue stresses in the drop forge. The second piston rod of 120 mm diam consisted of a steel with 0.25% C and 1.00% Mn. It allegedly had 57 kp/sq mm tensile strength and 26% elongation. The basic structure of the 120 mm piston rod was ferritic-pearlitic and hardness of 155 Brinell was accordingly low, corresponding to approximately 53 kp/sq mm tensile strength. The incipient fractures had no connection with the material defects in this shaft and therefore the fracture could not have been caused by them. Probably the low strength of the piston rod was insufficient for the high stresses.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001255
EISBN: 978-1-62708-232-7
... shaped steel castings with 0.8 to 1.0% C, 1% Mn, 1% Cr, 0.5% Mo and 0.4% Ni and were heat treated to a tensile strength of 950 N/sq mm. Because the bending stress on mounting was only 42 N/sq mm in the fracture cross section, it was evident at the outset that material defects had promoted the fracture...
Abstract
Several back up rolls of 1400 mm barrel diam from a broad strip mill broke after a relatively short operating time as a result of bending stresses when the rolls were dismantled. The fracture occurred in the conical region of the neck at about 600 mm diam. The rolls were shaped steel castings with 0.8 to 1.0% C, 1% Mn, 1% Cr, 0.5% Mo and 0.4% Ni and were heat treated to a tensile strength of 950 N/sq mm. Because the bending stress on mounting was only 42 N/sq mm in the fracture cross section, it was evident at the outset that material defects had promoted the fracture. In the case of this roll and the other broken rolls, the cracking and fracture were promoted by various casting defects. Investigation of the rolls showed that both the breaking off of the neck and the disintegration of the barrel edges was caused by material defects, more exactly casting defects. The fractures on the other rolls examined were so badly rusted or contaminated that they were incapable of yielding any information.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001016
EISBN: 978-1-62708-236-5
... proportion of the fracture area was fresh and bright. It was concluded that this was a fresh fracture which occurred during shipment, and the crack itself was not present prior to shipment. The fact that a material defect of some sort was present and probably determined the location of the crack...
Abstract
An automatic press for making burlap bags had been used for several years. The press failed after being shipped by truck for a distance of about 400 mi. The objective was to determine whether failure occurred during or before shipment. The large piece which broke off the press included a section of the ways and a heavy adjustable mechanism which normally rides on these ways. The weight of the broken section was estimated at several hundred pounds. There was no support for the broken piece beyond the point of breakage. The material was a commercial cast iron, and the largest proportion of the fracture area was fresh and bright. It was concluded that this was a fresh fracture which occurred during shipment, and the crack itself was not present prior to shipment. The fact that a material defect of some sort was present and probably determined the location of the crack was apparently not significant as far as its usage was concerned. The failure could have been avoided by providing support underneath the overhanging member.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001192
EISBN: 978-1-62708-234-1
... of the main bearing and ran across the jaw almost to the opposite fillet of the adjoining connecting rod bearing. The fillet was well rounded and smoothly machined. Thus, no reason for the fracture of the crankshaft could be found externally. No material defects were discernible in the origin or anywhere else...
Abstract
The fracture cause had to be determined in a three-cylinder crankshaft made of chrome steel 34Cr4 (Material No. 1.7033) according to DIN 17200. The fracture occurred after only 150 h of operation. The fracture was of the bend fatigue type which originated in the fillet of the main bearing and ran across the jaw almost to the opposite fillet of the adjoining connecting rod bearing. The fillet was well rounded and smoothly machined. Thus, no reason for the fracture of the crankshaft could be found externally. No material defects were discernible in the origin or anywhere else. No cause for the crank fracture could be established from material testing. Probably the load was too high for the strength of the crank. Tensile strength could have been increased for the same material by tempering at lower temperature. Additionally, the resistance against high bend fatigue stresses or torsion fatigue stresses could have been increased substantially by including the fillet in the case hardening process.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006836
EISBN: 978-1-62708-329-4
... of spring failures are also discussed. In addition, the article discusses common causes of failures and presents examples of specific spring failures, describes fatigue failures that resulted from these types of material defects, and demonstrates how improper fabrication can result in premature fatigue...
Abstract
Mechanical springs are used in mechanical components to exert force, provide flexibility, and absorb or store energy. This article provides an overview of the operating conditions of mechanical springs. Common failure mechanisms and processes involved in the examination of spring failures are also discussed. In addition, the article discusses common causes of failures and presents examples of specific spring failures, describes fatigue failures that resulted from these types of material defects, and demonstrates how improper fabrication can result in premature fatigue failure. It also covers failures of shape memory alloy springs and failures caused by corrosion and operating conditions.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003512
EISBN: 978-1-62708-180-1
...Abstract Abstract This article provides an overview of the structural design process and discusses the life-limiting factors, including material defects, fabrication practices, and stress. It details the role of a failure investigator in performing nondestructive inspection. The article...
Abstract
This article provides an overview of the structural design process and discusses the life-limiting factors, including material defects, fabrication practices, and stress. It details the role of a failure investigator in performing nondestructive inspection. The article provides information on fatigue life assessment, elevated-temperature life assessment, and fitness-for-service life assessment.
Image
in Failures Related to Metal Additive Manufacturing
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 3 Defects in selective-laser-melted (SLM) materials. (a) Porosity formed in SLM Ti-6Al-4V. (b) Balling. (c) Hot tears. Source: Ref 26
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Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003500
EISBN: 978-1-62708-180-1
..., namely, design deficiencies, material defects, manufacturing/installation defects, and service life anomalies, with examples. The article describes several common charting methods that may be useful in performing an RCA. It also discusses other failure analysis tools, including review of all sources...
Abstract
This article briefly introduces the concepts of failure analysis and root cause analysis (RCA), and the role of failure analysis as a general engineering tool for enhancing product quality and failure prevention. It reviews four fundamental categories of physical root causes, namely, design deficiencies, material defects, manufacturing/installation defects, and service life anomalies, with examples. The article describes several common charting methods that may be useful in performing an RCA. It also discusses other failure analysis tools, including review of all sources of input and information, people interviews, laboratory investigations, stress analysis, and fracture mechanics analysis. The article concludes with information on the categories of failure and failure prevention.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046146
EISBN: 978-1-62708-217-4
... side of the lubrication hole since no material defects were found at the failure origin. Recommendations included redesign of the lubrication hole, shot peeing of the faces of the lug for added resistance to fatigue failure, and changing of the forging material to aluminum alloy 7175-T736 for its...
Abstract
The torque-arm assembly (aluminum alloy 7075-T73) for an aircraft nose landing gear failed after 22,779 simulated flights. The part, made from an aluminum alloy 7075-T73 forging, had an expected life of 100,000 simulated flights. Initial study of the fracture surfaces indicated that the primary fracture initiated from multiple origins on both sides of a lubrication hole that extended from the outer surface to the bore of a lug in two cadmium-plated flanged bushings made of copper alloy C63000 (aluminum bronze) that were press-fitted into each bored hole in the lug. Sectioning and 2x metallographic analysis showed small fatigue-type cracks in the hole adjacent to the origin of primary fracture. Hardness and electrical conductivity were typical for aluminum alloy 7075. This evidence supported the conclusion that the arm failed in fatigue cracking that initiated on each side of the lubrication hole since no material defects were found at the failure origin. Recommendations included redesign of the lubrication hole, shot peeing of the faces of the lug for added resistance to fatigue failure, and changing of the forging material to aluminum alloy 7175-T736 for its higher mechanical properties.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001414
EISBN: 978-1-62708-221-1
... along this same edge. Failure was initiated at the extrados which suggested that a discrepancy in the size of the pin may have contributed to failure. Microscopic examination of a section through the main origin did not reveal any material defects or the presence of weld repairs which could have led...
Abstract
The fracture of a clevis which formed part of the derricking gear of a large crane showed well developed conchoidal markings. These were associated with a principal origin on the outer surface at about the mid-width of the section. A number of secondary origins were apparent along this same edge. Failure was initiated at the extrados which suggested that a discrepancy in the size of the pin may have contributed to failure. Microscopic examination of a section through the main origin did not reveal any material defects or the presence of weld repairs which could have led to the premature failure. Furthermore, there were no indications that corrosion had contributed to the fatigue cracking.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001263
EISBN: 978-1-62708-224-2
...Abstract Abstract After several years' use, an eyebolt suffered brittle fracture in the first turn of the thread. The fracture started at the notch at the root of the thread. Neither localized material defect nor an old crack were present. The investigation showed that instead of the specified...
Abstract
After several years' use, an eyebolt suffered brittle fracture in the first turn of the thread. The fracture started at the notch at the root of the thread. Neither localized material defect nor an old crack were present. The investigation showed that instead of the specified steel quality St 37-2 N, a steel with about 0.5% C had been used. The microstructure with the coarse ferrite network indicated that the forged eye bolt had been normalized either at too high a temperature or not at all. In any case the anneal at 900 deg C produced a considerably more finely grained structure. In addition, the nature of the fracture and the results of the notched bar impact tests showed that in spite of the high C-content, the eye bolt had become brittle as a result of aging.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0001813
EISBN: 978-1-62708-180-1
...Abstract Abstract This article discusses the common causes of failures of springs, with illustrations. Design deficiencies, material defects, processing errors or deficiencies, and unusual operating conditions are the common causes of spring failures. In most cases, these causes result...
Abstract
This article discusses the common causes of failures of springs, with illustrations. Design deficiencies, material defects, processing errors or deficiencies, and unusual operating conditions are the common causes of spring failures. In most cases, these causes result in failure by fatigue. The article describes the operating conditions of springs, common failure mechanisms, and presents an examination of the failures that occur in springs.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001242
EISBN: 978-1-62708-223-5
...) according to DIN 17200. Microstructural examination showed the shaft had ran hot, and there were no material defects. The shaft probably was overstressed by torsion forces. The presence of surface checks on both sides of the cam lobe that were filled with bearing metal proved that overstressing occurred...
Abstract
During dismantling of an eccentric camshaft of 340 mm diam that had worked for a total of 450,000 load reversals, it was found that it had cracked on both sides of the eccentric cam. The shaft was made of chromium-molybdenum alloy steel 34 Cr-Mo4 (Material No. 1.7220) according to DIN 17200. Microstructural examination showed the shaft had ran hot, and there were no material defects. The shaft probably was overstressed by torsion forces. The presence of surface checks on both sides of the cam lobe that were filled with bearing metal proved that overstressing occurred through galling of the end faces of the bearing liners.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001274
EISBN: 978-1-62708-215-0
...Abstract Abstract A laminated-paper microwave food tray collapsed with hot food in it. Microscopic examination of the failed tray revealed no structural or material defects. Five additional trays of like construction were also tested to determine the conditions necessary to simulate...
Abstract
A laminated-paper microwave food tray collapsed with hot food in it. Microscopic examination of the failed tray revealed no structural or material defects. Five additional trays of like construction were also tested to determine the conditions necessary to simulate the permanent deflection of the tray handles that had occurred in the failed tray. Full distortion of the handles was obtained experimentally only by dropping a full hot tray on its end onto the floor. The test results indicated that the tray had slipped from the hand of the user.
Image
Published: 30 August 2021
Fig. 25 Scanning electron photograph showing the failure origin relative to the tool mark as a result of forming the spring. No internal material defect was found near the failure origin
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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001362
EISBN: 978-1-62708-215-0
...Abstract Abstract Numerous cracks observed on the surface of a forged A470 Class 4 alloy steel steam turbine rotor disc from an air compressor in a nitric acid plant were found to be the result of caustic induced stress-corrosion cracking (SCC). No material defects or anomalies were observed...
Abstract
Numerous cracks observed on the surface of a forged A470 Class 4 alloy steel steam turbine rotor disc from an air compressor in a nitric acid plant were found to be the result of caustic induced stress-corrosion cracking (SCC). No material defects or anomalies were observed in the disc sample that could have contributed to crack initiation or propagation or secondary crack propagation. Chlorides detected in the fracture surface deposits were likely the primary cause for the pitting observed on the disc surfaces and within the turbine blade attachment area. It was recommended that the potential for water carryover or feedwater induction into the turbine be addressed via an engineering evaluation of the plant's water treatment procedures, steam separation equipment, and start-up procedures.
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006778
EISBN: 978-1-62708-295-2
...Abstract Abstract This article aims to identify and illustrate the types of overload failures, which are categorized as failures due to insufficient material strength and underdesign, failures due to stress concentration and material defects, and failures due to material alteration...
Abstract
This article aims to identify and illustrate the types of overload failures, which are categorized as failures due to insufficient material strength and underdesign, failures due to stress concentration and material defects, and failures due to material alteration. It describes the general aspects of fracture modes and mechanisms. The article briefly reviews some mechanistic aspects of ductile and brittle crack propagation, including discussion on mixed-mode cracking. Factors associated with overload failures are discussed, and, where appropriate, preventive steps for reducing the likelihood of overload fractures are included. The article focuses primarily on the contribution of embrittlement to overload failure. The embrittling phenomena are described and differentiated by their causes, effects, and remedial methods, so that failure characteristics can be directly compared during practical failure investigation. The article describes the effects of mechanical loading on a part in service and provides information on laboratory fracture examination.
Image
in Failure Prevention through Life Assessment of Structural Components and Equipment
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 4 Fatigue cracking in an aircraft wing fitting for the F-111 aircraft 94 that crashed in 1969. (a) and (b) Location of the left wing pivot box fitting. The 23 mm (0.91 in.) material defect was not observed during inspection, and a fatigue crack initiated and grew for only approximately 0.38
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Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001132
EISBN: 978-1-62708-214-3
..., an unfailed unit from the same room, and an unfailed unit from another room) and an unused 1991 unit -- were examined. casting revealed no material defects or mechanical damage. Because of several environmental factors, it was suspected that the failed unit was exposed to temperatures much above the normal...
Abstract
A sprinkler head unit that was installed in a smoking lounge of a multi story office building in 1975 failed, causing substantial water damage. There was no fire in the building. A set of four sprinkler heads -- three that had been installed in 1975 (the failed unit, an unfailed unit from the same room, and an unfailed unit from another room) and an unused 1991 unit -- were examined. casting revealed no material defects or mechanical damage. Because of several environmental factors, it was suspected that the failed unit was exposed to temperatures much above the normal office environment. On this basis, it was concluded that creep of the solder alloy was the most probable cause of failure.