Skip Nav Destination
Close Modal
Search Results for
localized heating
Update search
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
NARROW
Format
Topics
Book Series
Date
Availability
1-20 of 423 Search Results for
localized heating
Follow your search
Access your saved searches in your account
Would you like to receive an alert when new items match your search?
1
Sort by
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001246
EISBN: 978-1-62708-224-2
... Abstract Two sections of a galvanized cable 10.5 A 160 GR +NORM M 9533 (round stranded cable of normal type, h + 6, Langslay, right-handed) were examined. One had a 100 mm long blackish-brown tarnished zone obviously caused by localized heating at one end, inside which the hemp core was missing...
Abstract
Two sections of a galvanized cable 10.5 A 160 GR +NORM M 9533 (round stranded cable of normal type, h + 6, Langslay, right-handed) were examined. One had a 100 mm long blackish-brown tarnished zone obviously caused by localized heating at one end, inside which the hemp core was missing, and the other corresponded to the original condition of the cable. The cause of the damage was unknown. About a third of the wires had fractured and the rest had been cut. All were tensile fractures with a relatively high degree of necking. The cause of the localized heating was unknown. It can only be concluded from the investigation that the temperature did not exceed the Ac3 point of the wire material, which should be about 750 deg C, and that the heating lasted a fairly long time.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001478
EISBN: 978-1-62708-220-4
.... They could have conceivably arisen as a result of accidental heating by the flame of the brazing torch. If the temperature had been raised locally to above the lower critical — 730°C the region would harden subsequently due to the rapid cooling which would occur when the flame was removed. The cracks which...
Abstract
The broken end of a shaft from a centrifugal pump had a smooth fracture surface characteristic of failure from fatigue. Failure occurred in the plane of the keyway end and followed a slightly helical path, indicating that combined bending and torsional stresses were responsible. The material was a Cr-Mo-Ni alloy steel of the En 19 type in the hardened and tempered condition and of satisfactory quality. The assembly also included a copper sleeve attached by a circumferential braze behind the plane of fracture. The cracks were examined for the presence of copper, thinking that penetration by molten copper may have played a role, but no evidence was seen. An absence of chromium plating at the region of the heat-affected zone was also observed but could not be explained. Unfortunately, the end portion of the shaft was not available for examination.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001837
EISBN: 978-1-62708-241-9
... were caused primarily by the presence of coarse untempered martensite in the heat affected zone due to localized heating. The localized heating was caused by high welding heat input or low welding speed and resulted in high transformation stresses. These transformation stresses, working in combination...
Abstract
This case study describes the failure analysis of a steel nozzle in which cracking was observed after a circumferential welding process. The nozzle assembly was made from low-carbon CrMoV alloy steel that was subsequently single-pass butt welded using gas tungsten arc welding. Although no cracks were found when the welds were visually inspected, X-ray radiography showed small discontinuous surface cracks adjacent to the weld bead in the heat affected zone. Further investigation, including optical microscopy, microhardness testing, and residual stress measurements, revealed that the cracks were caused primarily by the presence of coarse untempered martensite in the heat affected zone due to localized heating. The localized heating was caused by high welding heat input or low welding speed and resulted in high transformation stresses. These transformation stresses, working in combination with thermal stresses and constraint conditions, resulted in intergranular brittle fracture.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0090639
EISBN: 978-1-62708-227-3
... to the cold-working coining process, and high residual stresses created by welding. Recommendations included the removal of the brittle, carbon-rich transformed martensite layer introduced by flame cutting and the application of a localized stress-relief heat treatment process. X-ray diffraction residual...
Abstract
Cracks initiating from the tip of the cloverleaf pattern in steel cargo tiedown sockets were observed by the builder following installation aboard several cargo vessels in various stages of construction. Testing of finite element models and measurements performed in the field on cargo ships with the cracking problem supported the conclusion that the failure was caused by overload. Additional testing showed that the overload failure and the transition from ductile to brittle fracture were facilitated by a combination of high brittleness due to flame cutting, increased hardness due to the cold-working coining process, and high residual stresses created by welding. Recommendations included the removal of the brittle, carbon-rich transformed martensite layer introduced by flame cutting and the application of a localized stress-relief heat treatment process. X-ray diffraction residual-stress measurements were then performed on heat treated tiedown sockets to verify the effectiveness of the localized heat treatment process applied.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0047586
EISBN: 978-1-62708-236-5
... typical of exposure to air when very hot. Several additional subsurface cracks, typical of hot tears, were observed in and near the weld. There had been too much local heat input in making the repair weld. The result was localized thermal contraction and hot tearing. The cracking of the repair weld...
Abstract
A fuel-nozzle-support assembly showed transverse indications after fluorescent liquid-penetrant inspection of a repair-welded area at a fillet on the front side of the support neck adjacent to the mounting flange. Visual examination disclosed an irregular crack. The crack through the neck was sectioned; examination showed that the crack had extended through the repair weld. The crack had followed an intergranular path. The crack was opened, and binocular-microscope examination of the fracture surface showed that the surface contained dendrites with discolored oxide films that were typical of exposure to air when very hot. Several additional subsurface cracks, typical of hot tears, were observed in and near the weld. There had been too much local heat input in making the repair weld. The result was localized thermal contraction and hot tearing. The cracking of the repair weld was attributed to unfavorable welding practice that accentuated thermal contraction stresses and caused hot tearing. Recommendations involved use of a small-diameter welding electrode, a lower heat input, and deposition in shallow layers that could be effectively peened between passes to minimize internal stress.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001624
EISBN: 978-1-62708-218-1
.... The findings suggested salt or salt water had leaked into the sensor and caused localized corrosion to the wire, possibly at an area where preexisting damage was present in the coating. Separation occurred in the wire when the current density at the reduced cross section caused excessive localized heating...
Abstract
An electronic sensor coil failed continuity testing, indicating that a break was present in the polymer-coated wire. An area of the wire showed a green discoloration and the break in the wire was located in this same region. The discoloration was suspected to be an indicator of what caused the failure. SEM/EDS and FTIR results showed the break in the coil wire was associated with corrosion. The corrosion debris contained relatively high levels of sodium and chlorine, which were likely in the form of salt. Some salt deposits were noted also in other areas along the wire surface. The findings suggested salt or salt water had leaked into the sensor and caused localized corrosion to the wire, possibly at an area where preexisting damage was present in the coating. Separation occurred in the wire when the current density at the reduced cross section caused excessive localized heating, which led to melting of the wire.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001171
EISBN: 978-1-62708-219-8
... the precipitation (including reduction of carbon content, appropriate heat treatment, cold work of steel, reduction of austenitic grain size and stabilizing elements) were described. The presence of microcracks due to highly localized heat concentrations with consequent thermal expansion and considerable shrinkages...
Abstract
The defects observed along weldings of stainless steel pipelines employed in marine environments were evidenced by metallographic and electrochemical examination. A compilation of cases on the effect of defective weldings, in addition to improper choice of stainless steel for water pipelines, lead to the conclusion that intercrystalline corrosion in steels involved precipitation of a surplus phase at grain boundaries. Intercrystalline corrosion in austenitic stainless steels due to precipitation of chromium carbides during conditions generated due to welding and ways to avoid the precipitation (including reduction of carbon content, appropriate heat treatment, cold work of steel, reduction of austenitic grain size and stabilizing elements) were described. The presence of microcracks due to highly localized heat concentrations with consequent thermal expansion and considerable shrinkages during cooling was investigated. The specimens were taken from various sources including transverse and longitudinal welding seam, sensitized areas and it was concluded appropriate material selection with respect to medium could control some corrosion processes.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001483
EISBN: 978-1-62708-225-9
... in between the bolt and the hole in the strip. The bolt end adjacent to the fracture had been subjected to intense local heating. The extent of the grain-growth indicating that the temperature had been in the region of 1200 deg C (2192 deg F). When the temperature reached the melting-point of copper, 1083...
Abstract
A steel bolt had been used to join the copper connecting strips between the poles of a 10-pole, series-connected, rotating field rotor of a synchronous motor. The exciting current was 155 amps. Failure of the bolt resulted in severe damage to the stator windings by the loosened ends of the strips. The bolt had fractured near the head, a location which probably coincided with the junction of the strips. A portion of the fracture surface was covered with copper that had been deposited in the molten state, while some was also present along the shank of the bolt, having apparently run in between the bolt and the hole in the strip. The bolt end adjacent to the fracture had been subjected to intense local heating. The extent of the grain-growth indicating that the temperature had been in the region of 1200 deg C (2192 deg F). When the temperature reached the melting-point of copper, 1083 deg C (1981 deg F), molten metal came into contact with the bolt, into which it penetrated along the grain boundaries, culminating in rupture.
Image
Published: 15 January 2021
Fig. 3 Electrical discharge and arcing through the bearing have produced blue-black oxide, indicating the local heating. The ball bearings also show local hot spots.
More
Image
Published: 01 January 2002
Fig. 3 Electrical discharge and arcing through the bearing have produced blue-black oxide, indicating the local heating. The ball bearings also show local hot spots.
More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001646
EISBN: 978-1-62708-219-8
... reduction in deformation. Inadequate lubrication or breakdown of the lubrication film during wire drawing results in greater friction due to metal-to-metal contact between the steel wire and the tungsten carbide die. This may lead to local heating of the wire surface and its abrupt cooling...
Abstract
Locked coil wire ropes, by virtue of their unique design and construction, have specialized applications in aerial ropeways, mine hoist installations, suspension bridge cables, and so forth. In such specialty ropes, the outer layer is constructed of Z-profile wires that provide not only effective interlocking but also a continuous working surface for withstanding in-service wear. The compact construction and fill-factor of locked coil wire ropes make them relatively impervious to the ingress of moisture and render them less vulnerable to corrosion. However, such ropes are comparatively more rigid than conventional wire ropes with fiber cores and therefore are more susceptible to the adverse effects of bending stresses. The reasons for premature in-service wire rope failures are rather complex but frequently may be attributed to inappropriate wire quality and/or abusive operating environment. In either case, a systematic investigation to diagnose precisely the genesis of failure is desirable. This article provides a microstructural insight into the causes of wire breakages on the outer layer of a 40 mm diam locked coil wire rope during service. The study reveals that the breakages of Z-profile wires on the outer rope layer were abrasion induced and accentuated by arrays of fine transverse cracks that developed on a surface martensite layer.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001295
EISBN: 978-1-62708-215-0
.... A different feature was observed on this wire—a pronounced blue color on the wire surface, extending several millimeters from the point of fracture. This is typical of a localized heating effect (e.g., wire being struck by lightning). Failure Type 3 Failure type 3 showed a shear-type fracture, oblique...
Abstract
Over a period of 2 or 3 years, 40 to 50 premature failures of drawn high-tensile, pearlitic high-carbon (0.8 wt% C) steel wires used as cables for towing targets behind aircraft occurred. Six service failures were examined in detail. Four types of failure characteristics were noted. A close examination of wire that had been flown several times without failure was also made, and dynamic tests were conducted to investigate the fracture characteristics of wire subjected to dynamic loading. It was concluded that dynamic shock loading transmitted by the target during unsteady flight conditions was the major cause of failure. Recommendations emphasized the need for a suitable shock absorber to be fitted at the constant-tensioning device of the winch system.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001850
EISBN: 978-1-62708-241-9
... heat load and hot abrasion due to velocity of hot blast, coal injection and oxygen enrichment. Several possible reasons for the cracking of refractory lining at this region have been discussed as follows. Localized Heating Localized heating of the refractory lining may be an outcome...
Abstract
After about a year of uninterrupted service, one of the blow pipes on a blast furnace developed a bulge measuring 300 x 150 x 12 mm. The conical shaped section was removed from the furnace and examined to determine why it failed. The investigation consisted of visual inspection, chemical analysis, microstructural characterization, and mechanical property testing. The pipe was made from nonresulfurized carbon steel as specified and was lined with an alumina refractory. Visual inspection revealed cracks in the refractory lining, which corresponded with the location of the bulge. Microstructural and EDS analysis yielded evidence of overheating, revealing voids, scale, grain boundary oxidation, decarburization, and grain coarsening on the inner surface of the pipe, which also suggest the initiation of creep. Based on the information gathered during the investigation, the blow pipe was exposed to high temperatures when the liner cracked and subsequently bulged out due to creep.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001598
EISBN: 978-1-62708-232-7
... cumulative service at elevated temperature. A recommendation was made to implement a support for the conical section of the CIM and to increase the wall thickness of the drain tube. Thus, the possibility of drain tube misalignment in the induction coils and localized over heating will be minimized...
Abstract
The metallurgical condition of a cylindrical induction melter (CIM) vessel was evaluated after approximately 375 h of operation over a two-year span at temperatures between 1400 to 1500 deg C. Wall thinning and significant grain growth was observed in the lower portion of the conical section and the drain tube. No through-wall penetrations were found in the cylindrical and conical sections of the CIM vessel and only one leak site was identified in the drain tube. Failure of the drain tube was associated with localized overheating and creep. The observed degradation resulted from cumulative service at elevated temperature. A recommendation was made to implement a support for the conical section of the CIM and to increase the wall thickness of the drain tube. Thus, the possibility of drain tube misalignment in the induction coils and localized over heating will be minimized. In addition, the use of grain stabilized Pt/Rh alloy should be evaluated as a method to prevent grain growth.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001849
EISBN: 978-1-62708-241-9
... is shown in Fig. 7 . In addition, plastic flow apparent on the surface and subsurface layer clearly indicates the presence of severe sliding conditions probably accompanied by localized heating (high shear stresses, frictional, or adiabatic heat generation), see Fig. 8 . Fig. 7 Optical micrograph...
Abstract
Spalled fragments from the work rolls of a steel bar straightening machine were received for failure analysis. Visual inspection coupled with optical and scanning electron microscopy were used as the principal analytical techniques for the investigation. Fractographic analysis revealed the presence of a characteristic fatigue crack propagation pattern (beach marks) and radial chevron marks indicating the occurrence of final overload through a brittle intergranular fracture. The collected evidence suggests that surface-initiated cracks propagated by fatigue led to spalling, resulting in severe work roll damage as well as machine downtime and increased maintenance costs.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001011
EISBN: 978-1-62708-229-7
... is recorded at the outlet steam collector, being an average from the mixing of steam from all superheater coils, no records of this local heating existed. Metallographic sections showed the grooves to consist of cracks containing oxide, one having progressed through the wall to cause rupture. The initial...
Abstract
After some 87,000 h of operation, failure took place in the bend of a steam pipe connecting a coil of the third superheater of a steam generator to the outlet steam collector. The unit operated at 538 deg C and 135 kPa, producing 400 t/h of steam. The 2.25Cr-1Mo steel pipe in which failure took place was 50.8 mm in diam with a nominal wall thickness of 8 mm. It connected to the AISI 321 superheater tube by means of a butt weld and was one of 46 such parallel connecting tubes. The Cr-Mo tubing was situated outside the heat transfer zone of the superheater. The overall sequence of failure involved overheating of the Cr-Mo outlet tubes, heavy oxidation, oxide cracking on thermal cycling, thermal fatigue cracking plus oxidation, creep-controlled crack growth, and rapid plastic deformation and rupture. This failure was indicative of excess temperature of the steam coming from the heat transfer zone of the coil. It showed that many damage mechanisms may combine in the transition from fracture initiation to final failure. The presence of grain boundary sliding as an indication of creep damage was useful in the characterization of the stress level as high and showed that the process of creep was not operative throughout the life of the equipment.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001768
EISBN: 978-1-62708-241-9
... visual characteristics and is usually a hard martensitic region that develops as a consequence of localized heating and rapid cooling of the steel components. In the present case also there must be some leakage of current from power conductors through insulator string causing localized heating...
Abstract
A steel splice plate in a power transmission line tower cracked while in service. Metallographic analysis indicated the presence of a white hard martensite layer near the crack, which occurred in the heel of the plate. Mechanical property tests revealed localized hardening in the area of the crack, supporting the metallurgical findings. A substantial deterioration of the Charpy impact toughness of the material in the heel region was also observed which is believed to have caused the initiation and propagation of the cracks leading to the failure.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001823
EISBN: 978-1-62708-241-9
... appearance, and contained dendritic grains, which are consistent with resolidified molten metal. Narrow heat-affected zones (HAZs) were present adjacent to the feature surfaces. The width of the zone indicates localized heating. Eutectic iron was likely present at the feature, which would suggest...
Abstract
A section of pipe in a hydrocarbon pipeline was found to be leaking. The pipeline was installed several decades earlier and was protected by an external coating of extruded polyethylene and a cathodic protection system. The failed pipe section was made from API 5L X46 line pipe steel, approximately 22 cm (8.7 in.) OD x 0.5 cm (0.2 in.) wall thickness, which was electric resistance welded along the longitudinal seam. The pressure at the time and location of the failure was 2760 kPa, which corresponds to 20% of the specified minimum yield strength. The cause of failure (based on visual inspection, magnetic particle inspection, stereoscopic analysis, scanning electron microscopy, tensile and hardness testing, and chemical analysis) was attributed to damage resulting from a lightning strike.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001105
EISBN: 978-1-62708-214-3
... The bellows failed by SCC caused by the presence of chlorine and sulfur. Stress-corrosion cracking allowed escaping hot gases to impinge on the threaded 4140 alloy steel tie rods. The insulation retained the heat, thus locally heating the tie rods to approximately 595 °C (1100 °F). Heating of the rods...
Abstract
A tie rod, nut, and bellows from a failed 610 mm (24 in.) diam tied universal expansion joint that carried tail gases consisting of N 2 + O 2 with slight traces of nitrogen oxides and water were examined. The materials were SA 193-B7 (AISI 4140), SA 194–214, and Incoloy 800H, respectively. Visual examination of the bellows revealed cracks in heavily cold-worked areas (both inside and outside) and considerable corrosion. SEM analysis showed a classical intergranular failure pattern with microcracking. The threaded tie rod microstructure contained spheroidized carbide that was more pronounced at the tie rod end of the failure. Energy-dispersive X-ray analysis of fracture surfaces from the bellows showed the presence of chlorine and sulfur. Failure of the bellows was attributed to stress-corrosion cracking, with chlorine and sulfur being the corroding agents. The rod damage was the result of failure of the bellows, which allowed escaping hot gases to impinge on the tie rods and heat them to approximately 595 deg C (1100 deg F). It was recommended that the insulation be analyzed to determine the origin of the chlorine and sulfur and that it be replaced if necessary.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001616
EISBN: 978-1-62708-229-7
... for local pitting bursting. Nonuniform heat transfer in Stage 3 operation accelerated the selective corrosion of front-end tubes. The relatively high heat transfer in this stage resulted in condensation of some corrosive gases and consequent corrosion. Continuous operation of the plant with some precautions...
Abstract
Severe pitting corrosion of a carbon steel tube was observed in the air preheater of a power plant, which runs on rice straw firing. Approximately 1450 tubes were removed from Stage 3 of the preheater (air inlet and flue gas outlet) due to corrosion and local bursting. Samples from Stage 2 (where corrosion was low) and Stage 3 (severe corrosion) were taken and subjected to visual inspection, SEM, x-ray diffraction, microhardness measurement, and chemical and microstructural analysis. It was determined that extended non-operation of the plant resulted in the settlement of corrosive species on the tubes in Stage 3. The complete failure of the tube occurred due to diffusion of these elements into the base metal and precipitation of potassium and chlorine compounds along the grain boundaries, with subsequent dislodging of grains. The nonmetallic inclusions acted as nucleating sites for local pitting bursting. Nonuniform heat transfer in Stage 3 operation accelerated the selective corrosion of front-end tubes. The relatively high heat transfer in this stage resulted in condensation of some corrosive gases and consequent corrosion. Continuous operation of the plant with some precautions during assembly of the tubes reduced the corrosion problem.
1