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lamination

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Published: 01 June 2019
Fig. 6 Shallow angle, planar flaw (lamination) in the off-cut of the Bruce 2 N06 pressure tube. [R and T are the radial and transverse directions respectively.] More
Image
Published: 01 June 2019
Fig. 8 Detail of tip of lamination in the rolled joint region of the Bruce 2 N06 pressure tube showing: (a) reorientation of hydrides, and (b) oxide wedging. More
Image
Published: 01 June 2019
Fig. 9 Detail of the tip of the lamination near the furthest inboard axial extent into the Bruce 2 N06 pressure tube, showing: (a) flap, and (b) discontinuous pores (arrows) similar to those seen in the off-cut. More
Image
Published: 01 June 2019
Fig. 4 Defect on as-received extrusion. Note appearance of lamination. ×100. More
Image
Published: 01 December 1993
Fig. 7 Photomacrograph of fracture origin and midwall lamination cracks More
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001274
EISBN: 978-1-62708-215-0
... Abstract A laminated-paper microwave food tray collapsed with hot food in it. Microscopic examination of the failed tray revealed no structural or material defects. Five additional trays of like construction were also tested to determine the conditions necessary to simulate the permanent...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0045926
EISBN: 978-1-62708-235-8
... Abstract A batch of bimetal foil/epoxy laminates was rejected because of poor peel strength. The laminates were manufactured by sintering a nickel/phosphorus powder layer to a copper foil, cleaning, then chromate conversion coating the nickel-phosphorus surface, and laminating the nickel...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001515
EISBN: 978-1-62708-229-7
... Abstract This paper describes the analysis of the failure of a Zr-2.5Nb pressure tube in a CANDU reactor. The failure sequence was established as: (1) the existence of an undetected manufacturing flaw in the form of a lamination, (2) in-service development of the flaw by oxidation...
Image
Published: 01 June 2019
Fig. 2 Results of XPS analyses of bimetal foil laminates. (a) XPS spectra of the underside of the nickel-phosphorus layer in the low peel strength sample. Note the height of the sodium peak at 1069 eV as compared with (b), which shows the XPS spectra from a high peel strength sample. More
Image
Published: 01 June 2019
Fig. 1 Ultrasonic c-scan of the laminate section submitted for analysis. Area A is the “defective” area and area B is the “good” area. (Original magnification 1×) More
Image
Published: 01 June 2019
Fig. 21 Laminated structure of magnetite scale × 50 More
Image
Published: 01 January 2002
Fig. 25 Porosity in GMAW core-plated silicon steel laminations. 100× More
Image
Published: 01 December 1993
Fig. 11 Fracture surface of diffuser cone near intake end, showing laminations and microcracks in Corten steel. More
Image
Published: 01 December 1993
Fig. 6 Photomacrograph of shell midwall laminations and fracture site in Fragment 17 More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001445
EISBN: 978-1-62708-227-3
... were basically laminations of a similar form to those which resulted in the failure of the portion of pipe. Defects Magnetic testing Steam pipes Plate steel Metalworking-related failures The presence of internal laminations constitutes an objectionable feature in the plates of vessels...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003507
EISBN: 978-1-62708-180-1
... discusses the types of imperfections that can be traced to the original ingot product. These include chemical segregation; ingot pipe, porosity, and centerline shrinkage; high hydrogen content; nonmetallic inclusions; unmelted electrodes and shelf; and cracks, laminations, seams, pits, blisters, and scabs...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001184
EISBN: 978-1-62708-235-8
... and was adapted to the latter by diffusion only at the periphery of the inclusion. In another section of a hardened piece of the same chromium steel, the steel in this case had a structure of martensite with hypereutectic carbide, while the inclusions consisted of a very fine laminated eutectoid of the lower...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048498
EISBN: 978-1-62708-234-1
... of the compression-loading skin panel were revealed by nondestructive visual examination. A band of de-lamination between the areas of through-thickness skin fracture at the front and rear spar was revealed. A map of the local directions of crack propagation over the fracture surface was generated by the orientation...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001347
EISBN: 978-1-62708-215-0
...-128 Grade B. As a result of the explosive failure of the tank car, fragments were ejected from the central region of the car between the support trucks from ground zero to a maximum of approximately 195 m (640 ft). The mode of failure was a brittle fracture originating at a preexisting lamination...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001491
EISBN: 978-1-62708-217-4
... cracking occurred adjacent to the bond line in the convergent/throat section, it may be said that the EPON 934 bond is stronger than the interlaminar strength of the MX-2646 silica phenolic laminate. Post-test examination of Nozzle Liner Assembly S/N 018 revealed two circumferential cracks...