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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047297
EISBN: 978-1-62708-235-8
... Abstract Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings...
Abstract
Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings was suspected. Metallurgical examination on two representative castings supported the conclusions that the cracks in these gray iron door closers that were present either before or during the heat treatment were attributed to a substandard microstructure of the wrong type of graphite combined with excessive ferrite. This anomalous structure is caused by shortcomings in the foundry practice of chemical composition, solidification, and inoculation control. Judging from the microstructure, the strength of the material was lower than desired for class 30 gray iron, and the suspected heat treatment further reduced the strength. Recommendations included that the chemistry and inoculation should be controlled to produce type A graphite structure. The chemistry control should aim for a carbon equivalent close to 4.3% to achieve adequate fluidity for thin sections and to alleviate gas defects.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001197
EISBN: 978-1-62708-235-8
... Abstract The front wall of a cast iron crankcase cracked at the transition from the comparatively minor wall thickness to the thick bosses for the drilling of the bolt holes. Metallographic examination showed the case was aggravated by the fact that the casting had a ferritic basic structure...
Abstract
The front wall of a cast iron crankcase cracked at the transition from the comparatively minor wall thickness to the thick bosses for the drilling of the bolt holes. Metallographic examination showed the case was aggravated by the fact that the casting had a ferritic basic structure and the graphite in part showed a granular formation, so that strength of the material was low. In a second crankcase with the same crack formation the structure in the thick-wailed part was better. But it also showed granular graphite in the ferritic matrix in the thin-walled part between the dendrites of the primary solid solution precipitated in the residual melt. A third crankcase had fractures in two places, first at the frontal end wall and second at the thinnest point between two bore holes. In all three cases casting stresses caused by unfavorable construction and rapid cooling were responsible for the crack formation. A fourth crankcase had cracked in the bore-hole of the frontal face. In this case the cause of the fracture was the low strength of a region that was caused by a bad microstructure further weakened by the bore hole.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001198
EISBN: 978-1-62708-221-1
... Abstract Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps...
Abstract
Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps consisted of graphite in pearlitic-ferritic matrix. Casting stresses did not play a decisive role because of the simple shape of the pieces that were without substantial cross sectional variations. Two factors exerted an unfavorable effect in addition to comparatively low strength. First, the operating stress was raised locally by the sharp-edged groove, and second, the fracture resistance of the cast iron was lowered at this critical point by the existence of a ferritic bright border. To avoid such damage in the future it was recommended to observe one or more of the following precautions: 1) Eliminate the grooves; 2) Remove the ferritic bright border; 3) Avoid undercooling in the mold and therefore the formation of granular graphite; 4) Inoculate with finely powdered ferrosilicon into the melt for the same purpose; and, 5) Anneal at lower temperature or eliminate subsequent treatment in consideration of the uncomplicated shape of the castings.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001200
EISBN: 978-1-62708-221-1
... Abstract During the operation of tractors with cantilevered body, the lateral wall of the hypoeutectic cast iron cylinder blocks cracked repeatedly. Three of the blocks were examined. The grain structure of the thick-walled part consisted of uniformly distributed graphite of medium flake size...
Abstract
During the operation of tractors with cantilevered body, the lateral wall of the hypoeutectic cast iron cylinder blocks cracked repeatedly. Three of the blocks were examined. The grain structure of the thick-walled part consisted of uniformly distributed graphite of medium flake size in a basic mass of pearlite with little ferrite. But the thin-walled part showed a structure of dendrites of precipitated primary solid solution grains with pearlitic-ferritic structure and a residual liquid phase with granular graphite in the ferritic matrix. The structure was formed by undercooling of the residual melt. In this case, it was promoted by fast cooling of the thin wall and had comparatively low strength. The fracture formation in the cylinder blocks was ascribed primarily to casting stresses. They could be alleviated by better filleting of the transition cross sections. The fracture was promoted by the formation of undercooled microstructure of low strength in the thin-walled part. Similar damage appeared in a cylinder head, in which case, the cracks were promoted by a supercooled structure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0090965
EISBN: 978-1-62708-221-1
... Abstract The upper frame from a large cone crusher failed in severe service after an unspecified service duration. The ductile iron casting was identified as grade 80-55-06, signifying minimum properties of 552 MPa (80 ksi) tensile strength, 379 MPa (55 ksi) yield strength, and 6% elongation...
Abstract
The upper frame from a large cone crusher failed in severe service after an unspecified service duration. The ductile iron casting was identified as grade 80-55-06, signifying minimum properties of 552 MPa (80 ksi) tensile strength, 379 MPa (55 ksi) yield strength, and 6% elongation. Investigation (visual inspection, chemical analysis, unetched 30x images, and 2% nital etched 30x images) was difficult because the fracture surface of the frame section was obliterated by postfracture corrosion. Repeated attempts at cleaning using progressively stronger chemicals revealed that no telltale fracture morphology remained. However, the investigation supported the conclusion that the crusher frame failed via brittle overload fracture, likely due to excessive service stresses and substandard mechanical properties. Recommendations included additional quality-control measures to provide better spheroidal graphite morphology at the frame surface.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0047234
EISBN: 978-1-62708-233-4
... Abstract Several deburring drums that fractured were filled with abrasive, water, and small parts, such as roller bearing rollers, and rotated on their axis at 36 rpm. Cracks were discovered very early in the service lives of these high-chromium white iron cast structures. All of the fractures...
Abstract
Several deburring drums that fractured were filled with abrasive, water, and small parts, such as roller bearing rollers, and rotated on their axis at 36 rpm. Cracks were discovered very early in the service lives of these high-chromium white iron cast structures. All of the fractures were through bolt holes in the mounting flange. The holes had a sharp edge and exhibited uneven wear on the inside diameter. In operation, the mounting bolts were frequently found to be loose and in at least one case broken off. A 25x scanning electron microscopy (SEM) fractograph from near this fracture-initiation area showed fatigue striations. No casting or metallurgical structural defects were found that could explain the failures. This evidence supports the conclusion that cracking was a result of the stress-concentration site at the bolt holes where a fatigue-initiated fracture occurred. Recommendations included that the radii be increased at the sharp corners and that lock-wiring be used to secure against bolt loosening.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001226
EISBN: 978-1-62708-234-1
..., 2.49Si, 0.51Mn, 0.485P, and 0.112S. The iron was thus distinctly hypereutectic. The galling of the pump parts therefore was favored by an unsuitable structure caused by improper composition and fast cooling. Distortion by casting stresses may have been contributory or may have played the principal part...
Abstract
A slide and the two guideways of a pump had to be disassembled already during run-in time after approximately 20 h because they had galled completely, before the rated speed of 800 rpm was reached. Chemical analysis of the slide showed the following composition: 3.60C, 3.22Graphite, 2.49Si, 0.51Mn, 0.485P, and 0.112S. The iron was thus distinctly hypereutectic. The galling of the pump parts therefore was favored by an unsuitable structure caused by improper composition and fast cooling. Distortion by casting stresses may have been contributory or may have played the principal part. In order to prevent a repetition, the use of hypoeutectic or eutectic iron, slower cooling of the casting, inoculation of the melt with finely powdered ferrosilicon, and possibly rounding-off the edges or machining of the surfaces are recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0048804
EISBN: 978-1-62708-230-3
... Abstract Several cases of failures in gray cast iron paper machine dryer rolls were evaluated. The rolls were found have ground outer cylindrical surfaces on which the paper web is dried. They were found to rotate about their longitudinal axes at speeds from 50 to 250 rpm while containing...
Abstract
Several cases of failures in gray cast iron paper machine dryer rolls were evaluated. The rolls were found have ground outer cylindrical surfaces on which the paper web is dried. They were found to rotate about their longitudinal axes at speeds from 50 to 250 rpm while containing saturated steam from 35 to 380 kPa. Failures were found to occur in the shell body, in a head near a hand hole or a manhole opening, or in a head near the journal-to-head interface. A cleavage fracture was revealed by scanning electron microscopy regardless of the driving stress for failure. Fracture surface were found to exhibit chevron marks typical of fatigue or raised points or tears pointing in the direction of the probable origin of failure. The characteristics of the thinwall cast iron structures like the variation in composition due to pouring from multiple ladles, variation in solidification rates, and variation in tensile strength to be noted during inspection were described.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001307
EISBN: 978-1-62708-215-0
... Abstract The right front spring hanger on a dual rear axle of the tractor of a tractor-trailer combination failed, causing the vehicle to roll-over. The hanger was made from malleable cast iron that had been heat treated to produce a decarburized surface layer and a pearlitic transition layer...
Abstract
The right front spring hanger on a dual rear axle of the tractor of a tractor-trailer combination failed, causing the vehicle to roll-over. The hanger was made from malleable cast iron that had been heat treated to produce a decarburized surface layer and a pearlitic transition layer. It had been repair welded after breaking into two pieces longitudinally in a prior incident, using cast iron as weld metal. The repair weld bead on both surfaces missed the fracture over 15 to 20% of their lengths. The incomplete repair weld and brittleness of the weld metal and heat-affected zones led to the failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
... Abstract A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall...
Abstract
A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall perforations and cracking along its axis. The perforations and the crack were at the 6 o'clock position. Investigation (visual inspection, radiography, unetched macrographs, and tensile testing) supported the conclusion that the failure occurred as result of years of exposure to ground water in the soil resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron or coated and lined steel pipe, generally not susceptible to graphitic corrosion, were suggested as suitable replacement materials, and cathodic protection was also considered as a possibility.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0089617
EISBN: 978-1-62708-232-7
... Abstract A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten...
Abstract
A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten metal, flowing through a trough, was poured into the mold beginning at the bell end and ending with the spigot end being poured last. After the pipe had cooled, it was pulled out from the bell end of the mold, and the procedure was repeated. Investigation supported the conclusion that failure of the mold surface was the result of localized overheating caused by splashing of molten metal on the bore surface near the spigot end. In addition, the mold-wash compound (a bentonite mixture) near the spigot end was too thin to provide the proper degree of insulation and to prevent molten metal from sticking to the bore surface. Recommendations included reducing the pouring temperatures of the molten metal and spraying a thicker insulating coating onto the mold surface.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001071
EISBN: 978-1-62708-214-3
... Abstract A gray cast iron (ASTM 247 type A) gate valve in an oleum and sulfuric acid piping loop at a chemical process plant fractured catastrophically after approximately 10 years of service. The valve was a 150 mm (6 in.) bolted flange type rated to conform to ANSI B16.1 for service at 1034...
Abstract
A gray cast iron (ASTM 247 type A) gate valve in an oleum and sulfuric acid piping loop at a chemical process plant fractured catastrophically after approximately 10 years of service. The valve was a 150 mm (6 in.) bolted flange type rated to conform to ANSI B16.1 for service at 1034 kPa (150 psi) and 120 deg C (250 deg F) maximum in 93 to 99% sulfuric acid. The fracture originated at stress-corrosion cracks that occurred in a high-stress transition region at the valve body-to-flange juncture. The mechanical properties of the failed valve were below those of the manufacturer's cited specification, and the wall thickness through which the fracture occurred exceeded the minimum 9.5 mm (38 in.) thickness cited by the manufacturer The valve flange had been unbolted and rebolted to a maintenanced piping coil immediately prior to failure. It was recommended that the flange-to-valve body juncture be redesigned to reduce stress levels. A method of maintenance and inspection in concert with a criterion for life prediction for this and other valves and components in the system was also recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0047263
EISBN: 978-1-62708-218-1
... with the exhaust-gas flow chamber. No recommendations were made. Castings Cylinder heads Porosity Shrinkage Gray iron Casting-related failures An engine cylinder head failed after operating just 3.2 km (2 miles) because of coolant leakage through the exhaust port. Investigation The left-bank...
Abstract
An engine cylinder head failed after operating just 3.2 km (2 mi) because of coolant leakage through the exhaust port. Visual examination of the exhaust ports revealed a casting defect on the No. 7 exhaust-port wall. A 0.9x examination of an unpolished, unetched longitudinal section through the defect indicated shrinkage porosity. This defect was found to interconnect the water jacket and the exhaust gas flow chamber. No cracks were found by magnetic-particle inspection. The gray iron cylinder head had a hardness of 229 HRB on the surface of the bottom deck. The microstructure consisted of type A size 4 flake graphite in a matrix of pearlite with small amounts of ferrite. this evidence supported the conclusion that the cylinder-head failure resulted from the presence of a casting defect (shrinkage) on the No. 7 cylinder exhaust-port wall interconnecting the water jacket with the exhaust-gas flow chamber. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0089567
EISBN: 978-1-62708-230-3
... Abstract A paper drier head manufactured from gray cast iron was removed from service as a result of NDE detection of crack-like surface discontinuities. This component was subjected to internal steam pressure to provide heat energy for drying. Investigation (visual inspection, chemical...
Abstract
A paper drier head manufactured from gray cast iron was removed from service as a result of NDE detection of crack-like surface discontinuities. This component was subjected to internal steam pressure to provide heat energy for drying. Investigation (visual inspection, chemical analysis, mechanical testing, as-polished 54x magnification, etched with nital 33x/54x/215x/230x magnification) supported the conclusions that the NDE indications were the consequence of a cold-shut condition in the casting. The cold shut served as a stress-concentration site and was therefore a potential source of crack initiation. The combination of low material strength and a casting defect was a potential source of unexpected fracture during service, because the component was under pressure from steam. Recommendations included removing other dryer heads exhibiting similar discontinuities and/or material quality from service.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006831
EISBN: 978-1-62708-329-4
... the intended function is decreased. The article addresses factors that may cause failures in castings for each metal type, starting with gray iron and progressing to ductile iron, steel, aluminum, and copper-base alloys. It describes the general root causes of failure attributed to the casting material...
Abstract
The information provided in this article is intended for those individuals who want to determine why a casting component failed to perform its intended purpose. It is also intended to provide insights for potential casting applications so that the likelihood of failure to perform the intended function is decreased. The article addresses factors that may cause failures in castings for each metal type, starting with gray iron and progressing to ductile iron, steel, aluminum, and copper-base alloys. It describes the general root causes of failure attributed to the casting material, production method, and/or design. The article also addresses conditions related to the casting process but not specific to any metal group, including misruns, pour shorts, broken cores, and foundry expertise. The discussion in each casting metal group includes factors concerning defects that can occur specific to the metal group and progress from melting to solidification, casting processing, and finally how the removal of the mold material can affect performance.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001375
EISBN: 978-1-62708-215-0
... Abstract Three sprinkler system dry pipe valve castings (class 30 gray iron), two that had failed in service and one that had been rejected during machining because of porosity, were submitted for examination. The two failures consisted of cracks in a seating face. All three were from the same...
Abstract
Three sprinkler system dry pipe valve castings (class 30 gray iron), two that had failed in service and one that had been rejected during machining because of porosity, were submitted for examination. The two failures consisted of cracks in a seating face. All three were from the same heat. Visual examination showed that the casting had cracked through a thin area in the casting sidewall. Evidence of a sharply machined corner at the fracture site was also discovered. Tensile testing and metallographic analysis revealed no metallurgical cause for the failure. It was recommended that the manufacturer work with the foundry to evaluate the criticality of core placement and to eliminate the undesired thin section.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0089526
EISBN: 978-1-62708-218-1
.... Controlled pouring temperatures, improved design and use of chills were recommended to avoid the casting defects. Casting defects Cracking (fracturing) Cylinder heads Microporosity Shrinkage Gray iron Casting-related failures A cracked cylinder head was removed from an engine after...
Abstract
A gray iron cylinder head cracked after approximately 16,000 km of service. The head was cracked on the rocker arm pan rail next to the No. 3 intake port and extended into the water jacket on the rocker-arm side of the head. Microporosity was revealed in the crack in the sections taken from the water jacket next to the plug and the area next to the No. 3 intake port. A wave of microporosity travels midway between the inner and outer surfaces of the casting was observed and was concluded to have caused the cracking. The reasons and remedies for shrinkage porosity were discussed. Controlled pouring temperatures, improved design and use of chills were recommended to avoid the casting defects.
Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003508
EISBN: 978-1-62708-180-1
... iron, gray cast iron, malleable irons, ductile iron, low-alloy steel castings, austenitic steels, corrosion-resistant castings, and cast aluminum alloys are the materials discussed. The article describes the general types of discontinuities or imperfections for traditional casting with sand molds...
Abstract
This article focuses on the general root causes of failure attributed to the casting process, casting material, and design with examples. The casting processes discussed include gravity die casting, pressure die casting, semisolid casting, squeeze casting, and centrifugal casting. Cast iron, gray cast iron, malleable irons, ductile iron, low-alloy steel castings, austenitic steels, corrosion-resistant castings, and cast aluminum alloys are the materials discussed. The article describes the general types of discontinuities or imperfections for traditional casting with sand molds. It presents the international classification of common casting defects in a tabular form.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001058
EISBN: 978-1-62708-214-3
... Abstract A white cast iron water-line plug in a fire sprinkler systems split during leak repair. Examination revealed no material flaws, fatigue, or excessive corrosion. The plug head exhibited signs of excessive loads used in attempts to force the plug farther into the pipe. The evidence...
Abstract
A white cast iron water-line plug in a fire sprinkler systems split during leak repair. Examination revealed no material flaws, fatigue, or excessive corrosion. The plug head exhibited signs of excessive loads used in attempts to force the plug farther into the pipe. The evidence obtained indicated that the failure resulted from human error.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089646
EISBN: 978-1-62708-235-8
... Abstract Nodular cast iron crankshafts and their main-bearing inserts were causing premature failures in engines within the first 1600 km (1000 mi) of operation. The failures were indicated by internal noise, operation at low pressure, and total seizing. Concurrent with the incidence of engine...
Abstract
Nodular cast iron crankshafts and their main-bearing inserts were causing premature failures in engines within the first 1600 km (1000 mi) of operation. The failures were indicated by internal noise, operation at low pressure, and total seizing. Concurrent with the incidence of engine field failures was a manufacturing problem: the inability to maintain a similar microfinish on the cope and drag sides of a cast main-bearing journal. Investigation supported the conclusion that the root cause of the failure was carbon flotation due to the crankshafts involved in the failures showing a higher-than-normal carbon content and/or carbon equivalent. Larger and more numerous cope side graphite nodules broke open, causing ferrite caps or burrs. They then became the mechanism of failure by breaking down the oil film and eroding the beating material. A byproduct was heat, which assisted the failure. Recommendations included establishing closer control of chemical composition and foundry casting practices to alleviate the carbon-flotation form of segregation. Additionally, some nonmetallurgical practices in journal-finishing techniques were suggested to ensure optimal surface finish.
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