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gas nitriding

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0092155
EISBN: 978-1-62708-221-1
... and the adjacent splined coupling sleeve. Specifications included that the gear and coupling be made from 4140 steel bar oil quenched and tempered to a hardness of 265 to 290 HB (equivalent to 27 to 31 HRC) and that the finish-machined parts be single-stage gas nitrided to produce a total case depth of 0.5 mm...
Image
Published: 01 January 2002
Fig. 13 Gas-nitrided 4140 steel (27–31 HRC) drive-gear assembly in which gear teeth deformed because of faulty design and low core hardness. Details A and B show deformed areas on drive-gear teeth and mating internal splines. Dimensions given in inches More
Image
Published: 01 June 2019
Fig. 1 Gas-nitrided 4140 steel (27–31 HRC) drive-gear assembly in which gear teeth deformed because of faulty design and low core hardness. Details A and B show deformed areas on drive-gear teeth and mating internal splines. Dimensions given in inches More
Image
Published: 15 January 2021
Fig. 13 Gas-nitrided 4140 steel (27–31 HRC) drive-gear assembly in which gear teeth deformed because of faulty design and low core hardness. Details A and B show deformed areas on drive-gear teeth and mating internal splines. Dimensions given in inches More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001189
EISBN: 978-1-62708-218-1
... at the outer part of the teeth. The nitride layer did not stand up to the high and one-sided compressive stress applied in this case and could not prevent pitting. It could even have accelerated the wear by the incipient break down. Gas nitriding at greater depth under application of a suitable special steel...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003573
EISBN: 978-1-62708-180-1
.... Preheating before austenitizing is often used as a means of minimizing warping of some tool steels and heavy sections because preheating reduces the temperature gradient between the surface and the interior of the part. Induction hardening and nitriding have been used to minimize warping when surface...
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006797
EISBN: 978-1-62708-295-2
... of temperature change are minimized. Preheating before austenitizing is often used as a means of minimizing warping of some tool steels and heavy sections, because preheating reduces the temperature gradient between the surface and the interior of the part. Induction hardening and nitriding have been used...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001676
EISBN: 978-1-62708-229-7
... the interaction with gamma radiation) and to prevent corrosion. A number of failures have occurred over the years because of a loss of the He cover gas in the assembly. This has resulted in either acid attack on the Inconel 600 sheath in a wet environment or gaseous corrosion in a dry environment. In the latter...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001712
EISBN: 978-1-62708-234-1
.... 5 Nitrogen pickup of roll alloys as a function of time in an N 2 atmosphere at 1000 °C. Tabulated results of nitridation study. Samples were exposed to flowing nitrogen gas at 1000 °C. Table 5 Tabulated results of nitridation study. Samples were exposed to flowing nitrogen gas at 1000...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0091362
EISBN: 978-1-62708-220-4
.... The increase in the weld nitrogen level was a direct result of inadequate argon gas shielding of the molten weld puddle. Two areas of inadequate shielding were identified: improper gas flow rate for a 19 mm (0.75 in.) diam gas lens nozzle, and contamination of the manifold gas system. Recommendations included...
Series: ASM Handbook
Volume: 11
Publisher: ASM International
Published: 15 January 2021
DOI: 10.31399/asm.hb.v11.a0006787
EISBN: 978-1-62708-295-2
... Abstract High-temperature corrosion can occur in numerous environments and is affected by various parameters such as temperature, alloy and protective coating compositions, stress, time, and gas composition. This article discusses the primary mechanisms of high-temperature corrosion, namely...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090114
EISBN: 978-1-62708-229-7
... Abstract The first-stage blades in a model 501D5 gas turbine had 16 cooling holes. After 32,000 h of service, the blades exhibited cracking at the cooling holes. The blade material was wrought Udimet 520 alloy, with nominal composition of 57Ni-19Cr-12Co-6Mo-1W-2Al-3Ti-0.05C-0.005B. The cooling...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001748
EISBN: 978-1-62708-225-9
... reoccurrence, specific inspection criteria were issued defining maximum limits for spline wear. A procedure and requirements were specified for installing the coupling and pinion gear at the next overhaul. Gas turbine engines Inspection Pinions Specifications Splines AMS 6470 UNS K24065 (Other...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001761
EISBN: 978-1-62708-241-9
... accurate crankshaft deviation . Diesel Gas Turbine Worldwide 19 ( 3 ), 30 – 32 ( 1987 ). 3. Haddara M.R. , Younis M.A. : Effect of connecting rod obliquity on the torsional vibration of marine diesel engines with variable inertia . Trans. Canadian Soc. Mech. Eng. 10 ( 4 ), 201...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001910
EISBN: 978-1-62708-217-4
... potential during the diffusion portion of a carbide-diffuse cycle, or by prolonged reheating in moist air or other decarburizing gas. 3 A complete decarburized layer consists of ferrite, which transitions to a layer of ferrite and a low-carbon martensite towards the core of the component. The component...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003564
EISBN: 978-1-62708-180-1
... as materials for rolling-contact bearing components show some practical advantages over traditional bearing steels. The properties of ceramics, specifically low density and high stiffness, are of most interest to gas turbine ( Ref 1 ) and machine tool manufacturers ( Ref 2 ). High hardness, low coefficient...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001575
EISBN: 978-1-62708-217-4
...) into an Al alloy casing. Failure of the scavenge pump causes the main shaft bearings to be overlubricated because the oil is no longer drained from those compartments. Flames and smoke from the engine tailpipe (when oil gets to the hot gas flow) is the latest step of the occurred failure. Pump...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0089563
EISBN: 978-1-62708-217-4
... reveals internal voids, such as gas porosity or shrinkage porosity, but does not detect a crack or a cold shut, unless the plane of the imperfection is nearly parallel to the x-ray beam and unless there is a finite opening; a cold shut that has its faces in contact is rarely revealed by radiography...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046252
EISBN: 978-1-62708-229-7
... operating temperatures for this gas-inlet line, intergranular fatigue failure in austenitic stainless steels usually occurs only in the presence of grain-boundary embrittlement. This type of embrittlement is usually the result of nitriding, intergranular oxidation, carbide precipitation, or the formation...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006816
EISBN: 978-1-62708-329-4
... agitation causes temperature gradients within workload and part May not be uniform Rolling on surface is poor guide to agitation Must be measured or modeled Type of quenchant Brine, water, oil, polymer, gas, air Quench rate must be fast enough to achieve desired properties...