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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001289
EISBN: 978-1-62708-215-0
... material was found to conform to specifications ( Table 1 ). The cracked end frame part was also subjected to instrumental gas analysis; the hydrogen gas content was found to be on the order of 22 ppm. Chemical specifications for 38KhA steel Table 1 Chemical specifications for 38KhA steel...
Abstract
The repeated occurrence of random cracks in the fillet radius portion of low-alloy steel (38KhA) end frame forgings following heat treatment was investigated. Microstructural analyses were carried out on both the failed part and disks of the rolled bar from which the part was made. Subsurface cracks were found to be zigzag and discontinuous as well as intergranular in nature. A mixed mode of fracture involving ductile and brittle flat facets was observed. Micropores and rod-shaped manganese sulfide inclusions were also noted. The material had a hydrogen content of 22 ppm, and cracking was attributed to hydrogen embrittlement. Measurement of hydrogen content in the raw material prior to fabrication was recommended. Careful control of acid pickling procedures for descaling of the hot-rolled bars was also deemed necessary.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001556
EISBN: 978-1-62708-218-1
... analysis and the hydrogen gas content was found to be of the order of 18 ppm. Summary and Conclusions A number of Cr-Mo steel piston rods got cracked during chrome plating and some after baking treatment. A detailed investigation was undertaken to pinpoint the source of cracking with the aid...
Abstract
A few Cr-Mo steel piston rods from different production batches were found identically cracked in the eye end near the radius after chrome plating and baking treatment. Two of them cracked in the plating stage itself instantly broke on slight tapping. Cracking initiated from the outer base surface of the forked eye end. The 40 mm diam forged piston rods were subjected to plating after heavy machining on the part without any stress-relieving treatment. Also, time lapses between plating and baking were varied from 3 to 11 h. The brittle cracking along forked eye-end radius portion was attributed to hydrogen embrittlement that occurred during chrome plating.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0065825
EISBN: 978-1-62708-228-0
... to still further enhancements permitting development of weldable higher-strength, larger-diameter pipe but with satisfactory fracture control. Overall, the changes in steel composition were relatively minor, at least on a total weight percent basis. However, these changes, chiefly in residual gas content...
Abstract
A case of continual product refinement stimulated by product failures was described. Brittle fracture of gas transmission line pipe steels occurred demonstrating a poor combination of materials, environment, manufacturing and installation problems, and loads. Initial efforts were concentrated towards decreasing the Charpy ductile-to-brittle transition temperature to avoid brittle fracture. It was subsequently revealed that the absorbed energy on the upper shelf of the Charpy energy-temperature curve was critical for arresting a moving crack. Both fracture initiation and fracture propagation were needed be controlled. It was concluded that improved steel processing procedures, chiefly hot-working temperature and deformation control, were also required to optimize microstructure and properties.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001557
EISBN: 978-1-62708-234-1
... requirement of 5 kg.M/cm 2 ). Based on the above, the cracked end frame was subjected to instrumental gas analysis and hydrogen gas content was found to be of the order of 22 ppm. Summary and Conclusions A number of Cr-Si-Mn alloy machined end frame steel forgings developed random tiny cracks...
Abstract
A number of machined end frame steel forgings made of Cr-Si-Mn alloy showed tiny cracks during magnetic particle inspection after heat treatment. The cracks were mostly confined to base edges and fillet radius. No significant abnormality was observed in chemical composition and microstructure. SEM, optical microscopy, and gas analysis revealed that the subsurface discontinuous cracks at the bore edges and in the fillet radius of the heat-treated end frame component had occurred due to hydrogen embrittlement, and not because of faulty heat treatment. This conclusion was supported by the presence of cracklike indications in machined bore surface of the annealed part.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001166
EISBN: 978-1-62708-228-0
... product from each pipe section were analyzed for carbon, sulfur, and iron and were found to consist mainly of iron sulfide mixed with soot and rust. The damage resulted from a high content of hydrogen sulfide in the gas (6% CO2, 20% CO, 8 to 12% H2, 0.5 to 1.5% CH4, remainder N2). To process the coal...
Abstract
After four months at a temperature of 400 to 5000 C, pipes at a gas generating plant were so heavily eroded they had to be replaced. Three sections of pipe, from different locations, were analyzed to determine whether mechanical wear or corrosion caused the damage. Samples of corrosion product from each pipe section were analyzed for carbon, sulfur, and iron and were found to consist mainly of iron sulfide mixed with soot and rust. The damage resulted from a high content of hydrogen sulfide in the gas (6% CO2, 20% CO, 8 to 12% H2, 0.5 to 1.5% CH4, remainder N2). To process the coal in question, the pipes material should be a heat-resistant steel that contains more chromium and has greater resistance to hydrogen sulfide.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0047392
EISBN: 978-1-62708-221-1
... Abstract A roadarm for a tracked vehicle failed during preproduction vehicle testing. The arm was a weldment of two cored low-alloy steel sand castings specified to ASTM A 148, grade 120–95. A maximum carbon content of 0.32% was specified. The welding procedure called for degreasing and gas...
Abstract
A roadarm for a tracked vehicle failed during preproduction vehicle testing. The arm was a weldment of two cored low-alloy steel sand castings specified to ASTM A 148, grade 120–95. A maximum carbon content of 0.32% was specified. The welding procedure called for degreasing and gas metal arc welding; neither preheating nor postheating was specified. The filler metal was E70S-6 continuous consumable wire with a copper coating to protect it from atmospheric oxidation while on the reel. Analysis of the two castings revealed that the carbon content was higher than specified, ranging from 0.40 to 0.44%. The fracture occurred in the HAZ , where quenching by the surrounding metal had produced a hardness of 55 HRC. Some roadarms of similar carbon content and welded by the same procedure had not failed because they had been tempered during a hot-straightening operation. Brittle fracture of the roadarm was caused by a combination of too high a carbon equivalent in the castings and the lack of preheating and postheating during the welding procedure. A pre-heat and tempering after welding were added to the welding procedure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001233
EISBN: 978-1-62708-232-7
... Abstract High-chromium steel pipes 42.25 x 3.25 mm from a blast furnace gas fired recuperator for the preheating of air were heavily oxidized and perforated in places. It was found that the blast furnace gas had a high sulfur content. Both the carburization and the formation of sulfide proved...
Abstract
High-chromium steel pipes 42.25 x 3.25 mm from a blast furnace gas fired recuperator for the preheating of air were heavily oxidized and perforated in places. It was found that the blast furnace gas had a high sulfur content. Both the carburization and the formation of sulfide proved that in addition, from time to time at least, combustion was incomplete and the operation was carried out in a reducing atmosphere, with the result that oxygen deficiency prevented the formation or maintenance of a protective surface layer on the external surface of the pipes. The sulfur would probably not have damaged the nickel-free steel used here at the given temperatures if it had been present as sulfur dioxide in an oxidizing atmosphere. The damage was therefore caused primarily by an incorrectly conducted combustion process.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001031
EISBN: 978-1-62708-214-3
... Abstract Pinhole defects were found in a main combustion chamber made from NARloy-Z after an unexpectedly short time in service. Analysis indicated that the throat section of the liner had been exposed to very severe environmental conditions of high temperature and high oxygen content, which...
Abstract
Pinhole defects were found in a main combustion chamber made from NARloy-Z after an unexpectedly short time in service. Analysis indicated that the throat section of the liner had been exposed to very severe environmental conditions of high temperature and high oxygen content, which caused ductility loss and grain-boundary separation. The excessive oxygen content in the liner was attributed to diffusion from an oxygen-rich environment that had resulted from nonuniform mixing of propellants. The internal oxygen embrittled the alloy and reduced its thermal conductivity, which resulted in a higher hot-gas wall temperature and associated degradation of mechanical properties.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046926
EISBN: 978-1-62708-232-7
... to have been caused by high-temperature oxidation resulting from the initial heating of the salt pot by the combustion of natural gas. The chromium content of a specimen taken from the bottom of the pot was 10.7% at the inner surface, 11.4% at center, and 16% on the outer surface. It was concluded...
Abstract
Over a period of about one year, three RA 330 alloy salt pots from a single heat-treating plant were submitted to failure analysis. All of the pots, which had 9.5 mm thick walls, were used primarily to contain neutral salts at temperatures from about 815 to 900 deg C (1500 to 1650 deg F). However, some cyaniding was also performed in these pots, which, when not in use, were idled at 760 deg C (1400 deg F). It was reported that sludge was removed from the bottom of the pots once a day. Normal pot life varied from about 6 to 20 months. The pots were removed from the furnace, visually inspected, and rotated 120 deg every three weeks to ensure that no single location was overheated for a prolonged period of time. Analysis (visual inspection, chemical analysis, metallographic examination, and x-ray analysis, 60x micrograph etched with 10% oxalic acid) supported the conclusion that the cause of failure of each of the three salt pots was severe intergranular corrosion accompanied by substantial chromium depletion. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001179
EISBN: 978-1-62708-228-0
... at 530 deg C. The connectors were made of SAE 4140 Cr-Mo steel. The material for the rod pipes was Fe-0.4C-1Mn steel. Structural stresses played a role in the cracking. Iron sulfide formed on the fracture planes and flake-like stress cracks occurred in the steel. The hydrogen sulfide content of the gas...
Abstract
During natural gas drilling in the EMS region in 1956, considerable numbers of longitudinal cracks and transverse fractures occurred in the connecting pieces of the bore rods. The connectors were screwed onto the rods by means of a fine thread and tightly joined with it by shrinkage at 530 deg C. The connectors were made of SAE 4140 Cr-Mo steel. The material for the rod pipes was Fe-0.4C-1Mn steel. Structural stresses played a role in the cracking. Iron sulfide formed on the fracture planes and flake-like stress cracks occurred in the steel. The hydrogen sulfide content of the gas was the cause of damage. Hydrogen liberated by reaction with the iron caused the formation of iron sulfide after penetration of the steel, which had an explosive effect during molecular separation under high pressure. This in turn caused the crack formation in conjunction with the external and residual stresses.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001408
EISBN: 978-1-62708-220-4
... Abstract Initially, two vertical double-acting two-stage compressors delivering chlorine gas at a pressure of 100 psi appeared to be running satisfactorily. About six months later the LP piston-rod of the No. 2 compressor failed due to burning, the compressor being worked double-acting...
Abstract
Initially, two vertical double-acting two-stage compressors delivering chlorine gas at a pressure of 100 psi appeared to be running satisfactorily. About six months later the LP piston-rod of the No. 2 compressor failed due to burning, the compressor being worked double-acting at the time. About five months later, the HP piston rod of the No. 1 compressor failed in a similar manner. Specimens for microscopic examination were cut from the rod in the region of the failure and from the extreme end that had been situated above the piston and hence not subjected to an appreciable rise in temperature. The material was a steel in the normalized condition with a 0.35% C content. It appears probable that deficient lubrication of the gland resulted in overheating of the rod due to friction. The presence of a sprayed-metal coating was probably an additional factor in promoting failure, as it would present to the gas a surface area considerably greater than that of a homogeneous material.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001174
EISBN: 978-1-62708-220-4
... Abstract A cooler of an ammonia synthesis plant was destroyed after three years of service due to the rupture of a distribution manifold. Synthesis gas under high pressure and at about 300 deg C, consisting of 10% NH3 and unconverted gas of 25% N2 and 75% H2 content, was water-cooled externally...
Abstract
A cooler of an ammonia synthesis plant was destroyed after three years of service due to the rupture of a distribution manifold. Synthesis gas under high pressure and at about 300 deg C, consisting of 10% NH3 and unconverted gas of 25% N2 and 75% H2 content, was water-cooled externally to room temperature in this unit. The fracture had the typical flat-gray fibrous structure of a material destroyed by hydrogen. Specimens for the metallographic investigation showed that the structure appeared to have been loosened by intergranular separations. DVM notched impact specimens from the affected area yielded low specific impact energy values. These are the significant characteristics of hydrogen attack. The attack penetrated to a depth of 13 to 16 mm. It was recommended that the manifolds be made of hydrogen-resistant steel instead of the unalloyed steel used.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048253
EISBN: 978-1-62708-234-1
... Abstract Two intermediate impeller drive gears (made of AMS 6263 steel, gas carburized, hardened, and tempered) exhibited evidence of pitting and abnormal wear after production tests in test-stand engines. The gears were examined for hardness, case depth, and microstructure of case and core...
Abstract
Two intermediate impeller drive gears (made of AMS 6263 steel, gas carburized, hardened, and tempered) exhibited evidence of pitting and abnormal wear after production tests in test-stand engines. The gears were examined for hardness, case depth, and microstructure of case and core. It was found that gear 1 had a lower hardness than specified while the case hardness of gear 2 was found to be within limits. Both the pitting and the wear pattern were revealed to be more severe on gear 1 than on gear 2. Surface-contact fatigue (pitting) of gear 1 (cause of lower carbon content of the carburized case and hence lower hardness) was found to be the reason for failure. It was recommended that the depth of the carburized case on impeller drive gears be increased from 0.4 to 0.6 mm to 0.6 to 0.9 mm to improve load-carrying potential and wear resistance. A minimum case-hardness requirement was set at 81 HRA.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001164
EISBN: 978-1-62708-227-3
.... In order to prevent the possibility of combustion of hydrocarbons the O 2 content of the gas was kept below 10% by volume; a typical composition is [in vol. %] Figure 2 shows the top half of the foot and gives a picture of the extent and distribution of the perforations. Figures 3 and 4...
Abstract
Plate perforation occurred in the cylindrical section and walls of the inlet foot (2.38 mm thick Incoloy 825 plate welded using INCO welding rod 135) of an inert gas fire prevention system in an oil tanker. Cross-sectional microprobe analysis showed the corrosion product to contain sulfur, mainly from the flue gas, and calcium and chlorine, mainly from the sea water. The gray corrosion product was interspersed with rust and a black carbonaceous deposit. Corrosion pitting and poor weld penetration, with carbide precipitation and heavy etching at grain boundaries, indicated sensitization and susceptibility to aqueous intergranular corrosion. Chemical analysis showed the predominant acid radical to be sulfate (6.20% in the carbonaceous deposit and 0.60% in the corrosion product), suggesting that oxidation of SO2 in the flue gas caused the corrosion. Moisture condensation, the carbon acting as a cathode, and alloy susceptibility to intergranular corrosion contributed to the corrosion.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001239
EISBN: 978-1-62708-232-7
... Abstract A coil made of a nickel-chromium alloy (Material No. 2.4869) with approx. 80Ni and 20Cr had burned through after a brief period of operation as a heating element in a brazing furnace. The protective atmosphere consisted of an incompletely combusted coal gas. Furnace temperature reached...
Abstract
A coil made of a nickel-chromium alloy (Material No. 2.4869) with approx. 80Ni and 20Cr had burned through after a brief period of operation as a heating element in a brazing furnace. The protective atmosphere consisted of an incompletely combusted coal gas. Furnace temperature reached 1150 deg C. This type of selective oxidation at which the easily oxidized chromium burns, while the nickel is not attacked, is caused by mildly oxidizing gases and is sometimes designated as green rot. Under these conditions, chromium-containing steels and alloys whose oxidation resistance is based upon formation of tight oxide layers are not stable.
Image
in Failure of Boilers and Related Equipment
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 58 Suggested minimum metal temperatures to avoid flue-gas corrosion in economizers and air heaters plotted as a function of as-fired sulfur contents of various fuels
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001433
EISBN: 978-1-62708-235-8
... band suggested that the weld had been made by the oxy-gas process. A lack of root fusion over most of its length was evident. Examination of the fracture faces, which were of crystalline appearance indicative of brittle behavior, indicated incomplete fusion of the weld root. Microscopic examination...
Abstract
On attempting to manipulate or bend a boiler tube some 22 ft. long, sudden failure occurred at what appeared to be a butt weld in the tube. Externally, the weld reinforcement had been ground flush and the entire tube surface painted. Internally, the appearance and width of the heated band suggested that the weld had been made by the oxy-gas process. A lack of root fusion over most of its length was evident. Examination of the fracture faces, which were of crystalline appearance indicative of brittle behavior, indicated incomplete fusion of the weld root. Microscopic examination showed the deposit to possess a large grain size with a low carbon content disposed as carbides along the grain boundaries, a feature which would provide an explanation of the brittle behavior. Subsequent inspection showed that this tube was one of several of the batch ordered for retubing of a boiler and which had a 2 ft. length welded to one end to make up the length.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001714
EISBN: 978-1-62708-232-7
... it to iron sponge at process temperature. The plant can make 1.000.000 tons of iron sponge per year. Reductor gases contain CO and H 2 and some amounts of CO 2 and H 2 O. This composition is obtained by mixing of reformer gas (fresh gas from reformer) with recycle gas. The CO 2 content of recycle gas...
Abstract
In a HyL III heat exchanger's radiant pipes, metal dusting reduced the pipe thickness from 8.5 to 3 mm in just nine months, leaving craters on the inner surface. The pipes are fabricated from HK 40 alloy. The heated gas (400 to 800 deg C) consisted of CO, CO2, and H2, with a 4:1 CO/CO2 ratio. Metallographic investigations revealed that the surface of the attacked pipes consisted of (Cr, Fe) carbide. The metal dusting was the result of a decomposition process (CO to CO2 + C) that deposited C on the pipe surface. Because of the high temperature, the C subsequently diffused through the surface oxide layer (Cr2O3), triggering a succession of reactions that led to pitting and the formation of craters.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0091362
EISBN: 978-1-62708-220-4
... will result in a flow condition that is turbulent enough to aspirate air into the gas stream, thus contaminating the weld and destroying its mechanical and corrosion properties. The manifold gas system also contributed to this failure. When this system is first used, it is necessary to purge the contents...
Abstract
A nozzle in a wastewater vaporizer began leaking after approximately three years of service with acetic and formic acid wastewaters at 105 deg C (225 deg F) and 414 kPa (60 psig). The shell of the vessel was weld fabricated from 6.4 mm (0.25 in.) E-Brite stainless steel plate and measured 1.5 m (58 in.) in diameter and 8.5 m (28 ft) in length. Investigation (visual inspection, chemical analysis, radiography, dye-penetrant inspection, and hydrostatic testing of all E-Brite welds, 4x images, 100x/200x images electrolytically etched with 10% oxalic acid, and V-notch Charpy testing) supported the conclusion that failure of the nozzle weld was the result of intergranular corrosion caused by the pickup of interstitial elements and subsequent precipitation of chromium carbides and nitrides. Carbon pickup was believed to have been caused by inadequate joint cleaning prior to welding. The increase in the weld nitrogen level was a direct result of inadequate argon gas shielding of the molten weld puddle. Two areas of inadequate shielding were identified: improper gas flow rate for a 19 mm (0.75 in.) diam gas lens nozzle, and contamination of the manifold gas system. Recommendations included changes in the cleaning and welding process.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001062
EISBN: 978-1-62708-214-3
... analysis on the fracture surface was carried out with a secondary ion mass spectrometer (SIMS). For this analysis, nitrogen gas ions ( N 2 + ) accelerated to 20 kV were bombarded on the fracture surface. Fig. 8 shows the effect of molybdenum content on the depth profile of sulfur ion ( 32 S...
Abstract
The causes of internal cracking that occurred in 9% Ni steel castings during manufacture were investigated using a series of eight laboratory castings containing varying amounts of molybdenum. The effect of mold thickness was also investigated. The laboratory castings were subjected to three-point bend testing, and fracture surfaces were examined using SEM fractography, metallography, and depth analysis (SIMS) of the fracture surface. The cracks were found to originate at austenitic grain boundaries that coincided with primary dendrite interfaces. The cracking was attributed to a decrease in grain-boundary cohesion resulting from sulfur segregation. Addition of molybdenum proved effective in preventing cracking. The molybdenum promoted MnS precipitation in the grain and preferentially segregated to the interfaces.
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