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galvanizing
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0046911
EISBN: 978-1-62708-227-3
... Abstract A steel galvanizing vat measuring 3 x 1.2 x 1.2 m (10 x 4 x 4 ft) and made of 19 mm thick carbon steel plate (ASTM A285, grade B)) at a shipbuilding and ship-repair facility failed after only three months of service. To verify suspected failure cause, two T joints were made in 12.5 mm...
Abstract
A steel galvanizing vat measuring 3 x 1.2 x 1.2 m (10 x 4 x 4 ft) and made of 19 mm thick carbon steel plate (ASTM A285, grade B)) at a shipbuilding and ship-repair facility failed after only three months of service. To verify suspected failure cause, two T joints were made in 12.5 mm thick ASTM A285, grade B, steel plate. One joint was welded using the semiautomatic submerged arc process with one pass on each side. A second joint was welded manually by the shielded metal arc process using E6010 welding rod and four passes on each side. The silicon content of the shielded metal arc weld was 0.54%, whereas that of the submerged arc weld was 0.86%. After being weighed, the specimens were submerged in molten zinc for 850 h. Analysis (visual inspection, chemical analysis, 100x 2% nital-etched micrographs) supported the conclusions that the vat failed due to molten-zinc corrosion along elongated ferrite bands, possibly because silicon was dissolved in the ferrite and thus made it more susceptible to attack by the molten zinc. Recommendations included rewelding the vat using the manual shielded metal arc process with at least four passes on each side.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001178
EISBN: 978-1-62708-235-8
... Abstract Eight cylinderhead screws cracked after a short running time in motors. They were made of Fe-0.45C-1Cr steel, had rolled threads, were heat treated to 110 kg/sq mm tensile strength, and were electrolytically galvanized. All fractured at the root of the thread. The surfaces of fracture...
Abstract
Eight cylinderhead screws cracked after a short running time in motors. They were made of Fe-0.45C-1Cr steel, had rolled threads, were heat treated to 110 kg/sq mm tensile strength, and were electrolytically galvanized. All fractured at the root of the thread. The surfaces of fracture were fine-grained and had not spread by rubbing. Because the screws were electrolytically galvanized, failure resulted from “delayed fracture.” Experience has shown that this type of fracture is seen on production parts made of high-strength steels, which absorbed hydrogen during pickling or during a galvanic surface treatment. Such parts will rupture below the elastic limit during continuous stressing. This often occurs only after the expiration of a certain time period, and preferably at locations of stress concentrations such as changes in cross section or threads. As a rule, the hydrogen cannot be verified analytically because most of it escapes again after prolonged storage at room temperature or short heating at 100 to 200 deg C.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001246
EISBN: 978-1-62708-224-2
... Abstract Two sections of a galvanized cable 10.5 A 160 GR +NORM M 9533 (round stranded cable of normal type, h + 6, Langslay, right-handed) were examined. One had a 100 mm long blackish-brown tarnished zone obviously caused by localized heating at one end, inside which the hemp core was missing...
Abstract
Two sections of a galvanized cable 10.5 A 160 GR +NORM M 9533 (round stranded cable of normal type, h + 6, Langslay, right-handed) were examined. One had a 100 mm long blackish-brown tarnished zone obviously caused by localized heating at one end, inside which the hemp core was missing, and the other corresponded to the original condition of the cable. The cause of the damage was unknown. About a third of the wires had fractured and the rest had been cut. All were tensile fractures with a relatively high degree of necking. The cause of the localized heating was unknown. It can only be concluded from the investigation that the temperature did not exceed the Ac3 point of the wire material, which should be about 750 deg C, and that the heating lasted a fairly long time.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046512
EISBN: 978-1-62708-234-1
... been nickel plated. During assembly of the actuators a lubricant containing molybdenum disulfide had been applied to the gaskets as a sealant. The vellum gasket was found to be electrically conductive, and analysis (visual inspection, 500x unetched micrographs, galvanic action testing, and x-ray...
Abstract
Immediately after installation, leakage was observed at the mounting surface of several rebuilt hydraulic actuators that had been in storage for up to three years. At each joint, there was an aluminum alloy spacer and a vellum gasket. The mounting flanges of the steel actuators had been nickel plated. During assembly of the actuators a lubricant containing molybdenum disulfide had been applied to the gaskets as a sealant. The vellum gasket was found to be electrically conductive, and analysis (visual inspection, 500x unetched micrographs, galvanic action testing, and x-ray diffraction) supported the conclusions that leakage was the result of galvanic corrosion of the aluminum alloy spacers while in storage. The molybdenum disulfide was apparently suspended in a volatile water-containing vehicle that acted as an electrolyte between the aluminum alloy spacer and the nickel-plated steel actuator housing. Initially, the vellum gasket acted as an insulator, but the water-containing lubricant gradually impregnated the vellum gasket, establishing a galvanic couple. Recommendations included discontinuing use of molybdenum disulfide lubricant as a gasket sealer, and assembling the actuators using dry vellum gaskets.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001651
EISBN: 978-1-62708-229-7
... at the inside surfaces of the tubes. Transgranular stress-corrosion cracking, probably the result of sulphates under basic conditions, and dezincification occurred also as the result of galvanic corrosion under the deposits in the tubes. Recommendations were to use a closed-loop water system to eliminate...
Abstract
Some of the admiralty brass tubes were failing in a heat exchanger. The heat exchanger cooled air by passing river water through the inside of the tubes. The wall thickness of all tubes ranged between 1.19 to 1.27 mm (0.047 to 0.050 in.). General intergranular corrosion occurred at the inside surfaces of the tubes. Transgranular stress-corrosion cracking, probably the result of sulphates under basic conditions, and dezincification occurred also as the result of galvanic corrosion under the deposits in the tubes. Recommendations were to use a closed-loop water system to eliminate sulphates, ammonia, etc., and to run trials on one unit with tubes of other alloys such as 80-20 Cu-Ni or 70-30 Cu-Ni to evaluate their performance prior to any large scale retubing operations.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001336
EISBN: 978-1-62708-215-0
... solution. It was determined that the assemblies failed due to an austenite-martensite galvanic couple activated by a chlorine bearing electrolyte. The martensitic areas resulted from a transformation during cold-forming operations. Solution annealing after forming, revision of the design of the pipe flange...
Abstract
Catastrophic pitting corrosion occurred in type 304L stainless steel pipe flange assemblies in an industrial food processor. During regular service the pumped medium was pureed vegetables. In situ maintenance procedures included cleaning of the assemblies with a sodium hypochlorite solution. It was determined that the assemblies failed due to an austenite-martensite galvanic couple activated by a chlorine bearing electrolyte. The martensitic areas resulted from a transformation during cold-forming operations. Solution annealing after forming, revision of the design of the pipe flange assemblies to eliminate the forming operation, and removal of the source of chlorine were recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046535
EISBN: 978-1-62708-234-1
... in the backfill revealed the site of failure. Analysis (visual inspection, electrical conductivity, and soil analysis) supported the conclusions that the failure had resulted from galvanic corrosion at a point where the corrosivity of the soil was substantially greater than the average, resulting in a voltage...
Abstract
One of five underground drain lines intended to carry a highly acidic effluent from a chemical-processing plant to distant holding tanks failed in just a few months. Each line was made of 304L stainless steel pipe 73 mm (2 in.) in diam with a 5 mm (0.203 in.) wall thickness. Lengths of pipe were joined by shielded metal arc welding. Soundness of the welded joints was determined by water back-pressure testing after several lengths of pipe had been installed and joined. Before completion of the pipeline, a pressure drop was observed during back-pressure testing. An extreme depression in the backfill revealed the site of failure. Analysis (visual inspection, electrical conductivity, and soil analysis) supported the conclusions that the failure had resulted from galvanic corrosion at a point where the corrosivity of the soil was substantially greater than the average, resulting in a voltage decrease near the point of failure of about 1.3 to 1.7 V. Recommendations included that the pipelines be asphalt coated and enclosed in a concrete trough with a concrete cover. Also, magnesium anodes, connected electrically to each line, should be installed at periodic intervals along their entire length to provide cathodic protection.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0046505
EISBN: 978-1-62708-219-8
... was occasionally used in the system. Analysis (visual inspection and 250x micrograph) supported the conclusions that failure of the latch was caused by plastic deformation from extensive loss of metal by galvanic corrosion and the sudden loading related to the tripping of the valve. Failure in some regions...
Abstract
One of three valves in a dry automatic sprinkler system tripped accidentally, thus activating the sprinklers. Maintenance records showed that the three valves had been in service less than two years. The valve consisted of a cast copper alloy clapper plate that was held closed by a pivoted malleable iron latch. The latch and top surface of the clapper plate were usually in a sanitary-water environment (stabilized, chlorinated well water with a pH of 7.3) under stagnant conditions. Process make-up water that had been clarified, filtered, softened, and chlorinated and had a pH of 9.8 was occasionally used in the system. Analysis (visual inspection and 250x micrograph) supported the conclusions that failure of the latch was caused by plastic deformation from extensive loss of metal by galvanic corrosion and the sudden loading related to the tripping of the valve. Failure in some regions of the contact area was by ductile (transgranular) fracture. Recommendations included changing the latch material from malleable iron to silicon bronze (C87300). The use of silicon bronze prevents corrosion or galvanic attack and proper adjustment of the latch maintains an adequate contact area.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0046079
EISBN: 978-1-62708-233-4
... Abstract After only a short time in service, oil-fired orchard heaters made of galvanized low-carbon steel pipe, 0.5 mm (0.020 in.) in thickness, became sensitive to impact, particularly during handling and storage. Most failures occurred in an area of the heater shell that normally reached...
Abstract
After only a short time in service, oil-fired orchard heaters made of galvanized low-carbon steel pipe, 0.5 mm (0.020 in.) in thickness, became sensitive to impact, particularly during handling and storage. Most failures occurred in an area of the heater shell that normally reached the highest temperature in service. A 400x etched micrograph showed a brittle and somewhat porous metallic layer about 0.025 mm (0.001 in.) thick on both surfaces of the sheet. Next to this was an apparently single-phase region nearly 0.05 mm (0.002 in.) in thickness. The examination supported the conclusion that prolonged heating of the galvanized steel heater shells caused the zinc-rich surface to become alloyed with iron and reduce the number of layers. Also, heating caused zinc to diffuse along grain boundaries toward the center of the sheet. Zinc in the grain boundaries reacted with iron to form the brittle intergranular phase, resulting in failure by brittle fracture at low impact loads during handling and storage. Recommendation included manufacture of the pipe with aluminized instead of galvanized steel sheet for the combustion chamber.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001100
EISBN: 978-1-62708-214-3
... Abstract Galvanized A36 steel unsleeved shear-type anchor bolts failed during installation. The galvanized steel bolts were approximately 18 mm (0.7 in.) in diameter with a 90 deg bend between the long and short legs. As-fractured, sawcut, and unfractured specimens were examined. Failure...
Abstract
Galvanized A36 steel unsleeved shear-type anchor bolts failed during installation. The galvanized steel bolts were approximately 18 mm (0.7 in.) in diameter with a 90 deg bend between the long and short legs. As-fractured, sawcut, and unfractured specimens were examined. Failure analysis revealed dark thumbnail regions at the fracture origins and a very narrow and uniform shear lip. The thumbnail region exhibited zinc deposits with no apparent fracture detail, indicating preexisting cracks that had occurred before galvanizing. The balance of the fracture exhibited a transgranular mode with cleavage and ductile, dimpled shear. Hardness values as high as 35 HRC were measured in the bend area. The as-galvanized bolts fractured in a brittle manner. Failure was attributed to improper bending of the bolts, which provided a severely cold-worked bend area susceptible to strain-age embrittlement.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001824
EISBN: 978-1-62708-241-9
... (which included visual, macroscopic, metallographic, SEM, and chemical analysis) showed that austenitic stainless steel and a nickel-base alloy were used instead. The unspecified materials are more prone to corrosion, particularly galvanic corrosion, which proved to be the primary failure mechanism...
Abstract
Nineteen out of 26 bolts in a multistage water pump corroded and cracked after a short time in a severe working environment containing saline water, CO 2 , and H 2 S. The failed bolts and intact nuts were to be made from a special type of stainless steel as per ASTM A 193 B8S and A 194. However, the investigation (which included visual, macroscopic, metallographic, SEM, and chemical analysis) showed that austenitic stainless steel and a nickel-base alloy were used instead. The unspecified materials are more prone to corrosion, particularly galvanic corrosion, which proved to be the primary failure mechanism in the areas of the bolts directly exposed to the working environment. Corrosion damage on surfaces facing away from the work environment was caused primarily by chloride stress-corrosion cracking, aided by loose fitting threads. Thread gaps constitute a crevice where an aggressive chemistry is allowed to develop and attack local surfaces.
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in Metallographic Studies of the U.S.S. Arizona
> ASM Failure Analysis Case Histories: Offshore, Shipbuilding, and Marine Equipment
Published: 01 June 2019
Fig. 9 Boat deck locker sample WB3, longitudinal galvanized section, 450×. 2% Nital etch.
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in Wire Fractures in Suspension Cables of a Twisted Cable Suspension Bridge
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
Fig. 1 Fracture of a galvanized outer wire, fracture origin designated by arrow. 5 ×
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in Wire Fractures in Suspension Cables of a Twisted Cable Suspension Bridge
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
Fig. 5 Fissure with contiguous stress crack in fractured galvanized wire. Longitudinal section through edge from which fracture propagated, unetched. 100 ×
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in Wire Fractures in Suspension Cables of a Twisted Cable Suspension Bridge
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
Fig. 6 Transverse crack in non-fractured galvanized wire, longitudinal section through fissured edge, etch: Picral 100 ×
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in Brittle Fracture of Galvanized Steel Heater Shells Because of Embrittlement by Intermetallic Compounds
> ASM Failure Analysis Case Histories: Design Flaws
Published: 01 June 2019
Fig. 1 Orchard heater of galvanized low-carbon steel that broke in a brittle manner because of an iron-zinc intermetallic compound along the grain boundaries. Dimensions given in inches. View A-A: micrograph of an etched section that shows the microstructure of the steel sheet. 400x
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in Failures of Structures and Components by Metal-Induced Embrittlement
> Handbook of Case Histories in Failure Analysis
Published: 01 December 2019
Fig. 25 Macroscopic views of the galvanized carbon-steel stiffeners showing ( a , b ) cracks at the outside of the bend, and ( c ) fracture surface partially covered by a film of zinc
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Published: 01 December 1993
Fig. 8 (a) Microstructure of galvanized sheet. Longitudinal section. Microstructure consists of pearlite and primary ferrite. Note coarse pearlite and divorced cementite. (b) Higher magnification of Fig. 8 .
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in Fractures of Hot Dip Galvanized Steel Anchor Bolts in Chemical Plant Construction Project
> Handbook of Case Histories in Failure Analysis
Published: 01 December 1992
Fig. 1 As-fractured galvanized anchor bolt. Arrow indicates fracture location.
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Published: 01 January 2002
Fig. 16 Galvanic attack at a water pipe joint involving dissimilar metals
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