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forging alloys

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001196
EISBN: 978-1-62708-224-2
... Abstract A forged alloy steel arm of a lifting fork with an approximate cross section of 150 x 240 mm (5.92 x 9.45 in.) fractured after only a short service life on a lift truck. The fracture surface had the appearance of a fracture originating from a surface crack. Analysis (visual inspection...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001022
EISBN: 978-1-62708-214-3
... grain-boundary attack. 305×. Fig. 16 Typical stress-corrosion crack in part 2. 315×. Abstract Two complete aircraft undercarriage-leg 2014 aluminum alloy forgings and a number of sectional ends that exhibited cracks during nondestructive testing were examined to determine the extent...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001553
EISBN: 978-1-62708-217-4
... Decarburizing Forgings Alloy steel Heat treating-related failures Fatigue fracture During examination of a failed engine in which a connecting rod had ruptured in fatigue, investigators were unable to detect any evidence of excessive stresses, detonation, overheating, or oil starvation. Though...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001270
EISBN: 978-1-62708-215-0
...-alloy medium-carbon steel forgings. The cracks were present on as-forged parts and grew during heat treatment. Examination revealed that areas near the parting line exhibited a large grain structure not present in the forged stock. High-temperature scale was also found in the cracks. It was concluded...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001283
EISBN: 978-1-62708-215-0
... the preproduction stages of forging, an initial batch of 50 mm (2 in.) diam Al-4Cu alloy (L77) extruded bar stock material was found to be cracking randomly. Failure analysis was conducted to determine the metallurgical factors underlying the phenomenon. Microexamination of sections across the defects revealed...
Image
Published: 01 June 2019
Fig. 1 Catapult-hook attachment fitting forged from aluminum alloy 2014-T6. The component cracked during straightening, then fractured in service More
Image
Published: 01 June 2019
Fig. 1 Forged aluminum alloy 2014-T6 actuator barrel lug that failed by SCC. (a) View of the lug. 2×. Fracture at top was the initial fracture; arrow indicates location of a tiny region of pitting corrosion (on back side of lug) at which failure originated. Final fracture is at left. (b More
Image
Published: 01 June 2019
Fig. 1 Forged aluminum alloy 7075-T6 receiver from an M16 rifle that failed by exfoliation corrosion. (a) Rifle receiver. 0.7×. Similar receivers were forged from three different materials to investigate the effects of processing on exfoliation resistance ( Table 1 ). Section A-A: (b), (c More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047169
EISBN: 978-1-62708-217-4
... Abstract The flange on an outboard main-wheel half (aluminum alloy 2014-T6 forging) on a commercial aircraft fractured during takeoff. The failure was discovered later during a routine enroute check. The flange section that broke away was recovered at the airfield from which the plane took off...
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006835
EISBN: 978-1-62708-329-4
... of wrought products. The article addresses the types of flaws or defects that can be introduced during the steel forging process itself, including defects originating in the ingot-casting process. Defects found in nonferrous forgings—titanium, aluminum, and copper and copper alloys—also are covered...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046022
EISBN: 978-1-62708-217-4
... Abstract A forged aluminum alloy 2014-T6 catapult-hook attachment fitting (anodized by the chromic acid process to protect it from corrosion) from a naval aircraft broke in service. Spectrographic analysis, visual examination, microscopic examination, and tensile analysis showed minute cracks...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046146
EISBN: 978-1-62708-217-4
... Abstract The torque-arm assembly (aluminum alloy 7075-T73) for an aircraft nose landing gear failed after 22,779 simulated flights. The part, made from an aluminum alloy 7075-T73 forging, had an expected life of 100,000 simulated flights. Initial study of the fracture surfaces indicated...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047199
EISBN: 978-1-62708-234-1
... Abstract The lower receiver of the M16 rifle is an anodized forging of aluminum alloy 7075-T6. Degradation of the receivers was observed after three years of service in a hot, humid atmosphere. The affected areas were those in frequent contact with the user's hands. There was no question...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089256
EISBN: 978-1-62708-235-8
... Abstract Alloy steel forgings used as structural members of a ski chair lift grip mechanism were identified to have contained forging laps (i.e., sharp-notched discontinuities) during an annual magnetic particle inspection of all chair lift grip structural members at a mountain resort...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047165
EISBN: 978-1-62708-217-4
... Abstract Two outboard main-wheel halves (aluminum alloy 2014-T6 forged) from a commercial aircraft were removed from service because of failure. One wheel half was in service for 54 days and had made 130 landings (about 1046 roll km, or 650 roll mi) when crack indications were discovered during...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003507
EISBN: 978-1-62708-180-1
... (such as inclusions or matrix interfaces). Flaking or hairline cracking in steels, particularly in forgings, heavy-section alloy plate steels, and railroad rails, has been an ongoing problem since the beginning of steelmaking and is reviewed in Ref 6 . At still higher concentrations of hydrogen in metal, blistering...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047125
EISBN: 978-1-62708-217-4
... Abstract A commercial aircraft wheel half, machined from an aluminum alloy 2014 forging that had been heat treated to the T6 temper, was removed from service because a crack was discovered in the area of the grease-dam radius during a routine inspection. Neither the total number of landings nor...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001541
EISBN: 978-1-62708-235-8
... Abstract A forging of 7075-T6 aluminum alloy, which formed a support for the cylinder of a cargo door, cracked at an attachment hole. Fluorescent penetrant inspection showed the crack ran above and below the hole out onto the machined flat surface of the flange. A 6500x electron fractograph...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091674
EISBN: 978-1-62708-217-4
... Abstract Forged aluminum alloy 2014-T6 hinge brackets in naval aircraft rudder and aileron linkages were found cracked in service. The cracks were in the hinge lugs, adjacent to a bushing made of cadmium-plated 4130 steel. Investigation (visual inspection and 250X micrographs) supported...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001292
EISBN: 978-1-62708-215-0
... the point of fatigue initiation. Etched in Tucker's reagent. 7.70× Abstract A crack was detected in one arm of the right-hand horizontal brace of the nose landing gear shock strut from a large military aircraft. The shock strut was manufactured from a 7049 aluminum alloy forging in the shape...