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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001254
EISBN: 978-1-62708-225-9
... Abstract The specified elongation of 10% could not be achieved in several hollow pinion gear shafts made of cast Cr-Mo steel GS 35 Cr-Mo 5 3 that were heat treated to a strength of 90 kp/sq mm. The steel was melted in a basic 3 ton arc furnace and deoxidized in the furnace and in the pan...
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Published: 01 June 2019
Fig. 24 Total elongation (in tension) as a function of dose for the current tests (♦), data from Ref 10 (▪), and neutron-irradiated alloy 718 from EBR II (X, Δ) 1 More
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Published: 01 June 2019
Fig. 20 Showing minimum elongation of copper in region of 550°–600°C. More
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Published: 01 June 2019
Fig. 3 Subsurface inclusion cluster of tensile specimen with 7% elongation. More
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Published: 01 December 2019
Fig. 6 Microstructure of sample 2a, 6.3 mm (¼ in.) from fracture. Elongation of grains is due to elevated-temperature deformation. More
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Published: 01 December 2019
Fig. 8 Microstructure of sample 2a at fracture. Severe elongation of grains is observed due to elevated-temperature deformation. Similar elongation was seen at all locations on side A where substantial thinning had occurred. More
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Published: 01 December 2019
Fig. 10 Severe elongation of grains in formed adiabatic shear bands in vicinity of interface More
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Published: 01 June 2019
Fig. 3 Polarized light image (90×) of elongate yellow-hued carbonate-enriched reaction product More
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Published: 01 June 2019
Fig. 6 Region showing elongated dimples (microvoid coalescence) in the exemplar torsional load specimen. More
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Published: 01 December 1992
Fig. 9 Typical elongated grain structure in longitudinal cross section through severe bend area of unfractured bolt. Nital etch. More
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Published: 01 December 1992
Fig. 4 SEM micrographs of the failed unit. Note elongated grains at the cup rim. (a) Higher-magnification view of boxed area in (b). More
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Published: 01 December 2019
Fig. 8 Hydrogen induced microcracks emanated from ( a ) elongated FeS, ( b ) acicular MnS inclusion in A216 steel More
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Published: 01 December 1993
Fig. 1 Rear valve guide, showing transverse fracture through an elongated hole. No plastic deformation was evident around the fracture zone. More
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Published: 01 December 1993
Fig. 3 Microstructure of the bellows material, showing flow lines and elongated grains More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091669
EISBN: 978-1-62708-227-3
... of the aluminum alloy coupling nuts was caused by stress corrosion. Contributing factors included use of a material that is susceptible to this type of failure, sustained tensile stressing in the presence of a marine (chloride-bearing) atmosphere, and an elongated grain structure transverse to the direction...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0047694
EISBN: 978-1-62708-219-8
... Abstract Extra high strength zinc-coated 1080 steel welded wire was wound into seven-wire cable strands for use in aerial cables and guy wires. The wires and cable strands failed tensile, elongation, and wrap tests, with wires fracturing near welds at 2.5 to 3.5% elongation and through...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001154
EISBN: 978-1-62708-223-5
... Abstract The cause of fracture of two piston rods of hammers of a drop forge was determined. The first rod of 180 mm diam consisted of an unalloyed steel with 0.37% C and 0.67% Mn and had a strength of 56 kp/sq mm at 26% elongation. Fatigue fractures propagated from several points which could...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001712
EISBN: 978-1-62708-234-1
... Abstract A failure analysis was conducted in late 1996 on two rolls that had been used in the production of iron and steel powder. The rolls had elongated over their length such that the roll trunnions had impacted with the furnace wall refractory. The result was distortion and bowing...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0046911
EISBN: 978-1-62708-227-3
... along elongated ferrite bands, possibly because silicon was dissolved in the ferrite and thus made it more susceptible to attack by the molten zinc. Recommendations included rewelding the vat using the manual shielded metal arc process with at least four passes on each side. Hot dip galvanizing...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047991
EISBN: 978-1-62708-225-9
... austenitized. Displacement of metal on the outer raceway was revealed by elongation of grain structure. It was concluded that the failure of the raceway surface was due to incomplete austenitization caused by the improper heat treatment during flame hardening process. Antennas Austenitizing Bearing...