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corrosion repair

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Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001067
EISBN: 978-1-62708-214-3
... this mode of cracking. It was recommended that weld seams be furnace heat treated at a temperature of 600 to 640 deg C (1110 to 1180 deg F) for a minimum of 1 h per inch of section thickness. Chemical processing equipment Heat-affected zone Pipe, corrosion Repair welding Welded joints, corrosion...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001349
EISBN: 978-1-62708-215-0
... of factors resulted in failure by stress-corrosion cracking. Implementation of a new repair procedure was recommended. Repairs were successfully made using the new procedure, and all cracks in the weld repair zones were eliminated. Domes Heat-affected zone Nuclear reactor components Nuclear reactors...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001650
EISBN: 978-1-62708-230-3
... to the manufacturer for repair. Some of the units failed the hydrostatic test after they were repaired. Microscopic examination revealed the presence of branched transgranular cracks characteristic of stress-corrosion cracking. Only some of the tubes failed and these did so by stress-corrosion cracking. The most...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001047
EISBN: 978-1-62708-214-3
... joint allowed the Nox to condense and subsequently reboil. This, coupled with repeated repair welding in the area, reduced resistance to acid attack. Intergranular corrosion continued until failure. Recommendations included changing operating parameter inlet to prevent HNO3 condensation outside...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091678
EISBN: 978-1-62708-217-4
...) supported the conclusion that the cause of failure was SCC resulting from exposure to a marine environment. The fracture occurred in normal operation at a point where damage from pitting and intergranular corrosion acted as a stress raiser, not because of overload. The pitting and intergranular attack...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0091622
EISBN: 978-1-62708-230-3
... Abstract A CF-8M (cast type 316) neck liner or manway was removed from the top of a digester vessel. Repeated attempts to repair the part in the field during its life cycle of many years had failed to keep the unit from leaking. The casting was a CF-8M modified with the molybdenum level...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001402
EISBN: 978-1-62708-220-4
...- and transgranular cracking. It is probable that the heating associated with the repair welds made from time to time also contributed to the trouble. The transgranular cracks, however, were indicative of stress-corrosion cracking. Chemical processing equipment Repair welding Storage vessels Vessels Weld...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0090943
EISBN: 978-1-62708-219-8
... by a progressive mechanism such as fatigue or stress-corrosion cracking (SSC). The cracking was not associated with regions that would be highly stressed and did not appear to be consistently correlated to casting imperfections, repair welds, or the associated heat-affected zones. The cast gear was a high-strength...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001569
EISBN: 978-1-62708-229-7
... in operation and maintenance/repair may increase a part's exposure and likelihood of failure during the part's life. Corrosion may assist the fatigue process to various degrees. Generally, it lowers the threshold stress for fatigue. It may act to roughen the surface of a part producing localized stress...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091330
EISBN: 978-1-62708-234-1
... conducted heat from the chimney and reheated the condensate. Investigation (visual inspection and welded coupon testing) supported the conclusion that the corrosion was caused by “Green Death,” a corrosive medium used to test for pitting resistance (11.9% H2SO4 + 1.3% HCl + 1% FeCl3 + 1% CuCl2) at 103 deg C...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091655
EISBN: 978-1-62708-229-7
.... An Inconel 600 thermal sleeve was welded to the safe-end, and a repair weld had obviously been made on the outside surface of the safe-end to correct a machining error. Initial visual examination of the safe-end disclosed that the cracking extended over approximately 85 deg of the circular circumference...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001365
EISBN: 978-1-62708-215-0
... cross sections removed from the impeller body. Areas that appeared to have the most severe surface damage were sectioned, fractured open, and examined using SEM. The chemistry of the impeller and an apparent repair weld were also analyzed. The examination indicated that the cracks were shrinkage voids...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047636
EISBN: 978-1-62708-217-4
... stresses. The fracture of the second elbow near the flange was caused by overaging during repair welding of the boss weld. Satisfactory weld penetration was achieved by improved training of the welders plus more careful inspection. Repair welding was prohibited, to avoid recurrence of overaging from...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001082
EISBN: 978-1-62708-214-3
... of solutions involving material selection and impeller redesign were recommended. Castings Chlorides, environment Propellers Repair welding Vibratory stresses 304L UNS S30403 Stress-corrosion cracking Fatigue fracture Background Several large-diameter impeller/propeller blades...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001317
EISBN: 978-1-62708-215-0
... Abstract Two AISI type 316 stainless steel dished ends failed through the formation of intergranular stress-corrosion cracks (IGSCC) within a few months of service. The dished ends failed in the straight portions near the circumferential welds that joined the ends to the cylindrical portions...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001675
EISBN: 978-1-62708-220-4
... in size, and the area repaired by welding. Subsequently, other deep cracks were found and the maintenance practice has consisted of welding only when the removal of defects was complete. The first failure in service occurred after 4,500 h of operation, on the north side of the tee, where repairs had...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0047615
EISBN: 978-1-62708-230-3
... in the area of the fin tip. Cracking at the end of the fin-to-tube fillet weld was noted. The results indicate the failures were due to corrosion fatigue whose stresses were primarily thermally induced. A temporary solution included inspecting all tubes with shear-wave ultrasonics. Tubes with the most severe...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001726
EISBN: 978-1-62708-234-1
... or no loss in wall thickness due to corrosion or scaling, and the tube wall was thinned to a knife edge at the rupture. Metallographic examination showed the condition of the material was satisfactory. The failure was mechanical in nature, typical of short time creep rupture. The localized oxidation...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001653
EISBN: 978-1-62708-219-8
..., the color near the key changed from yellow to red-brown. The gate was made from leaded red brass (85-5-5-5) while the spindle was made from silicon brass. It was concluded that the valves failed by dezincification resulting from bimetallic galvanic corrosion. It is common in the valve industry to use...
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Published: 01 January 2002
Fig. 5 Two views of severe corrosion of wastewater tunnel structure. Note the failed lining repairs. Courtesy of S. Paul, CorrTech, Inc. More