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corrosion in water
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001698
EISBN: 978-1-62708-222-8
... evaluation of a cross section of a copper pipe revealed extensive pitting corrosion throughout the inner diametral surfaces of the pipe. Some pits had penetrated through the wall thickness, causing the pin hole leaks. Analysis of a sample of water obtained from the subdivision revealed relatively high...
Abstract
A residential subdivision near Tampa, FL was constructed in 1984 through 1985. Several sections of copper pipe were removed from one residence that had reported severe leaking. Visual examination revealed extensive pitting corrosion throughout the ID surfaces of the sample. Microscopic evaluation of a cross section of a copper pipe revealed extensive pitting corrosion throughout the inner diametral surfaces of the pipe. Some pits had penetrated through the wall thickness, causing the pin hole leaks. Analysis of a sample of water obtained from the subdivision revealed relatively high hardness levels (210 mg/l), high levels of sulfate ions (55 mg/l), a pH of 7.6 and a sulfate-to-chloride ratio of 3:1. Analysis of corrosion product removed from the ID surfaces of the pipe section revealed that an environment rich in carbonates existed inside the pipe, a result of the hard water supply. It was concluded that pitting corrosion was a result of the corrosive waters supplied by the local water utility. Waters could be rendered non-pitting by increasing their pH to 8 or higher and neutralizing the free carbon dioxide.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0047335
EISBN: 978-1-62708-219-8
... Abstract A section of cast iron water main pipe contained a hole approximately 6.4 x 3.8 cm (2.5 x 1.5 in.). The pipe was laid in clay type soil. Examination revealed severe pitting around the hole and at the opposite side of the outside diam. A macroscopic examination of a pipe section...
Abstract
A section of cast iron water main pipe contained a hole approximately 6.4 x 3.8 cm (2.5 x 1.5 in.). The pipe was laid in clay type soil. Examination revealed severe pitting around the hole and at the opposite side of the outside diam. A macroscopic examination of a pipe section at the hole area showed that the porosity extended a considerable distance into the pipe wall. Metallographic examination revealed a graphite structure distribution expected in centrifugally cast iron with a hypoeutectic carbon equivalent. Chemical analyses of a nonporous sample had a composition typical of cast iron pipe. Chemical analyses of the porous region had a substantial increase in carbon, silicon, phosphorus, and sulfur. The porous appearance and the composition of the soft porous residue confirmed graphitic corrosion. The selective leaching of iron leaves a residue rich in carbon, silicon, and phosphorus. The high sulfur content is attributed to ferrous sulfide from a sulfate reducing bacteria frequently associated with clay soils. Reinforced coal tar protective coating was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001701
EISBN: 978-1-62708-219-8
... by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system. Water chemistry Water heaters Water pipelines Water treatment ASTM A106 UNS K03006 Crevice corrosion...
Abstract
A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials. The fittings were mechanically threaded assemblies. Temperatures ranged from 150 to 155 deg F (65.6 to 68.3 deg C). Leaks in the system had reportedly initiated immediately after the building had been placed in service. The cause of corrosion inside the steel pipes was attributed to tuberculation caused by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001700
EISBN: 978-1-62708-229-7
... and microscopic analysis revealed several large and small well rounded corrosion pits present at the inner diametral surfaces. The cause of corrosion was attributed to corrosive waters that were not only corroding the copper, but were corroding steel pipes upstream from the tubing. Grinding mills Heat...
Abstract
A straight-tube cooler type heat exchanger had been in service for about ten years serving a coal pulverizer in Georgia. Non-potable cooling water from a local lake passed through the inner surfaces of the copper tubing and was cooling the hot oil that surrounded the outer diametral surfaces. Several of the heat exchangers used in the same application at the plant had experienced a severe reduction in efficiency in the past few years. One heat exchanger reportedly experienced some form of leakage following discovery of oil contaminating the cooling water. This heat exchanger was the subject of a failure investigation to determine the cause and location of the leaks. Corrosion products primarily contained copper oxide, as would be expected from a copper tubing. The product also exhibited the presence of a significant amount of iron oxides. Metallographic cross sectioning of the tubes and microscopic analysis revealed several large and small well rounded corrosion pits present at the inner diametral surfaces. The cause of corrosion was attributed to corrosive waters that were not only corroding the copper, but were corroding steel pipes upstream from the tubing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001704
EISBN: 978-1-62708-218-1
.... The examinations revealed a classic case of microbiologically influenced corrosion (MIC), which preferentially attacked the heat affected zones of the tank welds, resulting in the leaks. Heat affected zone Leakage Water tanks Welded joints 304 UNS S30400 Biological corrosion The experienced...
Abstract
Several type 304 stainless steel fire truck water tanks developed through-wall leaks after being in service for approximately two years. One representative tank underwent a comprehensive laboratory analysis, which included metallographic examinations and chemical analyses. The examinations revealed a classic case of microbiologically influenced corrosion (MIC), which preferentially attacked the heat affected zones of the tank welds, resulting in the leaks.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048318
EISBN: 978-1-62708-234-1
... of 9.0 and 200 ppm of sodium sulfite should be added to the water. pH Purging Water chemistry Water treatment ASME SA276 Pitting corrosion A resistance-welded carbon steel superheater tube made to ASME SA-276 specifications failed by pitting corrosion and subsequent perforation ( Fig. 1...
Abstract
A resistance-welded carbon steel superheater tube made to ASME SA-276 specifications failed by pitting corrosion and subsequent perforation, which caused the tube to leak. The perforation was found to have occurred at a low point in a bend near the superheater outlet header. It was found that the low points of the superheater tubes could not be completely drained during idle periods. Water-level marks were noticed on the inside surface above the area of pitting. It was revealed by microscopic examination that localized pitting had resulted from oxidation. It was concluded that water contained in the tube during shutdowns had accumulated and cumulative damage due to oxygen pitting resulted in perforation of one of the tubes. Filling the system with condensate or with treated boiler water was suggested as a corrective action. Alkalinity was suggested to be maintained at a pH of 9.0 and 200 ppm of sodium sulfite should be added to the water.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001063
EISBN: 978-1-62708-214-3
... to stagnant water on the shell side. It was recommended that the surfaces not be kept in contacts with closed stagnant water for appreciable lengths of time. Chemical processing equipment Condenser tubes, corrosion Condensers 316 UNS S31600 Pitting corrosion Background Several tubes...
Abstract
Several tubes in a 35 m 2 (115 ft 2 ) type 316 stainless steel shell-and-tube condenser leaked unexpectedly in an organic chemical plant that produces vinyl acetate monomer. Leaks were discovered after 5 years of operation and relocation of the condenser to another unit in the same plant. Examination of tubes and tube sheets revealed pitting damage on the OD surface. Some of the pits had penetrated fully, resulting in holes. Inside diameter surfaces were free of corrosion. Macro- and microexaminations indicated that the tubes had been properly manufactured. Pitting was attributed to stagnant water on the shell side. It was recommended that the surfaces not be kept in contacts with closed stagnant water for appreciable lengths of time.
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in Failure of Nickel-Aluminum-Bronze Hydraulic Couplings, with Comments on General Procedures for Failure Analysis
> ASM Failure Analysis Case Histories: Offshore, Shipbuilding, and Marine Equipment
Published: 01 June 2019
Fig. 15 Stress-corrosion fracture in a Cu-30Zn brass tested in water containing sulfur dioxide showing crack-arrest markings due to the discontinuous nature of crack propagation 10
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001697
EISBN: 978-1-62708-219-8
... Abstract Corrosion in potable and nonpotable water systems has been well documented in the past, and new research discusses innovations in water treatment and materials that are designed to enhance the quality of a water system, whether commercial or residential. This paper is a collection...
Abstract
Corrosion in potable and nonpotable water systems has been well documented in the past, and new research discusses innovations in water treatment and materials that are designed to enhance the quality of a water system, whether commercial or residential. This paper is a collection of five case histories on the failure of copper and steels as used in potable and non-potable water systems. The case histories cover a range of applications in which copper and steel products have been used. Copper and steel pipes are the two most commonly used materials in residential, commercial and industrial applications. The projects that are discussed cover these three important applications. The purpose of presenting this information is to allow the reader to gain an understanding of real life corrosion issues that affect plumbing materials, how they should have been addressed during the design of the water system, and how a water system should be maintained during service. We share this information in the hope that the reader will gain some limited knowledge of the problems that exist, and apply that knowledge in designing or using water systems in day-to day life.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001683
EISBN: 978-1-62708-234-1
... Abstract Corrosion in a closed-loop cooling water system constructed of austenitic stainless steel occurred during an extended lay up of the system with biologically contaminated water. The characteristics of the failure were those of microbiologically influenced corrosion (MIC). The corrosion...
Abstract
Corrosion in a closed-loop cooling water system constructed of austenitic stainless steel occurred during an extended lay up of the system with biologically contaminated water. The characteristics of the failure were those of microbiologically influenced corrosion (MIC). The corrosion occurred at welds and consisted of large subsurface void formations with pinhole penetrations of the surfaces. Corrosive attack initiated in the heat affected zones of the welds, usually immediately adjacent to fusion lines. Stepwise grinding, polishing, and etching through the affected areas revealed that voids generally grew in the wrought material by uniform general corrosion. Tunneling or worm-holing was also observed, whereby void extension occurred by initiating daughter voids probably at flaws or other inhomogeneities. Selective attack occurred within the fusion zone, i.e., within the cast two-phase structure of the weld filler itself. The result was a void wall which consisted of a rough and porous ferritic material, a consequence of preferential attack of the austenitic phase and slightly lower rate of corrosive attack of the ferrite phase. The three-dimensional spongy surface was studied optically and with the scanning electron microscope.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
... resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron...
Abstract
A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall perforations and cracking along its axis. The perforations and the crack were at the 6 o'clock position. Investigation (visual inspection, radiography, unetched macrographs, and tensile testing) supported the conclusion that the failure occurred as result of years of exposure to ground water in the soil resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron or coated and lined steel pipe, generally not susceptible to graphitic corrosion, were suggested as suitable replacement materials, and cathodic protection was also considered as a possibility.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001243
EISBN: 978-1-62708-225-9
... Abstract A needle bearing from a filling and seating machine for milk cartons became unusable due to corrosion and fracture of a ring after only four weeks of operation of the machine in a Finnish milk packing plant. These bearings were subject to corrosion by water condensates in this type...
Abstract
A needle bearing from a filling and seating machine for milk cartons became unusable due to corrosion and fracture of a ring after only four weeks of operation of the machine in a Finnish milk packing plant. These bearings were subject to corrosion by water condensates in this type of environment because of constant temperature changes, and they normally are replaced after eight months. The bearings were lubricated by a molybdenum sulfide paste. Judging by their structure the needles probably consisted of ball bearing steel. They showed corroded initial cracks of the pitting type, i.e., shear-fatigue fractures due to excessive surface pressure. The needles too were overstressed by compression. It seemed that the higher pressure necessary for the pressing of thicker paper accelerated the corrosion, which lead to the crack initiations of the parts and possibly also to impaired lubrication. The machine manufacturer therefore switched to bearings with shells of a complex bronze.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001824
EISBN: 978-1-62708-241-9
... they are totally exposed to the severe environment comprising saline water, CO 2 , H 2 S, low pH, high temperature of 82 °C. The corrosion was severe, and pronounced metal loss took place. The bolts acted as an anode because of their lower content of alloying elements (austenitic stainless steel), and nuts have...
Abstract
Nineteen out of 26 bolts in a multistage water pump corroded and cracked after a short time in a severe working environment containing saline water, CO 2 , and H 2 S. The failed bolts and intact nuts were to be made from a special type of stainless steel as per ASTM A 193 B8S and A 194. However, the investigation (which included visual, macroscopic, metallographic, SEM, and chemical analysis) showed that austenitic stainless steel and a nickel-base alloy were used instead. The unspecified materials are more prone to corrosion, particularly galvanic corrosion, which proved to be the primary failure mechanism in the areas of the bolts directly exposed to the working environment. Corrosion damage on surfaces facing away from the work environment was caused primarily by chloride stress-corrosion cracking, aided by loose fitting threads. Thread gaps constitute a crevice where an aggressive chemistry is allowed to develop and attack local surfaces.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001051
EISBN: 978-1-62708-214-3
... for these nozzles was low-cycle corrosion fatigue. The cracks observed in this investigation were quite similar in appearance to feedwater cracks. Constant-extension-rate tests performed on A508 C12 steel, which is also used in pressure vessels, in oxygenated water at higher temperatures have demonstrated...
Abstract
A pair of steam generators operating at a pressurized water reactor site were found to be leaking near a closure weld. The generators were the vertical U-tube type, constructed from ASTM A302 grade B steel. The shell material exhibited high hardness values prior to confirmatory heat treatment, indicating high residual stresses in the area of the weld. All cracks were transgranular and were associated with pits on the inside surfaces of the vessels. It was concluded that the cracking was caused by a low-cycle corrosion fatigue phenomenon, with cracks initiating at areas of localized corrosion and propagating by fatigue. The cause of the pitting/cracking was related to the unit's copper species in solution.
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in Fatigue and Corrosion Fatigue Failure Surfaces of Concrete Reinforcement
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
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in “On-Load Corrosion” in Tubes of High Pressure Boilers
> ASM Failure Analysis Case Histories: Power Generating Equipment
Published: 01 June 2019
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Published: 01 January 2002
Fig. 4 Corrosion failure of 100-year-old riveted steel water transmission main. Courtesy of S. Paul, CorrTech, Inc.
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in Failures of Rolling-Element Bearings and Their Prevention
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 31 Bearings that were damaged by corrosive fluids. (a) Drawn cup for a needle-roller bearing damaged by vibration in the presence of dirt and moisture. Roller spacing is indicated by polished indentations. (b, c) Corrosion or water etch on bearing components resulting from a defective
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047332
EISBN: 978-1-62708-234-1
... areas representing graphitic residue and corrosion products that were not removed by erosion. Exposure of the pump bowl to the well water resulted in graphitic corrosion, which generated a soft, porous graphitic residue impregnated with insoluble corrosion products. Failure of the pump bowl resulted...
Abstract
Deterioration of the vanes and a wearing away of the area surrounding the mainshaft-bearing housing of the pump bowl for a submersible water pump used in a well field were noticed during a maintenance inspection. The bowl was sand cast from gray iron and had been in service approximately 45 months. Visual examination of the vanes and the area surrounding the mainshaft-bearing housing revealed a dark corrosion product that was soft, porous, and of low mechanical strength. There were areas with severe erosion. Macrographs of sections through the pump shell and a vane showed darker areas representing graphitic residue and corrosion products that were not removed by erosion. Exposure of the pump bowl to the well water resulted in graphitic corrosion, which generated a soft, porous graphitic residue impregnated with insoluble corrosion products. Failure of the pump bowl resulted from the continuous erosion of the residue by action of the water within the pump.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c0047328
EISBN: 978-1-62708-231-0
.... The part played by corrosion in the formation of the cracks was demonstrated with the help of metallographic techniques. The surface regions of the cracks widened into funnel form, which is a result of the corrosive influence of the cooling water. Actual corrosion pits could not be found indicating...
Abstract
Cracks formed on cylinder inserts from a water-cooled locomotive diesel engine, on the water side in the neck between the cylindrical part and the collar. Cracks were revealed by magnetic-particle inspection. As a rule, several parallel cracks had appeared, some of which were very fine. The part played by corrosion in the formation of the cracks was demonstrated with the help of metallographic techniques. The surface regions of the cracks widened into funnel form, which is a result of the corrosive influence of the cooling water. Actual corrosion pits could not be found indicating that the vibrational stresses had a greater share in the damage than the corrosive influence. Cracks appeared initially only in those engines in which no corrosion inhibitor had been added to the cooling water. The cracking was caused by corrosion fatigue. The combined presence of a corrosive medium and cyclical operating stress was needed to cause cracks. No cracks appeared when corrosion inhibitor was added to the cooling water.
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