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cold worked metal

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048289
EISBN: 978-1-62708-234-1
... ). There were no indications of a cold-worked structure in this area; hardness of the metal was 33 to 34 HRC. The microstructure and the lack of cold-worked metal indicated that a temperature above the transformation temperature of 727 °C (1340 °F) had been reached. Examination of the microstructure opposite...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001284
EISBN: 978-1-62708-215-0
... the presence of cold shuts at the same site in all specimens. It was recommended that all risers be thoroughly inspected and that the bow company work with their die casting shop to design a mold with acceptable filling characteristics. Selected Reference Selected Reference • Failures Related...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091533
EISBN: 978-1-62708-217-4
... with oxalic acid) supported the conclusion that the clamp fractured by SCC because the work metal was sensitized. Sensitization occurred during long-term exposure to the service temperature; the effects of sensitization were intensified as a result of cold forming. Recommendations included using a work metal...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0046242
EISBN: 978-1-62708-236-5
... teeth (found at visual inspection) was composed of the same material as the metal in the coupling. Beach marks and evidence of cold work, typical of fatigue failure, were found on the fracture surface. Chips remaining in the analysis cut were difficult to remove, indicating a strong magnetic field...
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003507
EISBN: 978-1-62708-180-1
... Abstract This article describes the general root causes of failure associated with wrought metals and metalworking. This includes a brief review of the discontinuities or imperfections that may be the common sources of failure-inducing defects in bulk working of wrought products. The article...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001581
EISBN: 978-1-62708-235-8
... Abstract A heavily worked 304 stainless steel wire basket recrystallized and distorted while in service at 650 deg C (1200 deg F). This case study demonstrates that heavily cold worked austenitic stainless steel components can experience large losses in creep strength, and potentially...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001345
EISBN: 978-1-62708-215-0
... deposits. Comparison of the microstructure and hardness of the swaged region and unswaged Grade TP 304 stainless steel tube metal indicated that the swaged section was not annealed to reduce the effects of cold working. The high hardness created during swaging increased the stainless steel's susceptibility...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001075
EISBN: 978-1-62708-214-3
... austenitic stainless steel, showing that the cold-worked condition has much lower fatigue strength if samples are notched. Source: Adapted from Ref 3 . Fig. 9 Fatigue curves for notched and unnotched type 302 austenitic steel in the annealed condition. No notch sensitivity is apparent...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001348
EISBN: 978-1-62708-215-0
... Fig. 6 Variation in hardness with cold work in a solution-annealed sample from the dished end Fig. 5 Hardness profile across the weldment on the inner surface of the tank. (a) and on the outer surface (b) Fig. 1 Schematic of the helium storage tank. The areas where samples were...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001724
EISBN: 978-1-62708-234-1
... “hoop” load when in operation, arising from a combination of stresses which will be discussed later, so it is very desirable that the rather soft and yielding austenitic steel be hardened and strengthened — and this can be done only by cold working (actually, warm working). For such a large ring...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048399
EISBN: 978-1-62708-226-6
... boundaries were seen in one of the pins and hence the fracture was revealed to have occurred along the grain boundaries. The other pin made from cold-worked cobalt-chromium alloy was observed to have randomly lines of primary inclusions. Intermingled dimples and fatigue striations were exhibited...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046414
EISBN: 978-1-62708-234-1
.... Micrographs of sections through the damaged surfaces showed a layer of distorted metal grains ( Fig. 1b ). At higher magnification, slip lines were visible, indicating that severe cold work had occurred at the surface. There was no evidence of intergranular attack or dezincification. The clean, pockmarked...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001360
EISBN: 978-1-62708-215-0
.../Fractography Discussion Conclusion and Recommendations Most Probable Cause Remedial Action Mechanical Properties Hardness Metallography Microstructural Analysis Microstructural analysis was difficult because of the highly cold worked condition of the blade. Basically...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001395
EISBN: 978-1-62708-220-4
... Measurements The hardness at various points across the weld, was measured and the results are depicted in Fig. 7 . It was ascertained that the head had been formed by cold spinning and the heavy work hardening thereby introduced had not been relieved by subsequent heat treatment. The shell hardness...
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001097
EISBN: 978-1-62708-214-3
... and that the fatigue cracking originated at corrosion pits. Hardness while below specification, still indicated that the screws were in the cold-worked condition and notch sensitive during fatigue loading. Use of a steel with a higher molybdenum content (317L) in the annealed condition was recommended. Selected...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001401
EISBN: 978-1-62708-220-4
..., confirming that the material had been cold-worked. In order to verify that the composition of the material conformed to that specified, a spectrographic analysis was carried out, the results being as follows: It will be noted that all three steels were of similar composition, being of the 18 8...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001805
EISBN: 978-1-62708-241-9
... Fig. 14 SEM image of the fracture surface near the middle of the spindle Fig. 15 Metallographic image of the microstructure around the nonfractured corner of the subject failed spindle (opposite the fracture origin). The elongated grains indicate significant cold work Fig. 16...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001186
EISBN: 978-1-62708-234-1
... Welded joints Wire Cold-drawn steel Ductile fracture A steel wire of 2.3 mm diameter broke during cable twisting. The fracture occurred obliquely to the longitudinal axis of the wire and showed a constriction at the end. Therefore it was a ductile fracture. File mark type work defects were...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001440
EISBN: 978-1-62708-235-8
... was heated to 550°C for a similar period, and its hardness dropped to 112–114. These tests showed that: ( a ) the end plate was in a cold worked condition; ( b ) the vessel had not been stress-relieved after fabrication; and ( c ) the area in the region of the crack did not attain a temperature as high...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001677
EISBN: 978-1-62708-222-8
... Geller in the early 1970's. Some documented work on the effect of metal and fracture was subsequently published in the Geller Papers [ 1 ]. The scientific evidence put forth in the form of light optical and electron micrographs were totally inconclusive, with wrong interpretations and poor quality...