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casting alloys
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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001753
EISBN: 978-1-62708-241-9
...-cast alloy, AA 712.0. Metallographic evaluation via optical microscopy and scanning electron microscopy revealed a high degree of porosity in the microstructure as well as the presence of deleterious intermetallic compounds within interdendritic regions. Macrohardness testing produced hardness values...
Abstract
A failure analysis investigation was conducted on a fractured aluminum tailwheel fork which failed moments after the landing of a privately owned, 1955 twin-engine airplane. Nondestructive evaluation via dye-penetrant inspection revealed no discernible surface cracks. The chemical composition of the sand-cast component was identified via optical emission spectroscopy and is comparable to an aluminum sand-cast alloy, AA 712.0. Metallographic evaluation via optical microscopy and scanning electron microscopy revealed a high degree of porosity in the microstructure as well as the presence of deleterious intermetallic compounds within interdendritic regions. Macrohardness testing produced hardness values which are noticeably higher than standard hardness values for 712.0. The primary fracture surfaces indicate evidence of mixed-mode fracture, via intergranular cracking, cleaved intermetallic particles, and dimpled cellular regions in the matrix. The secondary fracture surface demonstrates similar features of intergranular fracture.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048620
EISBN: 978-1-62708-225-9
.... Fasteners Intergranular corrosion Zinc-aluminum die casting alloy Stress-corrosion cracking The two nuts shown in Fig. 1(a) and (b) were used to secure the water-supply pipes to the threaded connections on hot-water and cold-water taps. The nut used on the cold-water tap ( Fig. 1a ) fractured...
Abstract
Two nuts were used to secure the water-supply pipes to the threaded connections on hot-water and cold-water taps. The nut used on the cold-water tap fractured about one week after installation. Examination of the fracture surfaces of the coldwater nut did not reveal any obvious defects to account for the fracture, but there were indications of excessive porosity in the nut. The fracture had occurred through the root of the first thread that was adjacent to the flange of the tap. It was found that the nut from the cold-water tap failed by SCC. Apparently, sufficient stress was developed in the nut to promote this type of failure by normal installation because there was no evidence of excessive tightening of the nut. Corrosion testing of the nuts indicated that the fractured nut was highly susceptible to intergranular corrosion because of either a deficiency in magnesium content or excessive impurities, such as lead, tin, or cadmium. This composition problem with zinc alloys was recognized many years ago, and particular attention has been directed toward ensuring that high-purity zinc is used. This corrective measure reportedly resulted in virtual elimination of this type of defect.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001908
EISBN: 978-1-62708-235-8
...: Rockeye Cluster Bomb tailcone assemblies Manufacturing defects: Casting heat checks, inclusions, porosity, shrinkage Background ARL conducted an analysis of two semicircular aluminum die-castings (Alloy A356) that are components of the tailcone assembly of the Rockeye Cluster Bomb. As the name...
Abstract
Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.
Book Chapter
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003508
EISBN: 978-1-62708-180-1
... iron, gray cast iron, malleable irons, ductile iron, low-alloy steel castings, austenitic steels, corrosion-resistant castings, and cast aluminum alloys are the materials discussed. The article describes the general types of discontinuities or imperfections for traditional casting with sand molds...
Abstract
This article focuses on the general root causes of failure attributed to the casting process, casting material, and design with examples. The casting processes discussed include gravity die casting, pressure die casting, semisolid casting, squeeze casting, and centrifugal casting. Cast iron, gray cast iron, malleable irons, ductile iron, low-alloy steel castings, austenitic steels, corrosion-resistant castings, and cast aluminum alloys are the materials discussed. The article describes the general types of discontinuities or imperfections for traditional casting with sand molds. It presents the international classification of common casting defects in a tabular form.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001224
EISBN: 978-1-62708-232-7
... in volume which puts the steel under stress 1 . The fractures of the finned tubes were both coarse- and fine-grained and undistorted which is not uncommon for this casting alloy ( Fig. 1 ). For the metallographic investigation, in which was also included an unused recuperator for purposes of comparison...
Abstract
A recuperator for blast heating of a cupola furnace became unserviceable because of the brittle fracture of several finned tubes made of heat resistant cast steel containing 1.4C, 2.3Si and 28Cr. The service temperature was reported as 850 deg C. This led to the suspicion that the fracturing had something to do with the precipitation of sigma phase. Metallographic examination showed that the multiaxial stresses caused by sigma phase formation and the related embrittlement was the cause for the fracture of the recuperator. A steel of lower chromium content with no or little tendency for sigma phase formation would have had adequate corrosion resistance at the relatively low service temperature.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0047220
EISBN: 978-1-62708-220-4
... of heavy sections can also be helpful. Stress relief can diminish internal stresses if the cast alloy is amenable to such treatment. Selected References Selected References • Failures Related to Casting , Failure Analysis and Prevention , Vol 11 , ASM Handbook , ASM International , 2002 , p...
Abstract
Two oil-pump gears broke after four months of service in a gas compressor that operated at 1000 rpm and provided a discharge pressure of 7240 kPa (1050 psi). The compressor ran intermittently with sudden starts and stops. The large gear was sand cast from class 40 gray iron with a tensile strength of 290 MPa (42 ksi) at 207 HRB. The smaller gear was sand cast from ASTM A536, grade 100-70-03, ductile iron with a tensile strength of 696 MPa (101 ksi) at 241 HRB. Analysis (metallographic examination) supported the conclusion that excessive beam loading and a lack of ductility in the gray iron gear teeth were the primary causes of fracture. During subsequent rotation, fragments of gray iron damaged the mating ductile iron gear. Recommendations included replacing the large gear material with ASTM A536, grade 100-70-03, ductile iron normalized at 925 deg C (1700 deg F), air cooled, reheated to 870 deg C (1600 deg F), and oil quenched. The larger gear should be tempered to 200 to 240 HRB, and the smaller gear to 240 to 280 HRB.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006831
EISBN: 978-1-62708-329-4
... the intended function is decreased. The article addresses factors that may cause failures in castings for each metal type, starting with gray iron and progressing to ductile iron, steel, aluminum, and copper-base alloys. It describes the general root causes of failure attributed to the casting material...
Abstract
The information provided in this article is intended for those individuals who want to determine why a casting component failed to perform its intended purpose. It is also intended to provide insights for potential casting applications so that the likelihood of failure to perform the intended function is decreased. The article addresses factors that may cause failures in castings for each metal type, starting with gray iron and progressing to ductile iron, steel, aluminum, and copper-base alloys. It describes the general root causes of failure attributed to the casting material, production method, and/or design. The article also addresses conditions related to the casting process but not specific to any metal group, including misruns, pour shorts, broken cores, and foundry expertise. The discussion in each casting metal group includes factors concerning defects that can occur specific to the metal group and progress from melting to solidification, casting processing, and finally how the removal of the mold material can affect performance.
Image
in Failure of a Cast Chain Link
> ASM Failure Analysis Case Histories: Construction, Mining, and Agricultural Equipment
Published: 01 June 2019
Fig. 1 Fracture surface of cast 10-cm (4-in.) high-strength low-alloy steel chain link that failed because of internal hydrogen-assisted cracking. Note hydrogen flake. 0.25×
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Image
in Brittle Fracture of a Roadarm Weldment of Two Steel Castings Because of Excessive Carbon-Equivalent Content
> ASM Failure Analysis Case Histories: Construction, Mining, and Agricultural Equipment
Published: 01 June 2019
Fig. 1 Section through weld in a roadarm (a weldment of low-alloy steel castings). The roadarm fractured in the HAZ because of high carbon-equivalent content. Fracture surface is at arrow. 0.8×
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Image
in Fracture of Cast Steel Equalizer Beams
> ASM Failure Analysis Case Histories: Automobiles and Trucks
Published: 01 June 2019
Fig. 1 Highway-truck equalizer beam, sand cast from low-alloy steel, that fractured because of mechanical cracking. (a) Fracture surface; detail A shows increments (regions B, C, D, and E) in which crack propagation occurred sequentially. Dimensions given in inches. (b) Micrograph
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Image
in Retrieved Bone Screw Made From Co-Cr-Mo Alloy with Casting Defects
> ASM Failure Analysis Case Histories: Medical and Biomedical Devices
Published: 01 June 2019
Fig. 1 Retrieved screw of cast Co-Cr-Mo alloy (type ASTM F75). (a) Defective screw threads from casting deficiencies. (b) Longitudinal section through threads showing porosity. 15×. (c) Enlarged thread of section shown in (b) with gas holes, segregation of primary phases, and dissolved oxides
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Image
in Tensile Fracture That Originated at Shrinkage Porosity in a Cast Low-Alloy Steel Connector
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
Fig. 1 Sand-cast low-alloy steel eye connector from a floating-bridge pontoon that broke under static tensile loading. (a) Schematic illustration of pontoon bridge and enlarged view of eye and clevis connectors showing location of fracture in eye connector. (b) A fracture surface of the eye
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Image
in Stress-Corrosion Cracking of a Die-Cast Zinc Alloy Nut
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Die-cast zinc alloy nuts from a water tap. (a) Nut for the cold-water tap that failed by SCC. (b) Mating nut for the hot-water top that shows only isolated areas of corrosion. (c) Unetched section showing metal in the cold-water tap after corrosion testing. 600×
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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001760
EISBN: 978-1-62708-241-9
... be prevented by eliminating the bolt hole, using a different type of bolt, or adjusting the fastening torque. References References 1. Aluminium and Aluminium Alloys - Castings - Chemical Composition and Mechanical Properties , Standard No. DIN-EN-1706( 1998 ) 2. AlSi9Cu3 Aluminum Alloy...
Abstract
This article presents a failure analysis of an aluminum cylinder head on an automotive engine. During an endurance test, a crack initiated from the interior wall of a hole in the center of the cylinder head, then propagated through the entire thickness of the component. Metallurgical examination of the crack origin revealed that casting pores played a role in initiating the crack. Stress components, identified by finite element analysis, also played a role, particularly the stresses imposed by the bolt assembly leading to plastic strain. It was concluded that the failure can be prevented by eliminating the bolt hole, using a different type of bolt, or adjusting the fastening torque.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001681
EISBN: 978-1-62708-234-1
... Abstract A microstructural analysis has been made of a burner nozzle removed from service in a coal gasification plant. The nozzle was a casting of a Co-29wt%Cr-19wt%Fe alloy. Extensive hot corrosion had occurred on the surface. There was penetration along grain boundaries, and corrosion...
Abstract
A microstructural analysis has been made of a burner nozzle removed from service in a coal gasification plant. The nozzle was a casting of a Co-29wt%Cr-19wt%Fe alloy. Extensive hot corrosion had occurred on the surface. There was penetration along grain boundaries, and corrosion products in these regions were particularly rich in S, and also contained Al, Si, O, and Cl. The grain boundaries contained Cr-rich particles which were probably Cr23-C6 type carbides. In the matrix, corrosion occurred between the Widmanstatten plates. Particles were found between these plates, most of which were rich in Cr and O, and probably were Cr2-O3 oxides. Other matrix particles were found which were rich in Al, O, and S. The corrosion was related to these grain boundary and matrix particles, which either produced a Cr-depleted zone around them or were themselves attacked.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0090971
EISBN: 978-1-62708-222-8
... Abstract A die-cast zinc adapter used in a snowthrower failed catastrophically in a brittle overload manner. The component had a chemical composition similar to standard zinc alloy ZA-27 (UNS Z35840), although the iron content was much higher and the copper slightly lower. The mechanical...
Abstract
A die-cast zinc adapter used in a snowthrower failed catastrophically in a brittle overload manner. The component had a chemical composition similar to standard zinc alloy ZA-27 (UNS Z35840), although the iron content was much higher and the copper slightly lower. The mechanical properties and alloy designation were not specified. Investigation (visual inspection, 187x SEM images, unetched 30x images, hardness testing, and chemical analysis) of both the failed adapter and an exemplar casting from known-good lot supported the conclusion that the casting failed as a result of brittle overload fracture due to excessive iron-zinc phase and gross porosity. These conditions acted synergistically to reduce the strength of the material. The composition was nonstandard, and the inherent brittleness suggested that it was unlikely that this material was an intentional proprietary alloy. No recommendations were made.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.9781627083294
EISBN: 978-1-62708-329-4
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046737
EISBN: 978-1-62708-229-7
... Abstract After 14 months of service, cracks were discovered in castings and bolts used to fasten together braces, posts, and other structural members of a cooling tower, where they were subjected to externally applied stresses. The castings were made of copper alloys C86200 and C86300...
Abstract
After 14 months of service, cracks were discovered in castings and bolts used to fasten together braces, posts, and other structural members of a cooling tower, where they were subjected to externally applied stresses. The castings were made of copper alloys C86200 and C86300 (manganese bronze). The bolts and nuts were made of copper alloy C46400 (naval brass, uninhibited). The water that was circulated through the tower had high concentrations of oxygen, carbon dioxide, and chloramines. Analysis (visual inspection, bend tests, fractographs, 50x unetched micrographs, 100x micrographs etched with H4OH, and 500x micrographs) supported the conclusions that the castings and bolts failed by SCC caused by the combined effects of dezincification damage and applied stresses. Recommendations included replacing the castings with copper alloy C87200 (cast silicon bronze) castings. Replacement bolts and nuts should be made from copper alloy C65100 or C65500 (wrought silicon bronze).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001638
EISBN: 978-1-62708-228-0
... used successfully in this application worldwide. During the 1960s, numerous failures of HK, HT, and HU cast headers and transfer lines were experienced. This was mainly due to lack of ductility of the cast alloys with an accompanying lack of resistance to thermal shock. Wrought Incoloy 800H, while...
Abstract
An Incoloy 800H (UNS N08810) transfer line on the outlet of an ethane-cracking furnace failed during decoking of the furnace tubes after nine years in service. A metallographic examination using optical and scanning electron microscopy as well as energy-dispersive x-ray spectroscopy revealed that the failure was due to sulfidation. The source of the sulfur in the furnace effluent was either dimethyl disulfide, injected into the furnace feed to prevent coke formation and carburization of the furnace tubes, or contamination of the feed with sulfur bearing oil.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001712
EISBN: 978-1-62708-234-1
... or carbonitrides, however these effects were not quantified in the references cited. Moreover, no mention was found on the effect of nitridation on alloy density. Therefore, the experiment was designed to help determine the effects of major elements Ni, Cr, Co, and Fe in cast heat resistant alloys. Ten alloys...
Abstract
A failure analysis was conducted in late 1996 on two rolls that had been used in the production of iron and steel powder. The rolls had elongated over their length such that the roll trunnions had impacted with the furnace wall refractory. The result was distortion and bowing of the roll bodies which necessitated their removal from service. The initial analysis found large quantities of nitrogen had been absorbed by the roll shell. Further research indicated nitrogen pickup accounted for 3% volumetric growth for every 1% by weight nitrogen absorption. This expansion was sufficient to account for the dimensional change observed in the failed rolls. This paper details the failure analysis and resulting research it inspired. It also provides recommendations for cast material choice in highly nitriding atmospheres.
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