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Friedrich Karl Naumann, Ferdinand Spies
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Friedrich Karl Naumann, Ferdinand Spies
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Friedrich Karl Naumann, Ferdinand Spies
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Friedrich Karl Naumann, Ferdinand Spies
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Samuel J. Brown
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Alan A. Johnson, Joseph A. von Fraunhofer
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Christopher A. Walton, Benjamin E. Nesbit, Henrique M. Candia, Zachary A. Myers, Wilburn R. Whittington ...
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Book Chapter
Cracked Cast Iron Crankcases
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001197
EISBN: 978-1-62708-235-8
... Abstract The front wall of a cast iron crankcase cracked at the transition from the comparatively minor wall thickness to the thick bosses for the drilling of the bolt holes. Metallographic examination showed the case was aggravated by the fact that the casting had a ferritic basic structure...
Abstract
The front wall of a cast iron crankcase cracked at the transition from the comparatively minor wall thickness to the thick bosses for the drilling of the bolt holes. Metallographic examination showed the case was aggravated by the fact that the casting had a ferritic basic structure and the graphite in part showed a granular formation, so that strength of the material was low. In a second crankcase with the same crack formation the structure in the thick-wailed part was better. But it also showed granular graphite in the ferritic matrix in the thin-walled part between the dendrites of the primary solid solution precipitated in the residual melt. A third crankcase had fractures in two places, first at the frontal end wall and second at the thinnest point between two bore holes. In all three cases casting stresses caused by unfavorable construction and rapid cooling were responsible for the crack formation. A fourth crankcase had cracked in the bore-hole of the frontal face. In this case the cause of the fracture was the low strength of a region that was caused by a bad microstructure further weakened by the bore hole.
Book Chapter
Worn Cast Iron Pump Parts
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001226
EISBN: 978-1-62708-234-1
..., 2.49Si, 0.51Mn, 0.485P, and 0.112S. The iron was thus distinctly hypereutectic. The galling of the pump parts therefore was favored by an unsuitable structure caused by improper composition and fast cooling. Distortion by casting stresses may have been contributory or may have played the principal part...
Abstract
A slide and the two guideways of a pump had to be disassembled already during run-in time after approximately 20 h because they had galled completely, before the rated speed of 800 rpm was reached. Chemical analysis of the slide showed the following composition: 3.60C, 3.22Graphite, 2.49Si, 0.51Mn, 0.485P, and 0.112S. The iron was thus distinctly hypereutectic. The galling of the pump parts therefore was favored by an unsuitable structure caused by improper composition and fast cooling. Distortion by casting stresses may have been contributory or may have played the principal part. In order to prevent a repetition, the use of hypoeutectic or eutectic iron, slower cooling of the casting, inoculation of the melt with finely powdered ferrosilicon, and possibly rounding-off the edges or machining of the surfaces are recommended.
Book Chapter
Cracked Bearing Caps Made of Cast Iron
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001198
EISBN: 978-1-62708-221-1
... Abstract Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps...
Abstract
Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps consisted of graphite in pearlitic-ferritic matrix. Casting stresses did not play a decisive role because of the simple shape of the pieces that were without substantial cross sectional variations. Two factors exerted an unfavorable effect in addition to comparatively low strength. First, the operating stress was raised locally by the sharp-edged groove, and second, the fracture resistance of the cast iron was lowered at this critical point by the existence of a ferritic bright border. To avoid such damage in the future it was recommended to observe one or more of the following precautions: 1) Eliminate the grooves; 2) Remove the ferritic bright border; 3) Avoid undercooling in the mold and therefore the formation of granular graphite; 4) Inoculate with finely powdered ferrosilicon into the melt for the same purpose; and, 5) Anneal at lower temperature or eliminate subsequent treatment in consideration of the uncomplicated shape of the castings.
Book Chapter
Cracks in Cylinder Blocks and in Cast Iron Cylinder Head
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001200
EISBN: 978-1-62708-221-1
... Abstract During the operation of tractors with cantilevered body, the lateral wall of the hypoeutectic cast iron cylinder blocks cracked repeatedly. Three of the blocks were examined. The grain structure of the thick-walled part consisted of uniformly distributed graphite of medium flake size...
Abstract
During the operation of tractors with cantilevered body, the lateral wall of the hypoeutectic cast iron cylinder blocks cracked repeatedly. Three of the blocks were examined. The grain structure of the thick-walled part consisted of uniformly distributed graphite of medium flake size in a basic mass of pearlite with little ferrite. But the thin-walled part showed a structure of dendrites of precipitated primary solid solution grains with pearlitic-ferritic structure and a residual liquid phase with granular graphite in the ferritic matrix. The structure was formed by undercooling of the residual melt. In this case, it was promoted by fast cooling of the thin wall and had comparatively low strength. The fracture formation in the cylinder blocks was ascribed primarily to casting stresses. They could be alleviated by better filleting of the transition cross sections. The fracture was promoted by the formation of undercooled microstructure of low strength in the thin-walled part. Similar damage appeared in a cylinder head, in which case, the cracks were promoted by a supercooled structure.
Book Chapter
Failure of a Mold for Centrifugal Casting of Gray- and Ductile-Iron Pipe
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0089617
EISBN: 978-1-62708-232-7
... Abstract A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten...
Abstract
A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten metal, flowing through a trough, was poured into the mold beginning at the bell end and ending with the spigot end being poured last. After the pipe had cooled, it was pulled out from the bell end of the mold, and the procedure was repeated. Investigation supported the conclusion that failure of the mold surface was the result of localized overheating caused by splashing of molten metal on the bore surface near the spigot end. In addition, the mold-wash compound (a bentonite mixture) near the spigot end was too thin to provide the proper degree of insulation and to prevent molten metal from sticking to the bore surface. Recommendations included reducing the pouring temperatures of the molten metal and spraying a thicker insulating coating onto the mold surface.
Book Chapter
Failure of a Cast Iron Water Pipe due to Graphitic Corrosion
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
... Abstract A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall...
Abstract
A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall perforations and cracking along its axis. The perforations and the crack were at the 6 o'clock position. Investigation (visual inspection, radiography, unetched macrographs, and tensile testing) supported the conclusion that the failure occurred as result of years of exposure to ground water in the soil resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron or coated and lined steel pipe, generally not susceptible to graphitic corrosion, were suggested as suitable replacement materials, and cathodic protection was also considered as a possibility.
Book Chapter
Brittle Fracture of a Cast Iron Valve in Oleum and Sulfuric Acid Service
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001071
EISBN: 978-1-62708-214-3
... Abstract A gray cast iron (ASTM 247 type A) gate valve in an oleum and sulfuric acid piping loop at a chemical process plant fractured catastrophically after approximately 10 years of service. The valve was a 150 mm (6 in.) bolted flange type rated to conform to ANSI B16.1 for service at 1034...
Abstract
A gray cast iron (ASTM 247 type A) gate valve in an oleum and sulfuric acid piping loop at a chemical process plant fractured catastrophically after approximately 10 years of service. The valve was a 150 mm (6 in.) bolted flange type rated to conform to ANSI B16.1 for service at 1034 kPa (150 psi) and 120 deg C (250 deg F) maximum in 93 to 99% sulfuric acid. The fracture originated at stress-corrosion cracks that occurred in a high-stress transition region at the valve body-to-flange juncture. The mechanical properties of the failed valve were below those of the manufacturer's cited specification, and the wall thickness through which the fracture occurred exceeded the minimum 9.5 mm (38 in.) thickness cited by the manufacturer The valve flange had been unbolted and rebolted to a maintenanced piping coil immediately prior to failure. It was recommended that the flange-to-valve body juncture be redesigned to reduce stress levels. A method of maintenance and inspection in concert with a criterion for life prediction for this and other valves and components in the system was also recommended.
Book Chapter
Mechanical Failure of a Repair Welded Ferritic Malleable Cast Iron Spring Hanger
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001307
EISBN: 978-1-62708-215-0
... Abstract The right front spring hanger on a dual rear axle of the tractor of a tractor-trailer combination failed, causing the vehicle to roll-over. The hanger was made from malleable cast iron that had been heat treated to produce a decarburized surface layer and a pearlitic transition layer...
Abstract
The right front spring hanger on a dual rear axle of the tractor of a tractor-trailer combination failed, causing the vehicle to roll-over. The hanger was made from malleable cast iron that had been heat treated to produce a decarburized surface layer and a pearlitic transition layer. It had been repair welded after breaking into two pieces longitudinally in a prior incident, using cast iron as weld metal. The repair weld bead on both surfaces missed the fracture over 15 to 20% of their lengths. The incomplete repair weld and brittleness of the weld metal and heat-affected zones led to the failure.
Book Chapter
Shell and Head Cracking in Gray Cast Iron Paper Machine Dryer Rolls
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0048804
EISBN: 978-1-62708-230-3
... Abstract Several cases of failures in gray cast iron paper machine dryer rolls were evaluated. The rolls were found have ground outer cylindrical surfaces on which the paper web is dried. They were found to rotate about their longitudinal axes at speeds from 50 to 250 rpm while containing...
Abstract
Several cases of failures in gray cast iron paper machine dryer rolls were evaluated. The rolls were found have ground outer cylindrical surfaces on which the paper web is dried. They were found to rotate about their longitudinal axes at speeds from 50 to 250 rpm while containing saturated steam from 35 to 380 kPa. Failures were found to occur in the shell body, in a head near a hand hole or a manhole opening, or in a head near the journal-to-head interface. A cleavage fracture was revealed by scanning electron microscopy regardless of the driving stress for failure. Fracture surface were found to exhibit chevron marks typical of fatigue or raised points or tears pointing in the direction of the probable origin of failure. The characteristics of the thinwall cast iron structures like the variation in composition due to pouring from multiple ladles, variation in solidification rates, and variation in tensile strength to be noted during inspection were described.
Image
As-cast gray cast iron loaded in tension. It is common to find little or no...
Available to Purchase
in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 01 January 2002
Fig. 58 As-cast gray cast iron loaded in tension. It is common to find little or no macroscale information visible on the fracture surface of many casting alloys to indicate the fracture origin and direction of crack propagation. There are exceptions to this, including the nodular irons
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Image
As-cast gray cast iron loaded in tension. It is common to find little or no...
Available to Purchase
in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 58 As-cast gray cast iron loaded in tension. It is common to find little or no macroscale information visible on the fracture surface of many casting alloys to indicate the fracture origin and direction of crack propagation. Exceptions to this include nodular irons and some aluminum
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Book Chapter
Failure Analysis and Mechanical Performance Evaluation of a Cast Aluminum Hybrid-Iron Golf Club Hosel
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001781
EISBN: 978-1-62708-241-9
... Abstract A commercial hybrid-iron golf club fractured during normal use. The club fractured through its cast aluminum alloy hosel. Optical analysis revealed casting pores through 20% of the hosel thickness. Mechanical properties were determined from characterization results, then used...
Abstract
A commercial hybrid-iron golf club fractured during normal use. The club fractured through its cast aluminum alloy hosel. Optical analysis revealed casting pores through 20% of the hosel thickness. Mechanical properties were determined from characterization results, then used to construct a finite element model to analyze material performance under failure conditions. In addition, a full scale structural test was conducted to determine failure strength. It was concluded that the club failed not from ground impact but from a force reversal at the bottom of the downswing. Large moments generated during the downswing aggravated by manufacturing defects and stress concentration combined to create an overload condition.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047297
EISBN: 978-1-62708-235-8
... Abstract Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings...
Abstract
Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings was suspected. Metallurgical examination on two representative castings supported the conclusions that the cracks in these gray iron door closers that were present either before or during the heat treatment were attributed to a substandard microstructure of the wrong type of graphite combined with excessive ferrite. This anomalous structure is caused by shortcomings in the foundry practice of chemical composition, solidification, and inoculation control. Judging from the microstructure, the strength of the material was lower than desired for class 30 gray iron, and the suspected heat treatment further reduced the strength. Recommendations included that the chemistry and inoculation should be controlled to produce type A graphite structure. The chemistry control should aim for a carbon equivalent close to 4.3% to achieve adequate fluidity for thin sections and to alleviate gas defects.
Image
Cast iron suction bell, 455 mm (18 in.) in diameter, from a low-pressure ge...
Available to PurchasePublished: 01 January 2002
Fig. 12 Cast iron suction bell, 455 mm (18 in.) in diameter, from a low-pressure general service water pump that failed by cavitation erosion after about 5 years of service. Note the deeply pitted surface and the irregular shape of the erosion pattern, both of which are typical characteristics
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Image
Cast iron suction bell, 455 mm (18 in.) in diameter, from a low-pressure ge...
Available to PurchasePublished: 01 January 2002
Fig. 34 Cast iron suction bell, 455 mm (18 in.) in diameter, from a low-pressure general service water pump that failed by cavitation erosion after about 5 years of service. Note the deeply pitted surface and the irregular shape of the erosion pattern, both of which are typical characteristics
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Image
Failures of gray cast iron paper-roll driers. (a) Axial-shell failure. (b) ...
Available to PurchasePublished: 01 January 2002
Fig. 13 Failures of gray cast iron paper-roll driers. (a) Axial-shell failure. (b) Circumferential-shell failure
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Image
Both sides of a journal-to-head failure in a cast iron paper-roll dryer. (a...
Available to PurchasePublished: 01 January 2002
Fig. 14 Both sides of a journal-to-head failure in a cast iron paper-roll dryer. (a) Bottom of failed dryer. (b) The failed bolted-on head
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Image
Scanning electron micrograph of ductile cast iron graphite nodules and ferr...
Available to PurchasePublished: 01 January 2002
Fig. 8 Scanning electron micrograph of ductile cast iron graphite nodules and ferritic phase after corrosion tests. Note the loss of material at the interface of the nodule. 2000×. Source: Ref 11 , 12
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Image
Graphitic corrosion of a gray cast iron sewer pipe section removed from the...
Available to PurchasePublished: 01 January 2002
Fig. 41 Graphitic corrosion of a gray cast iron sewer pipe section removed from the mud bottom of a seawater bay. Graphitic corrosion on the outside diameter surface is apparent for approximately 25% of the wall thickness. Courtesy of S.R. Freeman, Millennium Metallurgy, Ltd.
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Image
A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corr...
Available to PurchasePublished: 01 January 2002
Fig. 42 A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corrosion. The pipe was part of a water supply to a fire protection system. The external surface was covered with soil and the inside surface in contact with water. The pipe had been experienced cracking and through
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