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bearing steel
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001645
EISBN: 978-1-62708-232-7
... Abstract An extensive metallurgical investigation was carried out on samples of a failed roller bearing from the support and tilting system of a basic oxygen furnace converter used in the steel melting shop of an integrated steel plant. The converter bearing was fabricated from low-carbon...
Abstract
An extensive metallurgical investigation was carried out on samples of a failed roller bearing from the support and tilting system of a basic oxygen furnace converter used in the steel melting shop of an integrated steel plant. The converter bearing was fabricated from low-carbon, carburizing grade steel and had failed in service within a year of fitting to a repaired shaft. Microscopic observations of both the broken roller and inner-race samples revealed subsurface cracking and preponderance of brittle oxide and other macroinclusions. Electron probe microanalysis studies confirmed that the brittle oxides that formed stringers were alumina, and the other macroinclusions were complex silicates. Both the alumina and silicate inclusions were deleterious to contact-fatigue properties. Microstructurally, the carburized regions of the broken roller and of inner-race samples contained high-carbon tempered martensite. Microhardness measurements revealed that. Although the core hardness of the roller and the inner-race samples were similar, the surface hardness of the roller was approximately 8.5 HRC units harder than that of the inner-race. SEM observations of the roller fracture surface revealed striations indicative of fatigue, and EDS analyses corroborated a high incidence of silicate inclusions at crack sites. The study suggests that the failure of the bearing occurred because the hardness difference between the roller bearing and the inner-race surfaces resulted in wear of the inner-race. The wear led to shaft misalignment and play during service. The misalignment, coupled with the presence of inclusions, caused fatigue failure of the roller bearing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001513
EISBN: 978-1-62708-232-7
... Abstract While in the stationary mode, capillary action at the contact line between roller and race in a steel rolling mill taper bearing caused a concentration of lubricant and moisture to occur. This lead to lines of corrosion pits at roller intervals. During subsequent operation...
Abstract
While in the stationary mode, capillary action at the contact line between roller and race in a steel rolling mill taper bearing caused a concentration of lubricant and moisture to occur. This lead to lines of corrosion pits at roller intervals. During subsequent operation, the individual corrosion pits acted as stress raisers and initiated coarse grain spalling. Due to a bending moment on the rotating element, this in turn initiated bending fatigue normal to the longitudinal axis, which propagated through to the bore of the inner ring. Stain marks were visible in the bore at a spacing corresponding to roller intervals where lubricant had flowed through the cracks from the race.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0091893
EISBN: 978-1-62708-218-1
... Abstract An automotive front-wheel outer angular-contact ball bearing generated considerable noise shortly after delivery of the vehicle. The inner and outer rings were made of seamless cold-drawn 52100 steel tubing, the balls were forged from 52100 steel, and the retainer was stamped from 1008...
Abstract
An automotive front-wheel outer angular-contact ball bearing generated considerable noise shortly after delivery of the vehicle. The inner and outer rings were made of seamless cold-drawn 52100 steel tubing, the balls were forged from 52100 steel, and the retainer was stamped from 1008 steel strip. The inner ring, outer ring, and balls were austenitized at 845 deg C (about 1550 deg F), oil quenched, and tempered to a hardness of 60 to 64 HRC. Investigation (visual inspection) supported the conclusion that failure was caused by fretting due to vibration of the stationary vehicle position without bearing rotation. Recommendations included improving methods of securing the vehicle during transportation to eliminate vibrations.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047939
EISBN: 978-1-62708-225-9
... Abstract Rough operation of the roller bearing mounted in an electric motor/gearbox assembly was observed. The bearing components made of low-alloy steel (4620 or 8620) and the cup, cone and rollers were carburized, hardened and tempered. The contact surfaces of these components (cup, cone...
Abstract
Rough operation of the roller bearing mounted in an electric motor/gearbox assembly was observed. The bearing components made of low-alloy steel (4620 or 8620) and the cup, cone and rollers were carburized, hardened and tempered. The contact surfaces of these components (cup, cone and roller) were revealed to be uniformly electrolytically etched by visual examination. The action similar to anodic etching was believed to have occurred as a result of stray currents in the electric motor (not properly grounded) and the presence of an electrolyte (moisture) between the cup and roller surfaces of the bearing. As a remedial action, the bearing was insulated for protection from stray currents by grounding of the motor and the moisture was kept out by sealing both bearings in the assembly.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046371
EISBN: 978-1-62708-234-1
... shown in Fig. 1 . The bearing had not seized, and there was no evidence of heat discoloration in the galled areas. Fig. 1 Evidence of galling, or adhesive wear, on the inner surface of a carburized 4720 steel inner cone of a roller bearing. Galling was confirmed by the use of electron probe x...
Abstract
When a roller-bearing assembly was removed from an aircraft for inspection after a short time in service, several areas of apparent galling were noticed around the inside surface of the inner cone of the bearing. These areas were roughly circular spots of built-up metal. The bearing had not seized, and there was no evidence of heat discoloration in the galled areas. The inner cone, made of modified 4720 steel and carburized for wear resistance, rode on an AISI type 630 (17-4 PH) stainless steel spacer. Consequently, it was desirable to determine whether the galled spots contained any stainless steel from the spacer. Other items for investigation were the nature of the bond between the galled spot and the inner cone and any evidence of overtempering or rehardening resulting from localized overheating. Analysis (visual inspection, electron probe x-ray microanalysis, microscopic examination, and hardness testing) supported the conclusions that galling had been caused by a combination of local overload and abnormal vibration of mating parts of the roller-bearing assembly. No recommendations were made.
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in Fatigue Cracking of a 1040 Steel Crankshaft Because of Excessive Segregation of Nonmetallic Inclusions
> ASM Failure Analysis Case Histories: Automobiles and Trucks
Published: 01 June 2019
Fig. 1 Forged 1040 steel main-bearing journal that failed in fatigue. Top: Section showing cracks originating at coarse sulfide inclusions. Dimensions given in inches. Bottom: Macrograph of a 5%-nital-etched section showing the segregated inclusions (dark areas). 4x
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in Corrosion-Fatigue Failure of a Bearing in a Marine Environment
> ASM Failure Analysis Case Histories: Offshore, Shipbuilding, and Marine Equipment
Published: 01 June 2019
Fig. 1 Plastic-lined stainless steel spherical bearing for a hydrofoil that failed by corrosion fatigue. (a) Construction of bearing and location of fractures. Dimensions given in inches. (b) Fracture surface showing multiple fatigue origins (arrows) at edge of bore and on the spherical
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in Bearing Failure Caused by Improper Heat Treatment of Outer-Ring Raceway
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Large-diameter 4140 steel radar-antenna bearing that failed because of improper heat treatment of outer-ring raceway. (a) Configuration and dimensions (given in inches). (b) Fractograph showing typical damage on outer-ring raceway. (c) Micrograph of section through metal in outer ring
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in Failure of a Low-Alloy Steel Bearing in an Electric Motor Because of Stray Electric Currents
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Low-alloy steel roller bearing from an improperly grounded electric motor that was pitted and etched by electrolytic action of stray electric currents in the presence of moisture.
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in Pitting Failure of Ball Bearings in an Electric Motor by Static Electrical Discharges
> ASM Failure Analysis Case Histories: Mechanical and Machine Components
Published: 01 June 2019
Fig. 1 Weld spots on contact surfaces of a type 440C stainless steel ball bearing. The spots are caused by static electrical discharges resulting from use of an electrically nonconductive grease. (a) and (b) Photographs of inner-raceway surface. 10 and 100×, respectively. (c) and (d) SEM
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in Failure of a Bearing for a Jet Engine Because of Misalignment Between the Bearing and a Shaft
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 1 52100 steel jet-engine ball bearing that failed because of overheating resulting from misalignment. (a) Photograph of bearing components showing fractured cage. (b) Enlarged view of cage showing damage caused by scoring, scuffing, and plastic deformation around ball pockets
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in Failures of Rolling-Element Bearings and Their Prevention
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 34 Low-alloy steel roller bearing from an improperly grounded electric motor that was pitted and etched by electrolytic action of stray electric currents in the presence of moisture
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in Failures of Rolling-Element Bearings and Their Prevention
> Analysis and Prevention of Component and Equipment Failures
Published: 30 August 2021
Fig. 67 An AISI 52100 (100Cr6 or WN 1.3505) steel jet-engine ball bearing failed due to overheating that resulted from misalignment. (a) Bearing components showing fractured cage. (b) Enlarged view of the cage showing damage (scoring, scuffing, plastic deformation of the ball pockets
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Published: 30 August 2021
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Published: 30 August 2021
Fig. 15 Plastic-lined stainless steel spherical bearing for a hydrofoil that failed by corrosion fatigue. (a) Construction of bearing and location of fractures. Dimensions given in inches. (b) Fracture surface showing multiple fatigue origins (arrows) at edge of bore and on the spherical
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001258
EISBN: 978-1-62708-235-8
... Abstract A drawing plant which processed steel wire of designation 105 Cr 2 for ball bearings had losses due to crack formation and wire breakage during drawing. To establish the reason for the breakage, seven fractures were submitted for investigation with contiguous wire segments on both...
Abstract
A drawing plant which processed steel wire of designation 105 Cr 2 for ball bearings had losses due to crack formation and wire breakage during drawing. To establish the reason for the breakage, seven fractures were submitted for investigation with contiguous wire segments on both sides of the fracture of 300 mm each. Missing in the lamellar surface structure, with the exception of the remnants of a coarse network, were the pre-eutectically precipitated carbides to be expected in this steel. Surrounding the ferritic region in the surface structure, a ring of lamellar pearlite is seen, which turns into the granular annealed structure towards the core. The described structural phenomena were noted in all of the seven fracture regions. Their intensity always decreased with increasing distance from the fracture. Surface decarburization caused the formation of lamellar pearlite during annealing. This investigation further revealed that the localized decarburization and pearlite formation was present already in the rolled wire in uneven distribution over the entire coil length.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001243
EISBN: 978-1-62708-225-9
... of environment because of constant temperature changes, and they normally are replaced after eight months. The bearings were lubricated by a molybdenum sulfide paste. Judging by their structure the needles probably consisted of ball bearing steel. They showed corroded initial cracks of the pitting type, i.e...
Abstract
A needle bearing from a filling and seating machine for milk cartons became unusable due to corrosion and fracture of a ring after only four weeks of operation of the machine in a Finnish milk packing plant. These bearings were subject to corrosion by water condensates in this type of environment because of constant temperature changes, and they normally are replaced after eight months. The bearings were lubricated by a molybdenum sulfide paste. Judging by their structure the needles probably consisted of ball bearing steel. They showed corroded initial cracks of the pitting type, i.e., shear-fatigue fractures due to excessive surface pressure. The needles too were overstressed by compression. It seemed that the higher pressure necessary for the pressing of thicker paper accelerated the corrosion, which lead to the crack initiations of the parts and possibly also to impaired lubrication. The machine manufacturer therefore switched to bearings with shells of a complex bronze.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001191
EISBN: 978-1-62708-225-9
... Abstract Inner rings of spherical roller bearings out of full hardening ball bearing steel 100 CrMn 6 (Fe-1C-1.5Cr-1.1Mn, Material No. 1.3520) failed in service. Due to the cracks, parts from the middle flange broke or the rings failed in radial direction completely. All the cracks and fracture...
Abstract
Inner rings of spherical roller bearings out of full hardening ball bearing steel 100 CrMn 6 (Fe-1C-1.5Cr-1.1Mn, Material No. 1.3520) failed in service. Due to the cracks, parts from the middle flange broke or the rings failed in radial direction completely. All the cracks and fracture originated from the middle flange. In all of the three rings one flank showed heavy wearing and scouring. The cracks started from the edge of this flank with the cylindrical mantle surface of the middle flange. The cracking resembled fatigue cracking. However, in a fine-grained hardened steel such as this, fracture faces due to stress-cracking and overload fracture look the same. Metallographic examination showed the failure of the rings was a result of repeated heating and rapid cooling of the surface due to the grinding of the bearings on one flank of the middle flange. The stress-cracks (grindcracks) spread in steps which finally led to the breaking off of parts from the middle flange and complete failure of the rings.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001831
EISBN: 978-1-62708-241-9
... elements, were made from GCr15 bearing steel. The bearing also included a machined brass (MA/C3) cage and was packed with molybdenum disulfide (MoS 2 ) lithium grease. Metallurgical structures and chemical compositions of the bearing’s matrix materials were inspected using a microscope and photoelectric...
Abstract
An air blower in an electric power plant failed unexpectedly when a roller bearing in the drive motor fractured along its outer ring. Both rings, as well as the 18 rolling elements, were made from GCr15 bearing steel. The bearing also included a machined brass (MA/C3) cage and was packed with molybdenum disulfide (MoS 2 ) lithium grease. Metallurgical structures and chemical compositions of the bearing’s matrix materials were inspected using a microscope and photoelectric direct reading spectrometer. SEM/EDS was used to examine the local morphology and composition of fracture and contact surfaces. Chemical and thermal properties of the bearing grease were also examined. The investigation revealed that the failure was caused by wear due to dry friction and impact, both of which worsened as a result of high-temperature degradation of the bearing grease. Fatigue cracks initiated in the corners of the outer ring and grew large enough for a fracture to occur.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003563
EISBN: 978-1-62708-180-1
...) Various types Method of testing for rolling contact fatigue of bearing steels Ref 26 (i) Multiple bearing testing apparatus Deep-groove ball bearing design; typically 3000 rpm; four bearings on a single center shaft; maximum contact stress, 2.9 GPa (420 ksi); accelerometers on the outer housing...
Abstract
A major cause of failure in components subjected to rolling or rolling/sliding contacts is contact fatigue. This article focuses on the rolling contact fatigue (RCF) performance and failure modes of overlay coatings such as those deposited by physical vapor deposition, chemical vapor deposition, and thermal spraying (TS). It provides a background to RCF in bearing steels in order to develop an understanding of failure modes in overlay coatings. The article describes the underpinning failure mechanisms of TiN and diamond-like carbon coatings. It presents an insight into the design considerations of coating-substrate material properties, coating thickness, and coating processes to combat RCF failure in TS coatings.
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