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in Fracture of a Lifting Fork Arm
> ASM Failure Analysis Case Histories: Material Handling Equipment
Published: 01 June 2019
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001811
EISBN: 978-1-62708-241-9
... to be homogenous and had no banded structure. However, x-ray diffraction analysis confirmed the presence of up to 6% retained austenite which likely caused the tube to buckle during the 910 °C heat treating procedure. tube buckling retained austenite bainitic steel distortion x-ray diffraction analysis...
Abstract
A deformed steel tube was received for failure analysis after buckling during a heat-treat operation. The tube was subjected to various metallurgical tests as well as nondestructive testing to confirm the presence of residual stresses. The microstructure of the tube was found to be homogenous and had no banded structure. However, x-ray diffraction analysis confirmed the presence of up to 6% retained austenite which likely caused the tube to buckle during the 910 °C heat treating procedure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0090959
EISBN: 978-1-62708-222-8
... Abstract Mower blades manufactured from grade 1566 high-manganese carbon steel failed a standard 90 deg test. The blades had been austempered and reportedly fractured in a brittle manner during testing. The austempering treatment was intended to produce a bainitic microstructure...
Abstract
Mower blades manufactured from grade 1566 high-manganese carbon steel failed a standard 90 deg test. The blades had been austempered and reportedly fractured in a brittle manner during testing. The austempering treatment was intended to produce a bainitic microstructure, but investigation (visual inspection, 2% nital etched 8.9x/196x images) showed that the typical core microstructure contained alternating bands of martensite and bainite. The conclusion was that the nonuniform microstructure was likely responsible for the atypical brittle behavior of the blades, and the observed structure suggests that the austempering heat treatment was performed too close to the nominal martensite start temperature. Recommendations included raising the austempering salt-bath temperature 56 deg C (100 deg F) to account for localized compositional variation.
Image
in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 01 January 2002
Fig. 31 Radial marks on tensile test specimen of Society of Automotive Engineers (SAE) 4150 steel isothermally transformed to bainite, quenched to room temperature, and then tempered. (a) Lower bainite, isothermally transformed at 300 °C (570 °F) for 1 h, tempered at 600 °C (1110 °F) for 48 h
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001159
EISBN: 978-1-62708-232-7
... coarse-grained and acicular, and the microstructure of the welding seam had become predominantly martensitic as a result of the mixing of the weld metal with the fused pipe material. The chrome steel pipe had become partially transformed to martensite or bainite at the transition to the weld. Thus...
Abstract
A recuperator used for preheating the combustion air for a rolling mill furnace failed after a relatively short service time because of leakage of the pipes in the colder part. The 6 % chrome steel pipes used for the warmer part connected by means of welding with austenitic electrodes to the unalloyed mild steel pipe of larger diam. Visual inspection showed corrosion and deep, trench-like erosion over the entire circumference of the seam on the side of the thicker mild steel pipe. Examination using the V2-A solution for picral etch showed the microstructure of the unalloyed pipe had become coarse-grained and acicular, and the microstructure of the welding seam had become predominantly martensitic as a result of the mixing of the weld metal with the fused pipe material. The chrome steel pipe had become partially transformed to martensite or bainite at the transition to the weld. Thus, the failure occurred due to typical contact corrosion wherein the alloyed welding seam represented the less noble electrode. The martensitic structure may have contributed to the failure as well. Due to the typical nature of the failure, no recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001196
EISBN: 978-1-62708-224-2
..., 200x micrographs, chemical analysis, and metallographic examination) supported the conclusion that the primary cause of the failure was the brittleness (lack of impact toughness) of the steel. The coarse bainitic microstructure was inadequate for the service application. The microstructure resulted...
Abstract
A forged alloy steel arm of a lifting fork with an approximate cross section of 150 x 240 mm (5.92 x 9.45 in.) fractured after only a short service life on a lift truck. The fracture surface had the appearance of a fracture originating from a surface crack. Analysis (visual inspection, 200x micrographs, chemical analysis, and metallographic examination) supported the conclusion that the primary cause of the failure was the brittleness (lack of impact toughness) of the steel. The coarse bainitic microstructure was inadequate for the service application. The microstructure resulted from either improper heat treatment or no heat treatment after the forging operation. The surface cracks in the lifting-fork arm acted as starter notches (stress raisers), assisting in the initiation of fracture. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047830
EISBN: 978-1-62708-235-8
... was identified around one of the folds and a fatigue crack initiated in the fold and propagated across the cheek. Properties representative of 4140 steel, quenched and tempered to a hardness of 20 to 22 HRC, were observed. Tempered bainite was revealed in the general microstructure. As a corrective measure...
Abstract
Textile-machine crankshafts forged from 4140 steel fractured transversely on one cheek during one to three years of service. The cause of failure for two forgings (one complete fractured forging and second a section that contained the shorter shaft fracture cheek) was determined. Indication of fatigue failure was revealed by visual examination of the fracture surfaces. Rough grooves from hot trimming of the flash were visible on the surface of the cheeks. The outer face of one cheek of the throw on the forging contained shallow surface folds. Slightly decarburized forged surface was identified around one of the folds and a fatigue crack initiated in the fold and propagated across the cheek. Properties representative of 4140 steel, quenched and tempered to a hardness of 20 to 22 HRC, were observed. Tempered bainite was revealed in the general microstructure. As a corrective measure, the forgings were normalized, hardened and tempered to 28 to 32 HRC before being machined to increase fatigue strength and extremely rough surfaces were removed by careful grinding.
Image
in Mechanisms and Appearances of Ductile and Brittle Fracture in Metals
> Failure Analysis and Prevention
Published: 15 January 2021
Fig. 31 Radial marks on tensile test specimen of SAE 4150 alloy steel isothermally transformed to bainite, quenched to room temperature, and tempered. (a) Lower bainite, isothermally transformed at 300 °C (570 °F) for 1 h, tempered at 600 °C (1110 °F) for 48 h. (b) Lower bainite, isothermally
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048289
EISBN: 978-1-62708-234-1
... Abstract The center portions of two adjacent low-carbon steel boiler tubes (made to ASME SA-192 specifications) ruptured during a start-up period after seven months in service. It was indicated by reports that there had been sufficient water in the boiler two hours before start-up...
Abstract
The center portions of two adjacent low-carbon steel boiler tubes (made to ASME SA-192 specifications) ruptured during a start-up period after seven months in service. It was indicated by reports that there had been sufficient water in the boiler two hours before start-up. The microstructure near the rupture edge was revealed by metallographic examination to consist of ferrite and acicular martensite or bainite. The microstructure and the observed lack of cold work indicated a temperature above the transformation temperature of 727 deg C had been reached. Swelling of the tubes was disclosed by the wall thickness and OD of the tubing. The tubes were concluded to have failed due to rapid overheating.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0048674
EISBN: 978-1-62708-222-8
... Abstract Fasteners, made in high-production progressive dies from 0.7 mm thick cold-rolled 1060 steel, were used to secure plastic fabric or webbing to the aluminum framework of outdoor furniture. It was found that approximately 30% of the fasteners cracked and fractured as they were compressed...
Abstract
Fasteners, made in high-production progressive dies from 0.7 mm thick cold-rolled 1060 steel, were used to secure plastic fabric or webbing to the aluminum framework of outdoor furniture. It was found that approximately 30% of the fasteners cracked and fractured as they were compressed to clamp onto the framework prior to springback. The heat treatment cycle of the fasteners consisted of austenitizing, quenching, tempering to obtain a tempered martensite microstructure, acid cleaning, zinc electroplating, coating with a clear dichromate and thereafter baking to remove the nascent hydrogen. It was revealed that fasteners treated in this manner were brittle due to hydrogen embrittlement as the baking process was found to not be able to remove all the nascent hydrogen which had induced during acid cleaning and electroplating. The heat treatment cycle was modified to produce a bainitic structure and the method of plating the fastener with zinc was changed from electroplating to a mechanical deposition process to thus avoid hydrogen embrittlement.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001787
EISBN: 978-1-62708-241-9
... with low shear resistance, which makes fatigue crack from straight to zigzag and propagates slowly. The lower bainite/martensite duplex phase microstructure is capable of improving the strength and toughness of the steel [ 15 ]. Bainite matrix can increase the impact and twist resistance. Once...
Abstract
A masonry type drill bit, designed for impact drilling in rock, fractured after a short time in service. Samples of the failed bit were analyzed using optical and scanning electron microscopy, quantitative metallography, and chemical analysis. The composition was found to be that of 18CrNi3Mo steel. Investigators also found evidence of inclusions and prior austenite grain size, although it was determined that neither played a role in the failure. Rather, according to test data, the failure occurred because of stress concentration (due to geometric discontinuities along the tooth profiles) and the cumulative effect of torque and force loading (the byproduct of continuous twisting and axial impact). Cracks readily initiate under these conditions then propagate quickly through what was found to be networks of tempered martensite, thus resulting in premature failure.
Image
Published: 01 January 2002
Fig. 26 Debonding at the interface of a carbide particle and the matrix in a bainitic 4150 steel. Loading direction indicated. Source: Ref 42
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Image
Published: 15 January 2021
Fig. 27 Debonding at the interface of a carbide particle and the matrix in a bainitic 4150 steel. Loading direction indicated. Source: Ref 18
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Image
Published: 01 January 2002
Fig. 86 Micrograph of AISI 4140 steel as quenched and tempered, showing bands of tempered martensite and tempered martensite/bainite. 50×; 2% nital etch. Source: Ref 27
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Image
in Elevated-Temperature Life Assessment for Turbine Components, Piping, and Tubing
> Failure Analysis and Prevention
Published: 01 January 2002
Fig. 34 Effect of ductility on life-fraction estimates. CrMoV (ductile) is a ferric microstructure with approximately 15% elongation (high ductility) under long-term service conditions. CrMoV (brittle) is a bainitic microstructure with 3.5% elongation (low ductility). 2 1 4 Cr-1Mo
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Image
Published: 01 January 2002
Fig. 7 Effect of hydrostatic pressure on the transformation kinetics of 50CV4 steel. B , bainite; F. P., ferrite-pearlite transformation; M s , martensite start temperature. Source: Ref 7
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Image
Published: 01 January 2002
Fig. 87 Micrograph of AISI 4140 steel as quenched and tempered. Microstructure shows banded martensite and tempered martensite/bainite. Subsurface cracking is illustrated. 100×; 2% nital etch. Source: Ref 27
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001711
EISBN: 978-1-62708-229-7
... of the original bainitic structure is apparent. On the other hand, around the outside of the pipe, globulization is clearly smaller and the bainitic structure remains, though partially globulized. For comparison, Figure 7 shows the structure of a new pipe, with hardness 234 HB. Fig. 5 X20CrMoV12-1 steel...
Abstract
Failures of 10Cr-Mo9-10 and X 20Cr-Mo-V12-1 superheated pipes during service in steam power generation plants are described. Through micrographic and fractographic analysis, creep and overheating were identified as the cause of failure. The Larson-Miller parameter is computed, as a function of oxidation thickness, temperature and time, confirming the creep failure diagnostic.
Image
Published: 01 January 2002
Fig. 36 (a) Central bursting during extruding of AISI 4615 alloy steel specimen was promoted by (b) the presence of bainite and martensite (arrows point to microcracks in the martensite) in the as-rolled stock. Specimen etched with 4% picral, followed by 2% nital
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Image
Published: 15 January 2021
Fig. 45 (a) Central bursting during extruding of AISI 4615 alloy steel specimen was promoted by (b) the presence of bainite and martensite (arrows point to microcracks in the martensite) in the as-rolled stock. Specimen etched with 4% picral, followed by 2% nital
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