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Published: 01 June 2019
Fig. 2 Coarse bainitic structure of steel in condition as received, etched with Nital. 200 × More
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001811
EISBN: 978-1-62708-241-9
... to be homogenous and had no banded structure. However, x-ray diffraction analysis confirmed the presence of up to 6% retained austenite which likely caused the tube to buckle during the 910 °C heat treating procedure. tube buckling retained austenite bainitic steel distortion x-ray diffraction analysis...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0090959
EISBN: 978-1-62708-222-8
... Abstract Mower blades manufactured from grade 1566 high-manganese carbon steel failed a standard 90 deg test. The blades had been austempered and reportedly fractured in a brittle manner during testing. The austempering treatment was intended to produce a bainitic microstructure...
Image
Published: 01 January 2002
Fig. 31 Radial marks on tensile test specimen of Society of Automotive Engineers (SAE) 4150 steel isothermally transformed to bainite, quenched to room temperature, and then tempered. (a) Lower bainite, isothermally transformed at 300 °C (570 °F) for 1 h, tempered at 600 °C (1110 °F) for 48 h More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001159
EISBN: 978-1-62708-232-7
... coarse-grained and acicular, and the microstructure of the welding seam had become predominantly martensitic as a result of the mixing of the weld metal with the fused pipe material. The chrome steel pipe had become partially transformed to martensite or bainite at the transition to the weld. Thus...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c9001196
EISBN: 978-1-62708-224-2
..., 200x micrographs, chemical analysis, and metallographic examination) supported the conclusion that the primary cause of the failure was the brittleness (lack of impact toughness) of the steel. The coarse bainitic microstructure was inadequate for the service application. The microstructure resulted...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047830
EISBN: 978-1-62708-235-8
... was identified around one of the folds and a fatigue crack initiated in the fold and propagated across the cheek. Properties representative of 4140 steel, quenched and tempered to a hardness of 20 to 22 HRC, were observed. Tempered bainite was revealed in the general microstructure. As a corrective measure...
Image
Published: 15 January 2021
Fig. 31 Radial marks on tensile test specimen of SAE 4150 alloy steel isothermally transformed to bainite, quenched to room temperature, and tempered. (a) Lower bainite, isothermally transformed at 300 °C (570 °F) for 1 h, tempered at 600 °C (1110 °F) for 48 h. (b) Lower bainite, isothermally More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0048289
EISBN: 978-1-62708-234-1
... Abstract The center portions of two adjacent low-carbon steel boiler tubes (made to ASME SA-192 specifications) ruptured during a start-up period after seven months in service. It was indicated by reports that there had been sufficient water in the boiler two hours before start-up...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c0048674
EISBN: 978-1-62708-222-8
... Abstract Fasteners, made in high-production progressive dies from 0.7 mm thick cold-rolled 1060 steel, were used to secure plastic fabric or webbing to the aluminum framework of outdoor furniture. It was found that approximately 30% of the fasteners cracked and fractured as they were compressed...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001787
EISBN: 978-1-62708-241-9
... with low shear resistance, which makes fatigue crack from straight to zigzag and propagates slowly. The lower bainite/martensite duplex phase microstructure is capable of improving the strength and toughness of the steel [ 15 ]. Bainite matrix can increase the impact and twist resistance. Once...
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Published: 01 January 2002
Fig. 26 Debonding at the interface of a carbide particle and the matrix in a bainitic 4150 steel. Loading direction indicated. Source: Ref 42 More
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Published: 15 January 2021
Fig. 27 Debonding at the interface of a carbide particle and the matrix in a bainitic 4150 steel. Loading direction indicated. Source: Ref 18 More
Image
Published: 01 January 2002
Fig. 86 Micrograph of AISI 4140 steel as quenched and tempered, showing bands of tempered martensite and tempered martensite/bainite. 50×; 2% nital etch. Source: Ref 27 More
Image
Published: 01 January 2002
Fig. 34 Effect of ductility on life-fraction estimates. CrMoV (ductile) is a ferric microstructure with approximately 15% elongation (high ductility) under long-term service conditions. CrMoV (brittle) is a bainitic microstructure with 3.5% elongation (low ductility). 2 1 4 Cr-1Mo More
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Published: 01 January 2002
Fig. 7 Effect of hydrostatic pressure on the transformation kinetics of 50CV4 steel. B , bainite; F. P., ferrite-pearlite transformation; M s , martensite start temperature. Source: Ref 7 More
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Published: 01 January 2002
Fig. 87 Micrograph of AISI 4140 steel as quenched and tempered. Microstructure shows banded martensite and tempered martensite/bainite. Subsurface cracking is illustrated. 100×; 2% nital etch. Source: Ref 27 More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001711
EISBN: 978-1-62708-229-7
... of the original bainitic structure is apparent. On the other hand, around the outside of the pipe, globulization is clearly smaller and the bainitic structure remains, though partially globulized. For comparison, Figure 7 shows the structure of a new pipe, with hardness 234 HB. Fig. 5 X20CrMoV12-1 steel...
Image
Published: 01 January 2002
Fig. 36 (a) Central bursting during extruding of AISI 4615 alloy steel specimen was promoted by (b) the presence of bainite and martensite (arrows point to microcracks in the martensite) in the as-rolled stock. Specimen etched with 4% picral, followed by 2% nital More
Image
Published: 15 January 2021
Fig. 45 (a) Central bursting during extruding of AISI 4615 alloy steel specimen was promoted by (b) the presence of bainite and martensite (arrows point to microcracks in the martensite) in the as-rolled stock. Specimen etched with 4% picral, followed by 2% nital More