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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091690
EISBN: 978-1-62708-234-1
.... One commonly used ferrule was 3.5 cm long by 7.5 cm in diam and was drawn from 0.5 mm (0.020 in.) thick strip. Investigation (visual inspection, metallographic examination, and a mercurous nitrate test, which is an accelerated test used to detect residual stress in copper and copper alloys) of both...
Abstract
A substantial number of copper alloy C27000 (yellow brass, 65Cu-35Zn) ferrules for electrical fuses cracked while in storage and while in service in paper mills and other chemical processing plants. The ferrules, made by three different manufacturers, were of several sizes. One commonly used ferrule was 3.5 cm long by 7.5 cm in diam and was drawn from 0.5 mm (0.020 in.) thick strip. Investigation (visual inspection, metallographic examination, and a mercurous nitrate test, which is an accelerated test used to detect residual stress in copper and copper alloys) of both ferrules from fuses in service and storage in different types of plants, and ferrules from newly manufactured fuses, supported the conclusion that the ferrules failed by SCC resulting from residual stresses induced during forming and the ambient atmospheres in the chemical plants. The atmosphere in the paper mills was the most detrimental, and the higher incidence of cracking of ferrules there was apparently related to a higher concentration of ammonia in conjunction with high humidity. Recommendations included specifying that the fuses meet the requirements of ASTM B 154.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091669
EISBN: 978-1-62708-227-3
...Abstract Abstract During a routine inspection, cracks were discovered in several aluminum alloy (similar to either 2014 or 2017) coupling nuts on the fuel lines of a missile. The fuel lines had been exposed to a marine atmosphere for six months while the missile stood on an outdoor test stand...
Abstract
During a routine inspection, cracks were discovered in several aluminum alloy (similar to either 2014 or 2017) coupling nuts on the fuel lines of a missile. The fuel lines had been exposed to a marine atmosphere for six months while the missile stood on an outdoor test stand near the seacoast. A complete check was then made, both visually and with the aid of a low-power magnifying glass, of all coupling nuts of this type on the missile. Investigation (visual inspection, spectrographic and chemical analysis, and metallographic examination) supported the conclusion that the cracking of the aluminum alloy coupling nuts was caused by stress corrosion. Contributing factors included use of a material that is susceptible to this type of failure, sustained tensile stressing in the presence of a marine (chloride-bearing) atmosphere, and an elongated grain structure transverse to the direction of stress. The elongated grain structure transverse to the direction of stress was a consequence of following the generally used procedure of machining this type of nut from bar stock. Recommendations included changing the materials specification for new coupling nuts for this application to permit use of only aluminum alloys 6061-T6 and T651 and 2024-T6, T62, and T851.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001068
EISBN: 978-1-62708-214-3
... during the hydrostatic test. Testing Procedure and Results Surface Examination Visual The outside surfaces of each tank showed evidence of improper passivation. Atmospheric corrosion had occurred at a number of locations because of the aggressive coastal atmosphere.When the first tank...
Abstract
Four tanks made from type 304L stainless steel were removed from storage. Atmospheric corrosion on the outside of the tanks and pitting and crevice corrosion on the inside were visible. Metallographic examination revealed that the internal corrosion had been caused by crevices related to weld spatter and uneven weld deposit and by service water that had not been drained after hydrostatic testing. External corrosion was attributed to improper passivation. It was recommended that the surfaces be properly passivated and that, before storage, the interiors be rinsed with demineralized water and dried.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0048257
EISBN: 978-1-62708-217-4
...Abstract Abstract Evidence of destructive pitting on the gear teeth (AMS 6263 steel) in the area of the pitchline was exhibited by an idler gear for the generator drive of an aircraft engine following test-stand engine testing. The case hardness was investigated to be lower than specified...
Abstract
Evidence of destructive pitting on the gear teeth (AMS 6263 steel) in the area of the pitchline was exhibited by an idler gear for the generator drive of an aircraft engine following test-stand engine testing. The case hardness was investigated to be lower than specified and it was suggested that it had resulted from surface defects. A decarburized surface layer and subsurface oxidation in the vicinity of pitting were revealed by metallographic examination of the 2% nital etched gear tooth sample. It was concluded that pitting had resulted as a combination of both the defects. The causes for the defects were reported based on previous investigation of heat treatment facilities. Oxide layer was caused by inadequate purging of air before carburization while decarburization was attributed to defects in the copper plating applied to the gear for its protection during austenitizing in an exothermic atmosphere. It was recommended that steps be taken during heat treatment to ensure neither of the two occurred.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001389
EISBN: 978-1-62708-215-0
... to be a corrosion layer that resulted from exposure to ammonia in a humid atmosphere. Simulation tests confirmed that ammonia was the corrodent. The ammonia originated from the phenolic molding area of the plant. It was recommended that fumes from molding areas be vented outside the plant and that assembly, storage...
Abstract
During routine quality control testing, small circuit breakers exhibited high contact resistance and, in some cases, insulation of the contacts by a surface film. The contacts were made of silver-refractory (tungsten or molybdenum) alloys. Infrared analysis revealed the film to be a corrosion layer that resulted from exposure to ammonia in a humid atmosphere. Simulation tests confirmed that ammonia was the corrodent. The ammonia originated from the phenolic molding area of the plant. It was recommended that fumes from molding areas be vented outside the plant and that assembly, storage, and calibration areas be isolated from molding areas.
Image
Published: 01 January 2002
Fig. 44 Effect of presence of low concentration of arsenic, phosphorus, antimony, and silicon on time-to-fracture of copper by SCC under an applied tensile stress of 69 MPa (10 ksi) in a moist ammoniacal atmosphere. Composition of test atmosphere was 80% air, 16% ammonia, and 4% water vapor
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Image
Published: 01 January 2002
Fig. 45 Effect of presence of low-to-moderate concentrations of aluminum, nickel, tin, and zinc on time-to-fracture of copper by SCC under an applied tensile stress of 69 MPa (10 ksi) in a moist ammoniacal atmosphere. Composition of test atmosphere was 80% air, 16% ammonia, and 4% water vapor
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Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001046
EISBN: 978-1-62708-214-3
... of the same alloys, along with Inconel alloys 601, 617, and 690 and stainless steel type 347 was also conducted in a simulated waste incinerator nitrogen atmosphere containing 10% Co2, 9% O2, 4% HCl, 130 ppm HBr and 100 ppm SO2 at 595, 705, 815, and 925 deg C (1100, 1300,1500, and 1700 deg F). The tests...
Abstract
The thin plates within a type 309 stainless steel chlorinated solvent combustion preheater/heat exchanger designed to process fumes from a solvent coating process showed severe corrosion within 6 months of service. Within a year corrosion had produced holes in the plates, allowing gases to shunt across the preheater/exchanger. Metallographic examination of the plates showed that accelerated internal oxidation had been the cause of failure. Corrosion racks of candidate alloys (types 304, 309, and 316 stainless steels, Inconel 600, Inconel 625, Incoloy 800, Incoloy 825, and Inco alloy C-276) were placed directly in the hot gas stream, containing HCl and Cl2, for in situ testing. Results of this investigation showed that nickel-chromium corrosion-resistant alloys, such as Inconel 600, Inconel 625, and Inco alloy C-276, performed well in this environment. Laboratory testing of the same alloys, along with Inconel alloys 601, 617, and 690 and stainless steel type 347 was also conducted in a simulated waste incinerator nitrogen atmosphere containing 10% Co2, 9% O2, 4% HCl, 130 ppm HBr and 100 ppm SO2 at 595, 705, 815, and 925 deg C (1100, 1300,1500, and 1700 deg F). The tests confirmed the suitability of the nickel-chromium alloys for such an environment. Inconel 625 was selected for fabrication of a new preheater/exchanger.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047641
EISBN: 978-1-62708-235-8
...Abstract Abstract A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas...
Abstract
A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding for the exterior surface of the weld. A segmented backup ring with a gas channel was used inside the vessel to shield the weld root. The pressure vessel failed due to contamination of the fusion zone by oxygen, which resulted when the gas shielding the root face of the weld was diluted by air that leaked into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region of the segmented backup ring was provided, and a fine-mesh stainless steel screen diffuser was incorporated in the channel section of the backup ring to prevent air from leaking in. A titanium alloy color chart was furnished to permit correlation of weld-zone discoloration with the degree of atmospheric contamination.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001349
EISBN: 978-1-62708-215-0
... metal indicated severe sensitization in the HAZ due to high heat input during welding. An intergranular corrosion test confirmed the observations. The severe sensitization was coupled with residual stresses and exposure of the assembly to a coastal atmosphere during storage prior to installation...
Abstract
The dished ends of a heavy water/helium storage tank manufactured from 8 mm (0.3 in.) thick type 304 stainless plate leaked during hydrotesting. Repeated attempts at repair welding did not alleviate the problem. Examination of samples from one dished end revealed that the cracking was confined to the heat affected zone (HAZ) surrounding circumferential welds and, to a lesser extent, radial welds that were part of the original construction. Most of the cracks initiated and propagated from the inside surface of the dished ends. Microstructures of the base metal, HAZ, and weld metal indicated severe sensitization in the HAZ due to high heat input during welding. An intergranular corrosion test confirmed the observations. The severe sensitization was coupled with residual stresses and exposure of the assembly to a coastal atmosphere during storage prior to installation. This combination of factors resulted in failure by stress-corrosion cracking. Implementation of a new repair procedure was recommended. Repairs were successfully made using the new procedure, and all cracks in the weld repair zones were eliminated.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001319
EISBN: 978-1-62708-215-0
... marks were observed, indicating contamination by rusted carbon steel particles. Liquid penetrant testing was used to determine the extent of the cracks, and in situ metallographic analysis was performed over the cracked region. The morphology of the cracks was indicative of transgranular stress...
Abstract
Several type 304L stainless steel dished ends used in the fabrication of cylindrical vessels developed extensive cracking during storage. All of the dished ends had been procured from a single manufacturer and belonged to the same batch. When examined visually, several rust marks were observed, indicating contamination by rusted carbon steel particles. Liquid penetrant testing was used to determine the extent of the cracks, and in situ metallographic analysis was performed over the cracked region. The morphology of the cracks was indicative of transgranular stress-corrosion cracking (TGSCC). Conditions promoting the occurrence of the TGSCC included significant tensile stresses on the inside of the dished ends, the presence of surface contamination by iron due to poor handling practice using carbon steel implements, and storage in a coastal environment with an average temperature of 25 to 32 deg C (77 to 90 deg F), an average humidity ranging from 70 to 80%, and an atmospheric NaCl content ranging from 8 to 45 mg/m2 /day. Recommendations preventing further occurrence of the situation were strict avoidance of the use of carbon steel handling implements, strict avoidance of cleaning practices that cause long-term exposure to chlorine-containing cleaning fluid, and solution annealing of the dished ends at 1050 deg C (1920 deg F) for 1 h followed by water quenching to relieve residual stresses.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001377
EISBN: 978-1-62708-215-0
... for the admission of test atmospheres. Tests were conducted under static conditions, with bearing caps attached to the engine blocks by tightening the test bolts to specific torque values. The bolts were either dipped in a test fluid before tightening or subjected to a test atmosphere, introduced through...
Abstract
Sudden and unexplained bearing cap bolt fractures were experienced with reduced-shank design bolts fabricated from 42 CrMo 4 steel, quenched and tempered to a nominal hardness of 38 to 40 HRC. Fractographic analysis provided evidence favoring stress-corrosion cracking as the operating transgranular fracture failure mechanism. Water containing H7S was subsequently identified as the aggressive environment that precipitated the fractures in the presence of high tensile stress. This environment was generated by the chemical breakdown of the engine oil additive and moisture ingress into the normally sealed bearing cap chamber surrounding the bolt shank. A complete absence of fractures in bolts from one of the two vendors was attributed primarily to surface residual compressive stresses produced on the bolt shank by a finish machining operation after heat treatment. Shot cleaning, with fine cast shot, produced a surface residual compressive stress, which eliminated stress-corrosion fractures under severe laboratory conditions.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090181
EISBN: 978-1-62708-229-7
... structure in the matrix ( Fig. 5 ). Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere...
Abstract
Cracking in gas turbine blades was found to initiate from a mechanism of low-cycle fatigue (LCF). LCF is induced during thermal loading cycles in gas turbines. However, metallography of two cracked blades revealed a change in microstructure at as-cast surfaces for depths up to 0.41 mm (0.016 in.). Evaluation by SEM confirmed the difference in structure was associated with a lack of formation of coarse gamma prime structure in the matrix. Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere during the HIP process, resulting in the weakened structure. Because subsequent failures were found in blades that did not come from the suspect HIP lot, the scope of the problem was considered generic, and the conclusion was that the primary failure mechanism was LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001348
EISBN: 978-1-62708-215-0
...Abstract Abstract Two tanks made of AISI type 304 stainless steel exhibited cracking in the heat-affected zone (HAZ) of the weld that joined the dished end and the shell. The dished ends had been produced by cold deformation. Hardness measurement and simulation tests showed that the deformation...
Abstract
Two tanks made of AISI type 304 stainless steel exhibited cracking in the heat-affected zone (HAZ) of the weld that joined the dished end and the shell. The dished ends had been produced by cold deformation. Hardness measurement and simulation tests showed that the deformation was equivalent to a 30% reduction in thickness. Residual stresses were measured at about 135 MPa (20 ksi). The HAZ was found to be sensitized. The tanks had been stored in a coastal atmosphere for about 4 years before installation. The failure was attributed to intergranular stress-corrosion cracking in a sensitized HAZ due to chloride from the environment. Use of low-carbon type AISI 304L was recommended. Minimization of fit-up stresses and covering with polyethylene sheets during storage were also suggested.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001054
EISBN: 978-1-62708-214-3
... stress at the bond. The failures appeared to be predominantly located between the silver layer and the uranium substrate. Normal fracture location of specimens taken from similar components was at the silver/silver bond interface. Laboratory testing revealed that the uranium/silver joint was susceptible...
Abstract
Silver solid-state bonded components containing uranium failed under zero or low applied load several years after manufacture. The final operation in their manufacture was a proof loading that applied a sustained tensile stress to the bond, which all components passed. The components comprised circular cylinders fabricated by plating a thin layer of silver on each of the contact surfaces (uranium and stainless steel) and pressing the parts together at elevated temperature to solid-state bond the two silver surfaces. The manufacturing process produced a high level of residual stress at the bond. The failures appeared to be predominantly located between the silver layer and the uranium substrate. Normal fracture location of specimens taken from similar components was at the silver/silver bond interface. Laboratory testing revealed that the uranium/silver joint was susceptible to premature failure by stress-corrosion cracking under sustained loading if the atmosphere was saturated with water vapor.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001072
EISBN: 978-1-62708-214-3
... not extend to the outer diameter. The entire impeller surface was tested by the dry magnetic particle method. Visual and microstructural examinations revealed intergranular cracking. Energy-dispersive spectroscopy of corrosion products contained in the cracks disclosed the presence of chlorine and sulfur...
Abstract
Radial cracking occurred adjacent to 11 vanes in a 19-vane impeller operating in a chemical plant environment. The impeller vanes were fillet welded to both the disk and the cover Cracks were next to the fillet welds and near the cover outer diameter They generally did not extend to the outer diameter. The entire impeller surface was tested by the dry magnetic particle method. Visual and microstructural examinations revealed intergranular cracking. Energy-dispersive spectroscopy of corrosion products contained in the cracks disclosed the presence of chlorine and sulfur The failure was attributed to stress-corrosion cracking caused by a corrosive atmosphere.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0092148
EISBN: 978-1-62708-235-8
... carburized. The cylinder in which the spool fitted was made of 1117 steel, also gas carburized. Investigation (visual inspection, low magnification images, 400x images, metallographic exam, and hardness testing) supported the conclusion that momentary sliding contact between the spool and the cylinder wall...
Abstract
Occasional failures were experienced in spool-type valves used in a hydraulic system. When a valve would fail, the close-fitting rotary valve would seize, causing loss of flow control of the hydraulic oil. The rotating spool in the valve was made of 8620 steel and was gas carburized. The cylinder in which the spool fitted was made of 1117 steel, also gas carburized. Investigation (visual inspection, low magnification images, 400x images, metallographic exam, and hardness testing) supported the conclusion that momentary sliding contact between the spool and the cylinder wall caused unstable retained austenite in the failed cylinder to transform to martensite. The increase in volume resulted in sufficient size distortion to cause interference between the cylinder and the spool, seizing, and loss of flow control. The failed parts had been carburized in a process in which the carbon potential was too high, which resulted in a microstructure having excessive retained austenite after heat treatment. Recommendations included modifying the composition of the carburizing atmosphere to yield carburized parts that did not retain significant amounts of austenite when they were heat treated.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0047392
EISBN: 978-1-62708-221-1
...Abstract Abstract A roadarm for a tracked vehicle failed during preproduction vehicle testing. The arm was a weldment of two cored low-alloy steel sand castings specified to ASTM A 148, grade 120–95. A maximum carbon content of 0.32% was specified. The welding procedure called for degreasing...
Abstract
A roadarm for a tracked vehicle failed during preproduction vehicle testing. The arm was a weldment of two cored low-alloy steel sand castings specified to ASTM A 148, grade 120–95. A maximum carbon content of 0.32% was specified. The welding procedure called for degreasing and gas metal arc welding; neither preheating nor postheating was specified. The filler metal was E70S-6 continuous consumable wire with a copper coating to protect it from atmospheric oxidation while on the reel. Analysis of the two castings revealed that the carbon content was higher than specified, ranging from 0.40 to 0.44%. The fracture occurred in the HAZ , where quenching by the surrounding metal had produced a hardness of 55 HRC. Some roadarms of similar carbon content and welded by the same procedure had not failed because they had been tempered during a hot-straightening operation. Brittle fracture of the roadarm was caused by a combination of too high a carbon equivalent in the castings and the lack of preheating and postheating during the welding procedure. A pre-heat and tempering after welding were added to the welding procedure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046915
EISBN: 978-1-62708-232-7
... testing, and etched micrographs using Murakami's reagent) supported the conclusions that thinning of the pan walls at the surface of the molten lead resulted from using coke of high moisture content and from the low fluctuating coke level. Recommendations included reducing the supply of oxygen attacking...
Abstract
Severely reduced wall thickness was encountered at the liquid line of a lead-bath pan that was used in a continuous strip or wire oil-tempering unit. Replacement of the pan was necessary after six months of service. The pan, 6.9 m (22.5 ft) long, 0.6 m (2 ft) wide, and 38 cm (15 in.) deep with a 2.5-cm (1-in.) wall thickness, was a type 309 stainless steel weldment. Operating temperatures of the lead bath in the pan ranged from 805 deg C (1480 deg F) at the entry end to 845 deg C (1550 deg F) at the exit end. Analysis (visual inspection. metallographic analysis, moisture testing, and etched micrographs using Murakami's reagent) supported the conclusions that thinning of the pan walls at the surface of the molten lead resulted from using coke of high moisture content and from the low fluctuating coke level. Recommendations included reducing the supply of oxygen attacking the grain boundaries and the hydrogen that readily promoted decarburization with the use of dry (2 to 3% moisture content) coke. Maintaining a thick layer of coke over the entire surface of molten lead in the pan would exclude atmospheric oxygen from the grain boundaries.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001177
EISBN: 978-1-62708-234-1
...Abstract Abstract A solution containing 50 to 70% calcium chloride (pH 7.5 to 8.5) was concentrated by evaporation in a brick-lined vessel by passing steam at a pressure of 15 atmospheres through a system of heating coils made of austenitic stainless steel X 10 Cr-Ni-Mo-Ti 18 12 (Material...
Abstract
A solution containing 50 to 70% calcium chloride (pH 7.5 to 8.5) was concentrated by evaporation in a brick-lined vessel by passing steam at a pressure of 15 atmospheres through a system of heating coils made of austenitic stainless steel X 10 Cr-Ni-Mo-Ti 18 12 (Material No. 1.4573). After five months one of the coils, which consisted of tubes having a wall thickness of 3.4 mm, developed a leak. Tightly closed cracks were seen on the outer surface of the tube. Further tests with color penetration process revealed multiple branched cracks. Longitudinal section showed that the cracks had started from the outside surface of the tube. Electrolytic etching further showed that they had propagated mainly across the grains. It was concluded that this was a typical case of transcrystalline stress corrosion.