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aircraft bearings

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Image
Published: 01 June 2019
Fig. 1 Cracked type 440C stainless steel (a) aircraft wing flap hinge bearings. (b) Crack configuration of bearing 1 from (a). (c) Crack configuration of bearing 2 from (a). (d) Fracture surface of second crack in bearing 1. Arrow shows the probable fracture origin. 2.5x. (e) Fracture surface More
Image
Published: 01 January 2002
Fig. 21 Inner-ring raceway of an aircraft-transmission ball bearing that failed by rolling-contact fatigue because of subsurface nonmetallic inclusions. (a) Macrograph of inner-ring raceway showing fine-texture flaking damage (arrow A), coarse-texture flaking damage (arrow B), and origin More
Image
Published: 01 June 2019
Fig. 1 Inner-ring raceway of an aircraft-transmission ball bearing that failed by rolling-contact fatigue because of subsurface nonmetallic inclusions. (a) Macrograph of inner-ring raceway showing fine-texture flaking damage (arrow A), coarse-texture flaking damage (arrow B), and origin More
Image
Published: 30 August 2021
Fig. 56 Inner-ring raceway of an aircraft-transmission ball bearing that failed by rolling-contact fatigue because of subsurface nonmetallic inclusions. (a) Macrograph of inner-ring raceway showing fine-textured flaking damage (arrow A), coarse-textured flaking damage (arrow B), and origin More
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001755
EISBN: 978-1-62708-241-9
... of fatigue crack(s) in the inner race. When the crack reached the critical size, the collar of the race fractured, causing subsequent damage. The cage also failed due to excessive stresses in the axial direction, and its material was smeared on the steel balls and the outer race. aircraft bearings...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047975
EISBN: 978-1-62708-225-9
... Abstract An aircraft was grounded when illumination of the transmission oil-pressure light and an accompanying drop in pressure on the oil-pressure gage was reported by the pilot. No discrepancy in the bearing assemblies and related components was revealed by teardown analysis...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001754
EISBN: 978-1-62708-241-9
... to the discovery of overlooked debris in an engine chip detector, and thus resulted in a review of several maintenance practices. aircraft bearings operating overload inadequate maintenance and inspection M50 alloy steel bulk deformation energy dispersive spectrometry chemical composition AMS 6490...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047986
EISBN: 978-1-62708-217-4
... Abstract The engine on a jet aircraft was shut down immediately as it produced excessive vibration. Complete failure of the cage in one of the two main-shaft ball bearings (placed side by side in the engine) was revealed in the dismantled engine. The ball bearings (made of vacuum-melted 52100...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001019
EISBN: 978-1-62708-217-4
... Abstract A broken aircraft crankshaft and a severely damaged main brass bearing were examined to determine whether engine failure was initiated in the bearing or in the crankshaft. The steel crankshaft failure was a classical fatigue fracture. The bearing had been subjected to extremely high...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046371
EISBN: 978-1-62708-234-1
... Abstract When a roller-bearing assembly was removed from an aircraft for inspection after a short time in service, several areas of apparent galling were noticed around the inside surface of the inner cone of the bearing. These areas were roughly circular spots of built-up metal. The bearing...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001796
EISBN: 978-1-62708-241-9
... Abstract A tri-lobe cylindrical roller bearing was submitted for investigation to determine the cause of uniformly spaced axial fluting damages on its rollers and outer raceway surfaces. The rollers and raceways were made from premium-melted M50 and M50NiL, aircraft quality steels often used...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006448
EISBN: 978-1-62708-217-4
... by the laboratory for analysis ( Fig. 1a ). The bearings were fabricated from chromium-plated type 440C martensitic stainless steel. Fig. 1 Cracked type 440C stainless steel (a) aircraft wing flap hinge bearings. (b) Crack configuration of bearing 1 from (a). (c) Crack configuration of bearing 2 from (a). (d...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047059
EISBN: 978-1-62708-217-4
... Abstract The governor on an aircraft engine failed and upon disassembly of the unit, it was discovered that the retainer for the flyweight pivot pins was broken. The channel-shaped retainer was made of 0.8 mm (0.030 in.) thick 1018 or 1020 steel. The part was plated with copper, which acted...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047856
EISBN: 978-1-62708-217-4
... G43370 Fatigue fracture Routine inspection of a reciprocating aircraft engine revealed cracks in the master connecting rod. Cracks were observed in the channel-shaped section consisting of the knuckle-pin flanges and the bearing-bore wall. The rods were forged from 4337 (AMS 6412) steel and heat...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006409
EISBN: 978-1-62708-217-4
... Abstract Pitostatic system connectors were being found cracked on several aircraft. Two of the cracked connectors made of 2024-T351 aluminum alloy were submitted for failure analysis. The connectors had cut pipelike threads that were sealed with Teflon-type tape when installed. Longitudinal...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001145
EISBN: 978-1-62708-217-4
... configuration of the chamber and the stress distribution also have a bearing upon the failure modes. Several failures are reviewed to illustrate the problems. Aircraft components Breech chambers Electroless nickel plating Overheating 4340 UNS G43400 High-temperature corrosion and oxidation Stress...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046022
EISBN: 978-1-62708-217-4
... Abstract A forged aluminum alloy 2014-T6 catapult-hook attachment fitting (anodized by the chromic acid process to protect it from corrosion) from a naval aircraft broke in service. Spectrographic analysis, visual examination, microscopic examination, and tensile analysis showed minute cracks...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001296
EISBN: 978-1-62708-215-0
... Abstract A 52000 bearing steel valve guide component operating in the fuel supply system of a transport aircraft broke into two pieces after 26 h of flight. The valve guide fractured through a set of elongated holes that had been electrodischarge machined into the component. Analysis indicated...
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001812
EISBN: 978-1-62708-241-9
... Abstract Several cases of embrittlement failure are analyzed, including liquid-metal embrittlement (LME) of an aluminum alloy pipe in a natural gas plant, solid metal-induced embrittlement (SMIE) of a brass valve in an aircraft engine oil cooler, LME of a cadmium-plated steel screw from...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001694
EISBN: 978-1-62708-222-8
... Abstract The outer tube, or stem, on a bicycle frame fractured after two years of use. Detailed investigation revealed that the lower stem bearing had been loose for some time and the bottom bearing cup contained many cracks. Metallographic examination of the chromium-plated cup confirmed...