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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0046247
EISBN: 978-1-62708-235-8
... Abstract A double-flange trailer wheel, in service on a coke-oven pusher car for about five years, broke. Specifications called for rolled steel track wheels conforming to ASTM A 186 (since reclassified as A 504). Chemical analysis showed the metal in the wheel to be medium-carbon steel within...
Abstract
A double-flange trailer wheel, in service on a coke-oven pusher car for about five years, broke. Specifications called for rolled steel track wheels conforming to ASTM A 186 (since reclassified as A 504). Chemical analysis showed the metal in the wheel to be medium-carbon steel within the ranges given in ASTM A 186. Visual examination of the broken wheel revealed that cracks ran parallel with the base of the lower row of numbers stamped with heavy indentation on the web section. Microscopic examination showed the metal in the web, rim, and tread to be in the normalized condition. Evidence found supports the conclusions that fatigue failure of the wheel was the result of heavy stamp marks that acted as stress raisers in the weaker web section. Because this was a double-flange wheel, considerable side thrust was applied to the wheel, causing stress concentration at the web. Recommendations included following the ASTM specification A 504 regarding location of stamped identification numbers (marks identifying the wheels must be stamped on the back face of the rim not less than 3.2 mm from the inner edge of the rim).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001531
EISBN: 978-1-62708-231-0
..., and ductility are mainly determined by the carbon content of wheel steels. The fatigue crack growth resistance is insensitive to composition and microstructure, while the fatigue crack initiation life increases with the decrease of austenite grain size and pearlite colony size. The dynamic fracture toughness...
Abstract
In this study, the failure modes of cartwheel and mechanical properties of materials have been analyzed. The results show that rim cracking is always initiated from stringer-type alumina cluster and driven by a combination effect of mechanical and thermal load. The strength, toughness, and ductility are mainly determined by the carbon content of wheel steels. The fatigue crack growth resistance is insensitive to composition and microstructure, while the fatigue crack initiation life increases with the decrease of austenite grain size and pearlite colony size. The dynamic fracture toughness, KID, is obviously lower than static fracture toughness, KIC, and has the same trend as KIC. The ratio of KID/sigma YD is the most reasonable parameter to evaluate the fracture resistance of wheel steels with different composition and yield strength. Decreasing carbon content is beneficial to the performance of cartwheel.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006428
EISBN: 978-1-62708-217-4
... Abstract Four nose wheels fabricated from 2014-T6 aluminum alloy and cold worked at the flange were examined. Visual examination showed that the failure started in the tube well area on the wheel with serial number 31. The failure initiated in the flange fillet on wheels with serial numbers 67...
Abstract
Four nose wheels fabricated from 2014-T6 aluminum alloy and cold worked at the flange were examined. Visual examination showed that the failure started in the tube well area on the wheel with serial number 31. The failure initiated in the flange fillet on wheels with serial numbers 67, 217, and 250. Scanning electron microscopy (SEM) examination of the fractures showed that failure initiated by SCC or a corrosion pit on all failures examined. The failures then progressed by fatigue. Dye penetrant testing revealed no additional flaws on the wheels that had failed in the flange area. There was, however, one flaw area in the flange of the wheel that failed in the tube well. This flaw resembled a corrosion pit. It was concluded that failure of nose wheels 67, 217, and 250 was caused by cracking due to SCC or pitting. The failures progressed by fatigue. Because failure occurred in the same general area on all three wheels, these locations are suspect as being underdesigned. It was recommended that the nose wheel be redesigned and additional service data be accumulated to understand the contributing factors that resulted in wheel failure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0092103
EISBN: 978-1-62708-234-1
... Abstract A polyoxymethylene gear wheel that had been in operation in a boiler room failed. Investigation (visual inspection and 305x images) supported the conclusion that failure was due to postcrystallization causing considerable shrinkage. Breakdown along the crystalline superstructure...
Abstract
A polyoxymethylene gear wheel that had been in operation in a boiler room failed. Investigation (visual inspection and 305x images) supported the conclusion that failure was due to postcrystallization causing considerable shrinkage. Breakdown along the crystalline superstructure started mainly at the mechanically stressed tooth flanks. In addition, oil vapors, humidity, and other degradative agents could also have contributed to the observed failure. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001157
EISBN: 978-1-62708-218-1
... Abstract A suspension bushing separated from the disk on the rear wheel suspension of a racing vehicle while under operation on an express highway, causing the wheel to detach from the car. Visual inspection showed fresh turning grooves at four built-up fillet welds on the torus of the outside...
Abstract
A suspension bushing separated from the disk on the rear wheel suspension of a racing vehicle while under operation on an express highway, causing the wheel to detach from the car. Visual inspection showed fresh turning grooves at four built-up fillet welds on the torus of the outside of the disk. The welding heat and rapid cooling caused the base material of the disk – already with a martensitic structure – to harden throughout the torus, both of which caused cracking in the inner and outer fillets at the transition from bushing to disk. Visual inspection of the other rear wheel showed similar stress cracks in the hardened base material of the transition region as well as the same four welds. Rough finishing and the sharp-edged formation of the cross section transition may have also contributed to the failure. The results of the investigation suggested that machine shops neither execute nor permit repair-welds on highly stressed machine parts and especially vehicle components.
Image
Published: 01 January 2002
Fig. 8 Fitting for attaching dual wheels to a tractor axle that failed when 1045 steel U-bolts in the assembly were overstressed. The bolts failed because of poor hardenability relative to their diameter.
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Image
in Failure Analysis of Aircraft Landing Gear Components
> ASM Failure Analysis Case Histories: Air and Spacecraft
Published: 01 June 2019
Fig. 2 a: Fractured axle half attached to one of the wheels. b: Matching half, fracture started at the lock pin hole and propagated as indicated by the arrows. c: Fracture surface in the vicinity of a corrosion pit in the lock pin hole, the arrow points to the location of the fatigue crack
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Image
in Fatigue Fracture of 1045 Steel U-Bolts on a Tractor Fitting
> ASM Failure Analysis Case Histories: Construction, Mining, and Agricultural Equipment
Published: 01 June 2019
Fig. 1 Fitting for attaching dual wheels to a tractor axle that failed when 1045 steel U-bolts in the assembly were overstressed. The bolts failed because of poor hardenability relative to their diameter.
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Image
Published: 30 August 2021
Fig. 7 Fitting for attaching dual wheels to a tractor axle that failed when 1045 steel U-bolts in the assembly were overstressed. The bolts failed because of poor hardenability relative to their diameter.
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0048099
EISBN: 978-1-62708-235-8
... Abstract A bridge wheel on a crane, forged from 1055 steel, fractured after one year of service. The wheel fractured in the web between the hub and the rim. A small area containing beach marks that originated in a heavily burned area on the web surface was revealed by visual examination...
Abstract
A bridge wheel on a crane, forged from 1055 steel, fractured after one year of service. The wheel fractured in the web between the hub and the rim. A small area containing beach marks that originated in a heavily burned area on the web surface was revealed by visual examination of the fracture surface. Surface burning to a depth of approximately 0.8 mm was disclosed by metallographic examination of a section taken through the region that contained the beach marks. A forging defect was indicated by the degree of decarburization and oxide dispersion that were visible. The failure was concluded to have been caused by surface burning during the forging operation. As a preventive measure more closely controlled heating practice during forging to eliminate surface burning was recommended. The burnt region was suggested to be removed in case burning occurs.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0048586
EISBN: 978-1-62708-218-1
... Abstract Each of the ten studs on one wheel of a semitrailer used to haul coal broke in half while the trailer was in operation. Both halves of each of three studs were sent to the laboratory to determine the cause of failure. Visual examination of the fracture surfaces of the studs disclosed...
Abstract
Each of the ten studs on one wheel of a semitrailer used to haul coal broke in half while the trailer was in operation. Both halves of each of three studs were sent to the laboratory to determine the cause of failure. Visual examination of the fracture surfaces of the studs disclosed beach marks, indicative of fatigue cracking, starting at opposite sides of each stud, with final fracture occurring across the stud. Each failure occurred in the first thread of the stud. It was concluded that the wheel studs fractured by reversed-bending fatigue. To minimize the possibility of a recurrence, the wheel nuts were tightened with an air impact wrench to a torque of 610 to 678 J (450 to 500 ft · lb) dry. All wheel studs were checked at normal maintenance periods to ensure uniform and proper loading, and no further failures occurred.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001309
EISBN: 978-1-62708-215-0
... Abstract Bending fatigue caused crack propagation and catastrophic failures at several locations near the welds on the low-carbon steel tubular cargo box frame of police three-wheel motorcycles. ANSYS finite element analysis revealed that bending stresses in some of the frame members were...
Abstract
Bending fatigue caused crack propagation and catastrophic failures at several locations near the welds on the low-carbon steel tubular cargo box frame of police three-wheel motorcycles. ANSYS finite element analysis revealed that bending stresses in some of the frame members were aggravated by poor detail design between vertical and horizontal tubes. Stresses observed in the ANSYS analysis were not sufficient to cause the onset of fatigue. However when compounded by stress concentration factors and in-service dynamic loading, the frame could have been regularly subjected to stresses over the fatigue limit of the material. A strain gage static loading test verified FEM results, and finite element techniques were applied in the design of reinforcing members to renovate the frames. Material properties were determined and welding procedures specified for the reinforcing members. Inspection intervals were devised to avoid future problems.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001633
EISBN: 978-1-62708-221-1
... Abstract Failure analysis of a mobile harbor crane wheel hub that included SEM and EDS analyses demonstrated that the mechanism of failure was fatigue. The wheel hub was a ductile cast iron component that had been subjected to cyclic loading during a ten-year service period. The fracture...
Abstract
Failure analysis of a mobile harbor crane wheel hub that included SEM and EDS analyses demonstrated that the mechanism of failure was fatigue. The wheel hub was a ductile cast iron component that had been subjected to cyclic loading during a ten-year service period. The fracture surface of the fatigue failure also contained corrosion deposit, suggesting that cracking occurred over a period of time sufficient to allow corrosion of the cracked surfaces. Replacement and alignment of the failed wheel hub was recommended along with inspection of the nonfailed wheel hubs that remained on the crane.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001306
EISBN: 978-1-62708-215-0
... Abstract Failure of carbon-manganese steel wheel studs caused by improper tightening of the inner wheel nuts resulted in separation of a dual wheel assembly on a heavy truck. The benchmark pattern observed on the fracture surfaces of the studs evidenced fatigue cracks emanating from multiple...
Abstract
Failure of carbon-manganese steel wheel studs caused by improper tightening of the inner wheel nuts resulted in separation of a dual wheel assembly on a heavy truck. The benchmark pattern observed on the fracture surfaces of the studs evidenced fatigue cracks emanating from multiple origins around the circumference. There was no indication that any microstructural characteristics of the material contributed to the failure. Inclusions that were present were small and relatively few in number. Failure to check the torque of the inner wheel nuts as per the manufacturer's recommendation caused the inner wheel nuts to loosen during break-in and lose the required clamping force. The development and promotion of educational programs on proper wheel tightening procedures was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048102
EISBN: 978-1-62708-224-2
... Abstract A bridge wheel from a 272,160 kg stripper crane fractured in the web near the rim after one year of service. The wheel was forged from 1055 steel, and the tread, hub faces, and hub bore were machined. Beach marks indicative of fatigue at ten locations were revealed by macroscopic...
Abstract
A bridge wheel from a 272,160 kg stripper crane fractured in the web near the rim after one year of service. The wheel was forged from 1055 steel, and the tread, hub faces, and hub bore were machined. Beach marks indicative of fatigue at ten locations were revealed by macroscopic examination of the fracture surfaces. The surface of the web was heavily scaled and decarburized. A gross forging defect extending about 1.8 mm along the fracture surface was disclosed by examination of a micrograph of a section through one of the fatigue origins. Shallower forging defects were visible along the web surface. Fatigue cracking of the wheel was initiated at forging defects in the web. Replacement wheels were machined all over and were magnetic particle inspected to detect any cracks that could act as stress raisers.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047169
EISBN: 978-1-62708-217-4
... Abstract The flange on an outboard main-wheel half (aluminum alloy 2014-T6 forging) on a commercial aircraft fractured during takeoff. The failure was discovered later during a routine enroute check. The flange section that broke away was recovered at the airfield from which the plane took off...
Abstract
The flange on an outboard main-wheel half (aluminum alloy 2014-T6 forging) on a commercial aircraft fractured during takeoff. The failure was discovered later during a routine enroute check. The flange section that broke away was recovered at the airfield from which the plane took off and was thus available for examination. Failure occurred after 37 landings (about 298 roll km, or 185 roll miles). Examination of the fracture surfaces revealed that a forging defect was present in the wall of the wheel half. The anodized coating showed distinct twin-parallel and end-grain patterns between which the fracture occurred. The periphery of the defect was the site of several small fatigue cracks that eventually progressed through the remaining wall. Rapid fatigue then progressed circumferentially. Metallographic examination using Keller's reagent showed that the microstructure was normal for aluminum alloy 2014-T6 and the hardness surpassed the minimum hardness required for aluminum alloy 2014-T6. An abrupt change in the direction of grain flow across the fracture plane indicated that the wall had buckled during forging. This evidence supported the conclusion that the wheel half failed in the flange by fatigue as the result of a rather large subsurface forging defect. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001303
EISBN: 978-1-62708-215-0
... Abstract A sand-cast LM6M aluminum alloy sprocket drive wheel in an all-terrain vehicle failed. Extensive cracking had occurred around each of the six bolt holes in the wheel. Evidence of considerable deformation in this area was also noted. Examination indicated that the part failed because...
Abstract
A sand-cast LM6M aluminum alloy sprocket drive wheel in an all-terrain vehicle failed. Extensive cracking had occurred around each of the six bolt holes in the wheel. Evidence of considerable deformation in this area was also noted. Examination indicated that the part failed because of gross overload. Use of an alloy with a much higher yield strength and improvement in design were recommended.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001777
EISBN: 978-1-62708-241-9
... Abstract The structural collapse of an iron-ore bucket-wheel stacker reclaimer at the beginning of operation was investigated by means of mechanical tests, microstructural characterization, and computational structural analysis. The mechanical failure was a consequence of a brittle fracture...
Abstract
The structural collapse of an iron-ore bucket-wheel stacker reclaimer at the beginning of operation was investigated by means of mechanical tests, microstructural characterization, and computational structural analysis. The mechanical failure was a consequence of a brittle fracture by cleavage. The crack followed the heat-affected zone of a welded joint connecting a rectangular hollow section member and a plate flange. The main factors contributing to failure were related with a combination of design-in and manufacturing-in factors like high load-strength ratio at the point of failure, local stress concentration as a result of geometry restrictions, and weld defects. This particular section was responsible for the load transfer between the front tie member and the boom extremity, and its failure was the main cause of the catastrophic failure of the equipment.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047125
EISBN: 978-1-62708-217-4
... Abstract A commercial aircraft wheel half, machined from an aluminum alloy 2014 forging that had been heat treated to the T6 temper, was removed from service because a crack was discovered in the area of the grease-dam radius during a routine inspection. Neither the total number of landings nor...
Abstract
A commercial aircraft wheel half, machined from an aluminum alloy 2014 forging that had been heat treated to the T6 temper, was removed from service because a crack was discovered in the area of the grease-dam radius during a routine inspection. Neither the total number of landings nor the roll mileage was reported, but about 300 days had elapsed between the date of manufacture and the date the wheel was removed from service. The analysis (visual inspection, macrographs, micrographs, electron microprobe) supported the conclusions that the wheel half failed by fatigue. The fatigue crack originated at a material imperfection and progressed in more than one plane because changes in the direction of wheel rotation altered the direction of the applied stresses. Recommendations included rewriting the inspection specifications to require sound forgings.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047165
EISBN: 978-1-62708-217-4
... Abstract Two outboard main-wheel halves (aluminum alloy 2014-T6 forged) from a commercial aircraft were removed from service because of failure. One wheel half was in service for 54 days and had made 130 landings (about 1046 roll km, or 650 roll mi) when crack indications were discovered during...
Abstract
Two outboard main-wheel halves (aluminum alloy 2014-T6 forged) from a commercial aircraft were removed from service because of failure. One wheel half was in service for 54 days and had made 130 landings (about 1046 roll km, or 650 roll mi) when crack indications were discovered during eddy-current testing. The flange on the second wheel half failed after only 31 landings, when about 46 cm (18 in.) of the flange broke off as the aircraft was taxiing. Stains on the fracture surfaces were used to determine when cracking was initiated. The analysis (visual inspection, liquid penetrant inspection, and micrographs with deep etching in aqueous 20% sodium hydroxide) supported the conclusion that failure on both wheel halves was by fatigue caused by a forging defect resulting from abnormal transverse grain flow. The crack in the first wheel half occurred during service, and the surfaces became oxidized. Because the fracture surface of the second wheel half had chromic acid stains, it was obvious that the forging defect was open to the surface during anodizing. No recommendations were made except to notify the manufacturer.
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