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Iván Uribe Pérez, Tito Luiz da Silveira, Tito Fernando da Silveira, Heloisa Cunha Furtado
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Welded steel (Steel, general)
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Welded steel (Steel, general)
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0047529
EISBN: 978-1-62708-230-3
... of the undercut, which was an inherent stress raiser. Recommendations included revised joint design to ensure full root penetration. Fillet welds Heat affected zone Joint design Papermaking Shells (structural forms) Steam preheaters Weld defects Welded steel (Steel, general) Joining-related failures...
Abstract
A weld that attached the head to the shell of a preheater containing steam at 1.4 MPa (200 psi) and was used in the manufacture of paper cracked in service. The original joint contained a 6.4 by 50 mm backing ring that had been tack welded to the inside surface of the shell in a position to project beyond the fully beveled top edge of the shell. The projecting edge of the ring fitted against a deep undercut on the inner corner of the rim of the head. The internal 90-deg angle in this undercut was sharp, with almost no fillet. A bevel from the lower edge of the undercut to the outside of the head completed the groove for the circumferential attachment weld. Investigation (visual inspection and actual size views etched in hot 50% hydrochloric acid) supported the conclusion that cracking occurred in the HAZ in the head of the original design, originating in the sharp corner of the undercut, which was an inherent stress raiser. Recommendations included revised joint design to ensure full root penetration.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001609
EISBN: 978-1-62708-229-7
... Abstract Alloy 430 stainless steel tube-to-header welds failed in a heat recovery steam generator (HRSG) within one year of commissioning. The HRSG was in a combined cycle, gas-fired, combustion turbine electric power plant. Alloy 430, a 17% Cr ferritic stainless steel, was selected because...
Abstract
Alloy 430 stainless steel tube-to-header welds failed in a heat recovery steam generator (HRSG) within one year of commissioning. The HRSG was in a combined cycle, gas-fired, combustion turbine electric power plant. Alloy 430, a 17% Cr ferritic stainless steel, was selected because of its resistance to chloride and sulfuric acid dewpoint corrosion under conditions potentially present in the HRSG low-pressure feedwater economizer. Intergranular corrosion and cracking were found in the weld metal and heat-affected zones. The hardness in these regions was up to 35 HRC, and the weld had received a postweld heat treatment (PWHT). Metallographic examination revealed that the corroded areas contained undertempered martensite. Fully tempered weld areas with a hardness of 93 HRB were not attacked. No evidence of corrosion fatigue was found. Uneven temperature control during PWHT was the most likely cause of failure.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001049
EISBN: 978-1-62708-214-3
... Abstract Routine inspections of a carbon steel wood pulp digester revealed a sharply increasing number of cracks in the overlay metal on the internal surface of the digester after 1 and 2 years of service. The weld overlay was composed of type 309 stainless steel on the top fourth...
Abstract
Routine inspections of a carbon steel wood pulp digester revealed a sharply increasing number of cracks in the overlay metal on the internal surface of the digester after 1 and 2 years of service. The weld overlay was composed of type 309 stainless steel on the top fourth of the digester and of a proprietary high-nickel material on the bottom three-fourths. Examination revealed three distinct modes of deterioration. General corrosion was linked to the use of unspecified overlay metal. Cracking resulted during installation from the use of a material susceptible to hot cracking. Deep corrosion fissures then developed at hot crack sites as a result of crevice corrosion. Use of the appropriate overlay material was recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091528
EISBN: 978-1-62708-229-7
... of these cracks, which had penetrated the pipe wall, were responsible for leaks detected in a hydrostatic test performed during a general inspection after seven years of service. Investigation (visual inspection, visual and ultrasonic weld examination, water analysis, and chemical analysis) supported...
Abstract
A 150 mm (6 in.) schedule 80S type 304 stainless steel pipe (11 mm, or 0.432 in., wall thickness), which had served as an equalizer line in the primary loop of a pressurized-water reactor, was found to contain several circumferential cracks 50 to 100 mm (2 to 4 in.) long. Two of these cracks, which had penetrated the pipe wall, were responsible for leaks detected in a hydrostatic test performed during a general inspection after seven years of service. Investigation (visual inspection, visual and ultrasonic weld examination, water analysis, and chemical analysis) supported the conclusion that the failure was caused by SCC due to stress, sensitization, and environment. Recommendations included replacing all pipe sections and installing them using low-heat-input, multiple-pass welding procedures.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0091345
EISBN: 978-1-62708-220-4
... Abstract Beveled weld-joint V-sections were fabricated to connect inlet and outlet sections of tubes in a type 347 stainless steel heat exchanger for a nitric acid concentrator. Each V-section was permanently marked with the tube numbers by a small electric-arc pencil. After one to two years...
Abstract
Beveled weld-joint V-sections were fabricated to connect inlet and outlet sections of tubes in a type 347 stainless steel heat exchanger for a nitric acid concentrator. Each V-section was permanently marked with the tube numbers by a small electric-arc pencil. After one to two years of service, multiple leaks were observed in the heat-exchanger tubes. Investigation supported the conclusion that the corrosion occurred at two general locations: the stop point of the welds used to connect the inlet and outlet legs of the heat exchanger, and the stop points on the identifying numerals. Recommendations included replaced the material with type 304L stainless steel.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001223
EISBN: 978-1-62708-233-4
... Abstract The corner of a welded sheet construction made from austenitic corrosion-resistant chromium-nickel steel showed corrosive attack of the outer sheet. This attack was most severe at the points subjected to the greatest heat during welding. Particularly large amounts of weld metal had...
Abstract
The corner of a welded sheet construction made from austenitic corrosion-resistant chromium-nickel steel showed corrosive attack of the outer sheet. This attack was most severe at the points subjected to the greatest heat during welding. Particularly large amounts of weld metal had been applied. Microscopic examination showed grain disintegration was promoted by the thickness of the weld bead and the amount of heat required to produce it. If nonstabilized austenitic sheet is to be used in the future, one of the particularly low-carbon steels, X2 CrNi 18 9 or X2 CrNiMo 18 10, is recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048814
EISBN: 978-1-62708-229-7
... Abstract A nuclear steam-generator vessel constructed of 100-mm thick SA302, grade B, steel was found to have a small leak. The leak originated in the circumferential closure weld joining the transition cone to the upper shell. The welds had been fabricated from the outside by the submerged arc...
Abstract
A nuclear steam-generator vessel constructed of 100-mm thick SA302, grade B, steel was found to have a small leak. The leak originated in the circumferential closure weld joining the transition cone to the upper shell. The welds had been fabricated from the outside by the submerged arc process with a backing strip. The backing was back gouged off, and the weld was completed from the inside with E8018-C3 electrodes by the shielded metal arc process. Striations of the type normally associated with progressive or fatigue-type failures including beach marks that allowed tracing the origin of the fracture to the pits on the inner surface of the vessel were revealed. Copper deposits with zinc were revealed by EDS examination of discolorations. Pitting was revealed to have been caused by poor oxygen control in the steam generators and release of chloride into the steam generators. It was concluded by series of controlled crack-propagation-rate stress-corrosion tests that A302, grade B, steel was susceptible to transgranular stress-corrosion attack in constant extension rate testing with as low as 1 ppm chloride present. It was recommended to maintain the coolant environment low in oxygen and chloride. Copper ions in solution should be eliminated or minimized.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001562
EISBN: 978-1-62708-230-3
... is generally fabricated of carbon steel. However, the inlet cone, because of severe service erosion/corrosion conditions where sawdust, cooking liquor, and steam enter, was fabricated of American Iron and Steel Institute (AISI) 304L stainless steel with E308 welds. Typical liquor concentration...
Abstract
The Pandia digester is a long cylindrical vessel which uses alkaline sulfite liquor to cook sawdust for pulping. The inlet cone was fabricated from AISI 304L stainless steel with E308 welds. Typical liquor concentration was approximately 80% NaOH, 20% Na2SO3 with chloride concentrations at 2 grams per liter. The operating pressures in the inlet cone were up to 1.2 MN/sq m (170 psig). The inlet cone had developed leaks within a year of service. Liquid penetrant inspection showed significant through-wall cracking near the fillet welds joining the bottom flange and side wall and the butt welds. Metallographic specimens were prepared from the welds to examine the microstructure and nature of the cracks. The cooking liquor at the inlet cone contained over ppm chlorides and was aggressive to 304 stainless steel. The cracking was identified as chloride-induced SCC. The inlet cone was replaced with an Inconel clad carbon steel inlet cone to combat the SCC.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047566
EISBN: 978-1-62708-235-8
..., the fillet weld, and the cover. The structure was found to contain a zone of brittle martensite in the portion of the weld adjacent to the low-carbon steel handle; fracture had occurred in this zone. Sufficient heat had been generated during welding to fuse an excessive amount of the carbon steel...
Abstract
Handles welded to the top cover plate of a chemical-plant downcomer broke at the welds when the handles were used to lift the cover. The handles were fabricated of low-carbon steel rod; the cover was of type 502 stainless steel plate. The attachment welds were made with type 347 stainless steel filler metal to form a fillet between the handle and the cover. The structure was found to contain a zone of brittle martensite in the portion of the weld adjacent to the low-carbon steel handle; fracture had occurred in this zone. The brittle martensite layer in the weld was the result of using too large a welding rod and too much heat input, melting of the low-carbon steel handle, which diluted the austenitic stainless steel filler metal and formed martensitic steel in the weld zone. Because it was impractical to preheat and postheat the type 502 stainless steel cover plate, the low-carbon steel handle was welded to low-carbon steel plate, using low-carbon steel electrodes. This plate was then welded to the type 502 stainless steel plate with type 310 stainless steel electrodes. This design produced a large weld section over which the load was distributed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001525
EISBN: 978-1-62708-220-4
... of the welded low-carbon steel storage tank shows evidence of general corrosion with severe discoloration at the weld. A sample of this corrosion debris was placed into a watch glass and soaked in a few drops of deionized water. The pH of the resulting solution indicated that it was highly alkaline...
Abstract
Welded steel storage vessels used to hold mildly alkaline solution were produced in exactly the same manner from deep-drawn aluminum-killed SAE 1006 low-carbon steel sheet. After the cylindrical shell was drawn, a top low-carbon steel closure was welded to the inside diameter. The containers were then filled with the slightly alkaline solution, pressurized, and allowed to stand under ambient conditions. A small number, less than 1%, were returned because they began to leak in service. Inspection revealed general corrosion and pitting on the inner surfaces. However, other tanks that experienced the same service conditions developed no corrosion. Corrosion was linked to forming defects that provided sites for localized corrosion, and to lack of steam drying after cleaning, which increased susceptibility to general corrosion.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001061
EISBN: 978-1-62708-214-3
... Abstract Schedule 80 low-carbon steel pipes used to transfer kraft liquor in a Kamyr continuous pulp digester failed within 18 months after installation. Visual and metallographic examinations established that the cracking initiated on the internal surfaces of the equalizer pipes in the welds...
Abstract
Schedule 80 low-carbon steel pipes used to transfer kraft liquor in a Kamyr continuous pulp digester failed within 18 months after installation. Visual and metallographic examinations established that the cracking initiated on the internal surfaces of the equalizer pipes in the welds and heat-affected zones (HAZs). Fracture/crack morphology was brittle and primarily intergranular and deposits at crack tips were primarily iron oxides with significant amounts of sodium compounds. On these bases, the cracking was characterized as intergranular stress-corrosion cracking (IGSCC). Corrosion-related deterioration was not found, indicating that the material was generally suitable for the intended service. High residual tensile stresses in the welds and HAZS, resulting from field welding under highly constrained conditions using inadequate weld procedures, were the most probable cause of the failures. Minimizing residual stresses through use of welding procedures that include appropriate preweld and interpass temperatures and postweld stress relief heat treatment at 650 deg C (1200 deg F) was recommended to prevent further failures.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c0089716
EISBN: 978-1-62708-231-0
... identified but were generally classified as semi-killed carbon steels. Investigation (visual inspection, hardness testing, chemical analysis, Charpy V-notch testing, and drop-weight testing) supported the conclusions that the fracture was initiated by weld imperfections and propagated in a brittle manner...
Abstract
A railway tank car developed a fracture in the region of the sill and shell attachment during operation at -34 deg C (-30 deg F). On either side of the sill-support member, cracking initiated at the weld between a 6.4 mm thick frontal cover plate and a 1.6 mm thick side support plate. The crack then propagated in a brittle manner upward through the side plate, through the welds attaching the side plate to a 25 mm (1 in.) thick shell plate (ASTM A212, grade B steel), and continued for several millimeters in the shell plate before terminating. Other plates involved were not positively identified but were generally classified as semi-killed carbon steels. Investigation (visual inspection, hardness testing, chemical analysis, Charpy V-notch testing, and drop-weight testing) supported the conclusions that the fracture was initiated by weld imperfections and propagated in a brittle manner as a result of service stresses acting on the plate having low toughness at the low service temperatures encountered. Recommendations included that the specifications for the steel plates be modified to include a toughness requirement and that improved welding and inspection practices be performed to reduce the incidence of weld imperfections.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047428
EISBN: 978-1-62708-235-8
.... Given the small critical crack sizes characteristic of ultrahigh-strength materials, it is generally unwise to weld them. It is particularly inadvisable to hardface ultrahigh-strength steel parts with hard, brittle, crack-prone materials when high service stresses will be encountered. The operators...
Abstract
A cast dragline bucket tooth failed by fracturing after a short time in service. The tooth was made of medium-carbon low-alloy steel heat treated to a hardness of 555 HRB. The fracture surface was covered with chevron marks. These converged at several sites on the surface of the tooth. A hardfacing deposit was located at each of these sites. Visual inspection of the hardfacing deposits revealed numerous transverse cracks, characteristic of many types of hardfacing. This failure was caused by cracks present in hardfacing deposits that had been applied to the ultrahigh-strength steel tooth. Given the small critical crack sizes characteristic of ultrahigh-strength materials, it is generally unwise to weld them. It is particularly inadvisable to hardface ultrahigh-strength steel parts with hard, brittle, crack-prone materials when high service stresses will be encountered. The operators of the dragline bucket were warned against further hardfacing of these teeth.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001749
EISBN: 978-1-62708-215-0
... Abstract An oxygen line that was part of a mobile, truck -mounted oxygen-acetylene welding unit exploded in service. Analysis revealed that the failure occurred at the flexible hose-to-valve connection. It was further determined that a steel adapter had been installed at the point of failure...
Abstract
An oxygen line that was part of a mobile, truck -mounted oxygen-acetylene welding unit exploded in service. Analysis revealed that the failure occurred at the flexible hose-to-valve connection. It was further determined that a steel adapter had been installed at the point of failure to make the connection. Use of the adapter which joined with a brass nipple, created an unacceptable dissimilar metal joint. The steel also provided a source for the generation of sparks. Loctite, a hydrocarbon sealant that is highly flammable and explosive in contact with pure oxygen, had been used to seal the threaded joint. It was recommended that only brass fittings be used to assemble removable joints and that use of washers, sealants, and hydrocarbon lubricants be strictly avoided.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c0091598
EISBN: 978-1-62708-218-1
... Abstract After 10 to 20 months of service, the carbon steel hoppers on three trucks used to transport bulk ammonium nitrate prills developed extensive cracking in the upper walls. The prills were discharged from the steel hoppers using air superchargers that generated an unloading pressure...
Abstract
After 10 to 20 months of service, the carbon steel hoppers on three trucks used to transport bulk ammonium nitrate prills developed extensive cracking in the upper walls. The prills were discharged from the steel hoppers using air superchargers that generated an unloading pressure of approximately 11 kPa (7 psi). Each hopper truck held from 9,100 to 11,800 kg (10 to 13 tons) of prills when fully loaded and handled approximately 90,700 kg (100 tons) per month. The walls of the hoppers were made of 2.7 mm (0.105 in.) thick flat-rolled carbon steel sheet of structural quality, conforming to ASTM A 245 (obsolete specification replaced by A 570 and A 611). Investigation (visual inspection and 100x micrographs polished and etched with nital) supported the conclusion that failure of the hoppers was the result of intergranular SCC of the sheet-steel walls because of contact with a highly concentrated ammonium nitrate solution. Recommendations included the cost-effective solution of applying a three-coat epoxy-type coating with a total dry thickness of 0.3 mm (0.013 in.) to the interior surfaces of the hoppers.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001051
EISBN: 978-1-62708-214-3
... Abstract A pair of steam generators operating at a pressurized water reactor site were found to be leaking near a closure weld. The generators were the vertical U-tube type, constructed from ASTM A302 grade B steel. The shell material exhibited high hardness values prior to confirmatory heat...
Abstract
A pair of steam generators operating at a pressurized water reactor site were found to be leaking near a closure weld. The generators were the vertical U-tube type, constructed from ASTM A302 grade B steel. The shell material exhibited high hardness values prior to confirmatory heat treatment, indicating high residual stresses in the area of the weld. All cracks were transgranular and were associated with pits on the inside surfaces of the vessels. It was concluded that the cracking was caused by a low-cycle corrosion fatigue phenomenon, with cracks initiating at areas of localized corrosion and propagating by fatigue. The cause of the pitting/cracking was related to the unit's copper species in solution.
Book Chapter
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001813
EISBN: 978-1-62708-241-9
..., the formation of graphite nodules in carbon and low alloy steels, contributes to many failures in high-temperature environments. Three such failures in power-generating systems were analyzed to demonstrate the unpredictable nature of this failure mechanism and its effect on material properties and structures...
Abstract
Graphitization, the formation of graphite nodules in carbon and low alloy steels, contributes to many failures in high-temperature environments. Three such failures in power-generating systems were analyzed to demonstrate the unpredictable nature of this failure mechanism and its effect on material properties and structures. In general, the more randomly distributed the nodules, the less effect they have on structural integrity. In the cases examined, the nodules were found to be organized in planar arrays, indicating they might have an effect on material properties. Closer inspection, however, revealed that the magnitude of the effect depends on the relative orientation of the planar arrangement and principle tensile stress. For normal orientation, the effect of embrittlement tends to be most severe. Conversely, when the orientation is parallel, the nodules have little or no effect. The cases examined show that knowledge is incomplete in regard to graphitization, and the prediction of its occurrence is not yet possible.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001141
EISBN: 978-1-62708-227-3
... of the welds shown in Figs. 4 , 5 , and 9 . The maximum hardness recorded was 270HV. Lamellar Tearing Test To assess the susceptibility of steel late to lamellar tearing the slice bend test 1 , 2 , a simple and inexpensive destructive test was used. Figure 11 illustrates the procedure...
Abstract
During a refit of a twenty-year-old Naval destroyer, two cracks were found on the inside of the killed carbon-manganese steel hull plate at the forward end of the boiler room. The cracks coincided with the location of the top and bottom plates of the bilge keel. Metallurgical examination of sections cut from the cracked area identified lamellar tearing as the principle cause of the cracking. This was surprising in 6 mm thick hull plates. Corrosion fatigue and general corrosion also contributed to hull plate perforation. Although it is probable that more lamellar tears exist near the bilge keel in other ships and may be a nuisance in the future, the hull integrity of the ships is not threatened and major repairs are not needed.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001344
EISBN: 978-1-62708-215-0
... Abstract Several 304H stainless steel superheater tubes fractured in stressed areas within hours of a severe caustic upset in the boiler feedwater system. Tests performed on a longitudinal weld joint, which connected two adjacent tubes in the tertiary superheater bank, confirmed caustic-induced...
Abstract
Several 304H stainless steel superheater tubes fractured in stressed areas within hours of a severe caustic upset in the boiler feedwater system. Tests performed on a longitudinal weld joint, which connected two adjacent tubes in the tertiary superheater bank, confirmed caustic-induced stress-corrosion cracking, promoted by the presence of residual welding stresses. Improved maintenance of check valves and routine inspection of critical monitoring systems (conductivity alarms, sodium analyzers, etc.) were recommended to help avoid future occurrences of severe boiler feedwater contamination. Additional recommendations were to eliminate these short longitudinal weld joints by using a bracket assembly joint between the tubes, use a post-weld heat treatment to relieve residual welding stress or select a more stress-corrosion cracking resistant alloy for this particular application.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001909
EISBN: 978-1-62708-235-8
... parameters resulted in acceptable welds. Bombs (weapons) Bomb fins Welded joints Weld defects Low-carbon steel Joining-related failures Introduction Component: MK#83 and MK#84 general purpose bomb fins Manufacturing defects: Nonpenetrating plug welds Background A First Article...
Abstract
Welded low-carbon steel bomb fins were rejected because of poor weld practice. Visual and metallographic examination revealed that the resistance plug welds that attach the outer skin to the inner spar displayed inadequate weld penetration. Recommended changes to the resistance welding parameters resulted in acceptable welds.