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Weld joints

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Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001317
EISBN: 978-1-62708-215-0
... dished ends were from the same batch. Dished ends from other batches have performed without problems. Specimen Selection Specimen 1 was removed by cutting along the circumferential weld joint (retaining some portion of the weldment with the dished end) after the sodium was drained off...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001411
EISBN: 978-1-62708-234-1
...Abstract Abstract A welded joint between lengths of 4 in. OD x 13 SWG copper pipe which formed part of a cold-water main failed by cracking over one-third of the circumference. Microscopic examination of the filler metal showed that it had a structure corresponding to a brass of the 60:40 type...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001186
EISBN: 978-1-62708-234-1
... Welded joints Wire Cold-drawn steel Ductile fracture A steel wire of 2.3 mm diameter broke during cable twisting. The fracture occurred obliquely to the longitudinal axis of the wire and showed a constriction at the end. Therefore it was a ductile fracture. File mark type work defects were...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089738
EISBN: 978-1-62708-235-8
... the conclusion that the crack in the header tube was the result of a stress concentration at the toe of the weld joining a doubler collar to the tube. The stress concentration was caused by undercutting from poor welding technique and an unfavorable joint design that did not permit a good fit-up. Recommendations...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048356
EISBN: 978-1-62708-229-7
...Abstract Abstract Welded to the top of a dust bin for rigid support, a furnace water-wall tube in a new stationary boiler broke at the welded joint shortly after start-up. The tubes measured 64 mm (2.5 in.) OD by 3.2 mm (0.125 in.) wall thickness and were made of carbon steel to ASME SA-226...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0089722
EISBN: 978-1-62708-217-4
.... Aircraft components Butt welds Design Elbows Fatigue cracking Lap welds Tubes Vibratory stresses Welded joints 321 UNS S32100 Joining-related failures Fatigue fracture The welded elbow assembly shown in Fig. 1 was part of a hydraulic-pump pressure line for a jet aircraft. The other end...
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Published: 01 December 1992
Fig. 2 Fracture surface through weld joint. 3×. More
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Published: 01 December 1992
Fig. 3 Fracture opposite weld joint. 3×. More
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Published: 01 December 1992
Fig. 4 Fracture surface of weld joint. 10×. More
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Published: 01 December 1992
Fig. 5 Fracture surface opposite weld joint. 10×. More
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Published: 01 December 1992
Fig. 10 Microstructure near weld joint. Structure of martensite and retained austenite. 5% nital etch. 1000×. More
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Published: 01 December 1992
Fig. 11 Microstructure opposite weld joint. Structure is tempered martensite. 5% nital etch. 1000×. More
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Published: 30 August 2021
Fig. 3 Schematic of defects and discontinuities in welded joints More
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Published: 30 August 2021
Fig. 39 Fracture weld joint on alloy 7075 collar side of the swing arm structure More
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001594
EISBN: 978-1-62708-229-7
...Abstract Abstract Nuclear power plants typically experience two or three high-cycle fatigue failures of stainless steel socket-welded connections in small bore piping during each plant-year of operation. This paper discusses fatigue-induced failure in socket-welded joints and the strategy Texas...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0047694
EISBN: 978-1-62708-219-8
... the welded joints in wrap tests. The welded wire was annealed by resistance heating. The wire ends had a chisel shape, produced by the use of sidecutters. Tests of the heat treatment temperatures showed that the wire near the weld area exceeded 775 deg C (1425 deg F). Metallographic examination revealed...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001344
EISBN: 978-1-62708-215-0
...Abstract Abstract Several 304H stainless steel superheater tubes fractured in stressed areas within hours of a severe caustic upset in the boiler feedwater system. Tests performed on a longitudinal weld joint, which connected two adjacent tubes in the tertiary superheater bank, confirmed...
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001350
EISBN: 978-1-62708-215-0
...Abstract Abstract Upon arrival at the erection site, an AISI type 316L stainless steel tank intended for storage of fast breeder test reactor coolant (liquid sodium) exhibited cracks on its shell at two of four shell/nozzle fillet-welded joint regions. The tank had been transported from...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047710
EISBN: 978-1-62708-225-9
...Abstract Abstract A 9310 steel gear was found to be defective after a period of engine service. A linear crack approximately was discovered by routine magnetic-particle inspection of an electron beam welded joint that attached a hollow stub shaft to the web of the gear. The welding procedure...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0048733
EISBN: 978-1-62708-235-8
...Abstract Abstract The brine-heater shell in a seawater-conversion plant failed by bursting along a welded joint connecting the hot well (C70600 per ASTM B 466) to the heater shell (ASTM A285, grade C steel). Three cracks in the welded joints between the heater shell and the hot well were...