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Book Chapter
Pitting Corrosion of Copper Pipes in a Residential Water Delivery System
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001698
EISBN: 978-1-62708-222-8
... hardness levels (210 mg/l), high levels of sulfate ions (55 mg/l), a pH of 7.6 and a sulfate-to-chloride ratio of 3:1. Analysis of corrosion product removed from the ID surfaces of the pipe section revealed that an environment rich in carbonates existed inside the pipe, a result of the hard water supply...
Abstract
A residential subdivision near Tampa, FL was constructed in 1984 through 1985. Several sections of copper pipe were removed from one residence that had reported severe leaking. Visual examination revealed extensive pitting corrosion throughout the ID surfaces of the sample. Microscopic evaluation of a cross section of a copper pipe revealed extensive pitting corrosion throughout the inner diametral surfaces of the pipe. Some pits had penetrated through the wall thickness, causing the pin hole leaks. Analysis of a sample of water obtained from the subdivision revealed relatively high hardness levels (210 mg/l), high levels of sulfate ions (55 mg/l), a pH of 7.6 and a sulfate-to-chloride ratio of 3:1. Analysis of corrosion product removed from the ID surfaces of the pipe section revealed that an environment rich in carbonates existed inside the pipe, a result of the hard water supply. It was concluded that pitting corrosion was a result of the corrosive waters supplied by the local water utility. Waters could be rendered non-pitting by increasing their pH to 8 or higher and neutralizing the free carbon dioxide.
Book Chapter
Stress-Corrosion Cracking of a Die-Cast Zinc Alloy Nut
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0048620
EISBN: 978-1-62708-225-9
... Abstract Two nuts were used to secure the water-supply pipes to the threaded connections on hot-water and cold-water taps. The nut used on the cold-water tap fractured about one week after installation. Examination of the fracture surfaces of the coldwater nut did not reveal any obvious defects...
Abstract
Two nuts were used to secure the water-supply pipes to the threaded connections on hot-water and cold-water taps. The nut used on the cold-water tap fractured about one week after installation. Examination of the fracture surfaces of the coldwater nut did not reveal any obvious defects to account for the fracture, but there were indications of excessive porosity in the nut. The fracture had occurred through the root of the first thread that was adjacent to the flange of the tap. It was found that the nut from the cold-water tap failed by SCC. Apparently, sufficient stress was developed in the nut to promote this type of failure by normal installation because there was no evidence of excessive tightening of the nut. Corrosion testing of the nuts indicated that the fractured nut was highly susceptible to intergranular corrosion because of either a deficiency in magnesium content or excessive impurities, such as lead, tin, or cadmium. This composition problem with zinc alloys was recognized many years ago, and particular attention has been directed toward ensuring that high-purity zinc is used. This corrective measure reportedly resulted in virtual elimination of this type of defect.
Book Chapter
Crevice Corrosion of Tubing in a Hydraulic-Oil Cooler
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048708
EISBN: 978-1-62708-229-7
... by crevice corrosion. The tubing in the cooler was replaced, and cooling-water supply was changed from river to city water, which contained no dirt to deposit on the tube surfaces. An alternate solution of installing replacement tubes in the vertical position to make deposition of solids from river water...
Abstract
The horizontal heat-exchanger tubes made of copper alloy C70600, in one of two hydraulic-oil coolers in an electric power plant, leaked after 18 months of service. River water was used as the coolant in the heat-exchanger tubes. Several nodules on the inner surface and holes through the tube wall, which appeared to have formed by pitting under the nodules, were revealed by visual examination. Steep sidewalls, which indicated a high rate of attack, were revealed by microscopic examination of a section through the pit which had penetrated the tube wall. The major constituent of reddish deposit on the inner surfaces of the tubes was revealed to be iron oxide and slight manganese dioxide. Effluent from steel mills upstream was indicated by the presence of these and other constituents to be the source of most of the solids found in the tubes. It was concluded that the tubing failed by crevice corrosion. The tubing in the cooler was replaced, and cooling-water supply was changed from river to city water, which contained no dirt to deposit on the tube surfaces. An alternate solution of installing replacement tubes in the vertical position to make deposition of solids from river water less likely was suggested.
Book Chapter
Dezincification of a Chromium-Plated Copper Alloy Tube
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091378
EISBN: 978-1-62708-219-8
... Abstract A 12.7 mm (0.5 in.) diam tube was removed from a potable water supply due to leaks. The tube wall thickness was 0.711 mm (0.028 in.) with a thin layer of chromium plate on the OD surface. The tube had been in service for approximately 33 years. Investigation (visual inspection, EDS...
Abstract
A 12.7 mm (0.5 in.) diam tube was removed from a potable water supply due to leaks. The tube wall thickness was 0.711 mm (0.028 in.) with a thin layer of chromium plate on the OD surface. The tube had been in service for approximately 33 years. Investigation (visual inspection, EDS deposit analysis, metallurgical examination, and unetched magnified images) supported the conclusion that failure occurred due to porous material typical of plug-type dezincification initiating from the inside surface. Where the dezincification had progressed through the tube wall, the chromium plate had exfoliated from the base material and cracked. Recommendations included replacing the piping with a more corrosion-resistant material such as red brass (UNS C23000), inhibited Admiralty brass (UNS C44300), or arsenical aluminum brass (UNS C68700).
Book Chapter
Pitting Corrosion of Copper Pipes for Potable Water Delivery
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001697
EISBN: 978-1-62708-219-8
... supplied to the property. The quantity of dissolved calcium carbonates in the tested water samples that were tested, was observed to be fairly high ( Tables 5 ) but generally typical of waters in Northeast Florida. Results of X-ray Diffraction Analysis of Four Corrosion Product Samples. Table 3...
Abstract
Corrosion in potable and nonpotable water systems has been well documented in the past, and new research discusses innovations in water treatment and materials that are designed to enhance the quality of a water system, whether commercial or residential. This paper is a collection of five case histories on the failure of copper and steels as used in potable and non-potable water systems. The case histories cover a range of applications in which copper and steel products have been used. Copper and steel pipes are the two most commonly used materials in residential, commercial and industrial applications. The projects that are discussed cover these three important applications. The purpose of presenting this information is to allow the reader to gain an understanding of real life corrosion issues that affect plumbing materials, how they should have been addressed during the design of the water system, and how a water system should be maintained during service. We share this information in the hope that the reader will gain some limited knowledge of the problems that exist, and apply that knowledge in designing or using water systems in day-to day life.
Image
A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corr...
Available to PurchasePublished: 01 January 2002
Fig. 42 A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corrosion. The pipe was part of a water supply to a fire protection system. The external surface was covered with soil and the inside surface in contact with water. The pipe had been experienced cracking and through
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A 25 cm (10 in.) diameter gray cast iron pipe that failed due to graphitic ...
Available to PurchasePublished: 15 January 2021
Fig. 42 A 25 cm (10 in.) diameter gray cast iron pipe that failed due to graphitic corrosion. The pipe was part of a water supply to a fire-protection system. The external surface was covered with soil and the inside surface in contact with water. The pipe experienced cracking and through
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Image
A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corr...
Available to Purchase
in Failure of a Cast Iron Water Pipe due to Graphitic Corrosion
> ASM Failure Analysis Case Histories: Buildings, Bridges, and Infrastructure
Published: 01 June 2019
Fig. 1 A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corrosion. The pipe was part of a water supply to a fire protection system. The external surface was covered with soil and the inside surface in contact with water. The pipe had been experienced cracking and through
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0046505
EISBN: 978-1-62708-219-8
... valves Water supply Malleable iron Galvanic corrosion One of three valves in a dry automatic sprinkler system tripped accidentally, thus activating the sprinklers. A check of the system indicated that the two other valves were about to trip. Maintenance records showed that the three valves had...
Abstract
One of three valves in a dry automatic sprinkler system tripped accidentally, thus activating the sprinklers. Maintenance records showed that the three valves had been in service less than two years. The valve consisted of a cast copper alloy clapper plate that was held closed by a pivoted malleable iron latch. The latch and top surface of the clapper plate were usually in a sanitary-water environment (stabilized, chlorinated well water with a pH of 7.3) under stagnant conditions. Process make-up water that had been clarified, filtered, softened, and chlorinated and had a pH of 9.8 was occasionally used in the system. Analysis (visual inspection and 250x micrograph) supported the conclusions that failure of the latch was caused by plastic deformation from extensive loss of metal by galvanic corrosion and the sudden loading related to the tripping of the valve. Failure in some regions of the contact area was by ductile (transgranular) fracture. Recommendations included changing the latch material from malleable iron to silicon bronze (C87300). The use of silicon bronze prevents corrosion or galvanic attack and proper adjustment of the latch maintains an adequate contact area.
Book Chapter
Impingement-Corrosion Failure of a Ferritic Malleable Iron Elbow
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0091402
EISBN: 978-1-62708-234-1
... Abstract Leakage was detected in a malleable iron elbow (ASTM A 47, grade 35018) after only three months in service. Life expectancy for the elbow was 12 to 24 months. The piping alternately supplied steam and cooling water to a tire-curing press. The supply line and elbow were subjected to 14...
Abstract
Leakage was detected in a malleable iron elbow (ASTM A 47, grade 35018) after only three months in service. Life expectancy for the elbow was 12 to 24 months. The piping alternately supplied steam and cooling water to a tire-curing press. The supply line and elbow were subjected to 14 heating and cooling cycles per hour for at least 16 h/day, or a minimum of 224 cycles/day. Steam and water pressure were 1035 kPa (150 psi) and 895 kPa (130 psi) respectively, and water-flow rate was estimated to be 1325 L/min (350 gal/min) based on pump capacity. Water-inlet temperature was 10 to 15 deg C (50 to 60 deg F) and outlet temperature was 50 to 60 deg C (120 to 140 deg F). The pH of the water was 6.9. Investigation (visual inspection, chemical analysis, and 67x nital etched micrographs) supported the conclusion that the elbows had been given the usual annealing and normalizing treatment for ferritizing malleable iron. This resulted in lower resistance to erosion and corrosion than pearlitic malleable iron. Recommendations included replacing the elbows with heat-treated fittings with a pearlitic malleable microstructure.
Book Chapter
Failure of a Bronze Pump Impeller by Cavitation Damage
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046414
EISBN: 978-1-62708-234-1
... quantities of air were being drawn into the system when water in the supply tank dropped below a certain level. It was concluded that cavitation erosion (due to the uptake of air) caused metal removal and microstructural damage in the impellers. Recommendations included adding a water-level control...
Abstract
Two water pumps were taken out of service because of reduced output. Visual inspection revealed considerable material loss in both impellers, which were 25.4 cm (10 in.) in diam x 1.3 cm (0.5 in.) wide and made from a cast bronze alloy. Several similar water pumps operating under nearly identical conditions, drawing water from an open tank through a standpipe, had no observable failures. Etched micrographs 100x of samples taken from the impellers showed clean, pockmarked, severely eroded surfaces, characteristic of cavitation damage. Investigation also revealed that considerable quantities of air were being drawn into the system when water in the supply tank dropped below a certain level. It was concluded that cavitation erosion (due to the uptake of air) caused metal removal and microstructural damage in the impellers. Recommendations included adding a water-level control to the piping system and excluding air from the pump inlet.
Book Chapter
Failure of a Cast Iron Water Pipe due to Graphitic Corrosion
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
... since a porous mass of material remains in place. Fig. 1 A 25 cm (10 in.) diam gray cast iron pipe that failed due to graphitic corrosion. The pipe was part of a water supply to a fire protection system. The external surface was covered with soil and the inside surface in contact with water...
Abstract
A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall perforations and cracking along its axis. The perforations and the crack were at the 6 o'clock position. Investigation (visual inspection, radiography, unetched macrographs, and tensile testing) supported the conclusion that the failure occurred as result of years of exposure to ground water in the soil resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron or coated and lined steel pipe, generally not susceptible to graphitic corrosion, were suggested as suitable replacement materials, and cathodic protection was also considered as a possibility.
Book Chapter
Corrosion of Steel Pipes in a Closed-Loop Hot Water Heating System
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001701
EISBN: 978-1-62708-219-8
... Abstract A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials...
Abstract
A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials. The fittings were mechanically threaded assemblies. Temperatures ranged from 150 to 155 deg F (65.6 to 68.3 deg C). Leaks in the system had reportedly initiated immediately after the building had been placed in service. The cause of corrosion inside the steel pipes was attributed to tuberculation caused by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system.
Book Chapter
Failure by Blowout of Aluminum Alloy 6061-T6 Connector Tubes From a Water-Cooling System
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047080
EISBN: 978-1-62708-235-8
... Abstract Several of the aluminum alloy 6061-T6 drawn seamless tubes (ASTM B 234, 2.5 cm (1.0 in.) OD with wall thickness of 1.7 mm (0.065 in.)) connecting an array of headers to a system of water-cooling pipes failed. The tubes were supplied in the O temper. They were bent to the desired...
Abstract
Several of the aluminum alloy 6061-T6 drawn seamless tubes (ASTM B 234, 2.5 cm (1.0 in.) OD with wall thickness of 1.7 mm (0.065 in.)) connecting an array of headers to a system of water-cooling pipes failed. The tubes were supplied in the O temper. They were bent to the desired curvature, preheated, then solution treated, water quenched, and then aged for 8 to 10 h. Analysis (visual inspection, slow-bend testing, 65x macrographic analysis, macroetching, spectrographic analysis, hardness tests, microhardness tests, tension tests, and microscopic examination) supported the conclusions that bending of the connector tubes in the annealed condition induced critical strain near the neutral axis of the tube, which resulted in excessive growth of individual grains during the subsequent solution treatment. Recommendations included bending the connector tubes in the T4 temper as early as possible after being quenched from the solution temperature. The tubes should be stored in dry ice after the quench until bending can be done. The tubes should be aged immediately after being formed. Flattening and slow-bend tests should be specified to ensure that the connector tubes had satisfactory ductility.
Book Chapter
Chloride Cracking of an Austenitic Stainless Steel Process Vessel Heating Coil
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001403
EISBN: 978-1-62708-220-4
... Abstract A process vessel heating coil, consisting of several 3 ft diam turns, was supplied with steam at 400 psi and a temperature of 343 deg C (650 deg F). At bi-weekly intervals well water was introduced to effect rapid cooling of the contents. After about eight months, leakage developed...
Abstract
A process vessel heating coil, consisting of several 3 ft diam turns, was supplied with steam at 400 psi and a temperature of 343 deg C (650 deg F). At bi-weekly intervals well water was introduced to effect rapid cooling of the contents. After about eight months, leakage developed from a circumferential crack on the underside of the uppermost turn. Shorter cracks were found at a similar location on the bottom turn, and further leakage occurred at pinhole perforations adjacent to the crack in the top turn and near to a butt-weld in the coil. Microscopic examination revealed that the cracks were predominantly of the intergranular variety. In addition, transgranular cracks were present. Material was an austenitic stainless steel of the type specified but the absence of columbium and titanium in significant amounts showed that it was not stabilized against intergranular carbide precipitation. The transgranular cracks indicated that failure was due partly to stress-corrosion. It was concluded that the chlorides provided the main corrodent for both the stress and intercrystalline-corrosion cracking.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001083
EISBN: 978-1-62708-214-3
... Abstract Copper alloy (C83600) impellers from two different feed pumps that supplied water to a 2-year-old boiler failed repeatedly. Examination by various methods indicated that the failures were caused by sulfide attack that concentrated in shrinkage voids in the castings. Two alternatives...
Abstract
Copper alloy (C83600) impellers from two different feed pumps that supplied water to a 2-year-old boiler failed repeatedly. Examination by various methods indicated that the failures were caused by sulfide attack that concentrated in shrinkage voids in the castings. Two alternatives to prevent future failures were recommended: changing the impeller composition to a cast stainless steel, or implementing stricter nondestructive evaluation requirements for copper alloy castings.
Book Chapter
Failure of Bearings Because of Wear of Labyrinth Seals
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047998
EISBN: 978-1-62708-225-9
... in the inner-ring raceway which had been softened by the elevated temperatures reached during the failure. Broken retainers and worn and bent out of shape seals were found. Penetration of gritty particles, water and other corrosive agents and leakage of lubricant out of the bearing permitted by the worn seals...
Abstract
The drive-shaft hanger bearings failed after 300 to 400 h in service. The shaft, supported by labyrinth-sealed single row radial ball bearings of ABEC-1 tolerances, was made of aluminum 2024-T3 tubing (2.5 cm diam and 1.2 mm wall thickness). The bearings were lubricated with a paste-type mineral-oil lubricant (containing molybdenum disulfide and polytetrafluoroethylene particles) or grease conforming to MIL-G-81322 (containing thickening agent and synthetic hydrocarbons) and had two-piece spot-welded retainers. On visual examination, the balls were observed to be embedded in the inner-ring raceway which had been softened by the elevated temperatures reached during the failure. Broken retainers and worn and bent out of shape seals were found. Penetration of gritty particles, water and other corrosive agents and leakage of lubricant out of the bearing permitted by the worn seals was observed. It was concluded that overheating was caused by lubricant flow was permitted by wear of the labyrinth seals. Positive rubbing seals and MIL-G-81322 grease lubricant were found to have longer life than those with the labyrinth seals and mineral-oil-paste lubricant on testing under simulated environmental conditions and were installed as a corrective measure. Importance of dirt free supply and drainage of oil was discussed.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001808
EISBN: 978-1-62708-241-9
... experienced multiple failures after only 8 months of service. The 24 in. (61 cm) pipeline supplied brackish water to a water treatment overflow reservoir used to house sewage when the treatment facility experienced overload. The pipeline operated on at least a weekly basis or when there was a heavy rainfall...
Abstract
Six cases of failure attributed to microbiologically influenced corrosion (MIC) were analyzed to determine if any of the failures could have been avoided or at least predicted. The failures represent a diversity of applications involving typical materials, primarily stainless steel and copper alloys, in contact with a variety of liquids, chemistries, and substances. Analytical techniques employed include stereoscopic examination, energy dispersive x-ray spectroscopy (EDS), temperature and pH testing, and metallographic analysis. The findings indicate that MIC is frequently the result of poor operations or improper materials selection, and thus often preventable.
Book Chapter
Single-Phase Erosion Corrosion of a 460 mm (18 in.) Diam Feedwater Line Break
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001065
EISBN: 978-1-62708-214-3
..., corrosion Pipe, corrosion Pumps Water supply ASTM A106 grade B UNS K03006 Erosion - corrosion Background A 460 mm (18 in.) diam suction line to the main feedwater pump for a nuclear power plant failed in a catastrophic manner. The failure was so violent that large section ofpipe was found...
Abstract
A 460 mm (18 in.) diam suction line to the main feed water pump for a nuclear power plant failed in a violent, catastrophic manner. Samples of pipe, elbow, and weld materials (ASTM A106 grade B carbon steel, ASTM A234 grade WPB carbon steel, and E7018 carbon steel electrode, respectively) from the suction line were analyzed. Evidence of overall thinning of the elbow and pipe material and ductile tearing of fractures indicated that the feed water pipe failed as a result of an erosion corrosion mechanism, which thinned the wall sufficiently to cause rapid, ductile tearing of the material after its design stress had been exceeded. It was recommended that steel with a higher chromium content be used to mitigate the erosion corrosion potential in the lines and that more rigorous nondestructive (ultrasonic) examinations be performed.
Book Chapter
Rapid Pitting Failure of Type 304 Stainless Steel Pipework
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001064
EISBN: 978-1-62708-214-3
.... This covered a total period of 5 months. All pipework was hydrotested using untreated borehole water supplied to the site through 17 km (11 mi), 115 mm (4.5 in.) diam carbon steel pipework. The borehole water was resident in the pipelines for 2 months, but no water quality/corrosion monitoring was undertaken...
Abstract
Several hundred leaks were reported in the type 304 stainless steel pipelines, vessels, and tanks of a chemical plant at a tropical location within a few weeks after startup. Investigation of the failure involved a site visit, metallographic examination and analysis of the material, analysis of hydrotest waters, and microbiological examination of slime that had formed in certain pipework sections. It was determined that the failure resulted from microbially induced corrosion promoted by the use of poor-quality hydrotest water and uncontrolled hydrotesting practice. Use of appropriate hydrotesting procedures was recommended to prevent similar failures.
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