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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001551
EISBN: 978-1-62708-233-4
.... It was found that the natural frequency of the wheel truing device was the culprit. A tuned damped absorber was designed and built to modify the resonance. This eliminated the problem. Grinding machines Printing press rolls Shafts (power) Vibration analysis Structural steel Fatigue fracture...
Abstract
A multi-million dollar, four-color printing press used to produce a major weekly magazine was breaking pinions (shouldered shafts) on rolls. The cause of fracture was cyclic fatigue. Steel quality and heat treatment met expected standards. The pinion fracture showed multiple origins indicating rotational vibration fatigue. Keeping bolts tight solved this problem. In another case, grinding machines were unable to produce surfaces of uniform quality and smoothness on steel bearing products. Measurements showed that self-excited vibrations were created when particular steels were ground. It was found that the natural frequency of the wheel truing device was the culprit. A tuned damped absorber was designed and built to modify the resonance. This eliminated the problem.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001578
EISBN: 978-1-62708-233-4
... Abstract Vibration analysis can be used in solving both rotating and nonrotating equipment problems. This paper presents case histories that, over a span of approximately 25 years, used vibration analysis to troubleshoot a wide range of problems. Current testing Fans Generators Motors...
Abstract
Vibration analysis can be used in solving both rotating and nonrotating equipment problems. This paper presents case histories that, over a span of approximately 25 years, used vibration analysis to troubleshoot a wide range of problems.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046418
EISBN: 978-1-62708-234-1
... Abstract Equipment in which an assembly of in-line cylindrical components rotated in water at 1040 rpm displayed excessive vibration after less than one hour of operation. The malfunction was traced to an aluminum alloy 6061-T6 combustion chamber that was part of the rotating assembly. Analysis...
Abstract
Equipment in which an assembly of in-line cylindrical components rotated in water at 1040 rpm displayed excessive vibration after less than one hour of operation. The malfunction was traced to an aluminum alloy 6061-T6 combustion chamber that was part of the rotating assembly. Analysis (visual inspection, 100x/500x/800x micrographic examination, spectrographic analysis, and hardness testing) supported the conclusions that, as a result of improper heat treatment, the combustion-chamber material was too soft for successful use in this application. Misalignment of the combustion chamber and one or both of the mating parts resulted in eccentric rotation and the excessive vibration that caused malfunction of the assembly. Irregularities in the housing around the combustion chamber and temperature variation relating to the combustion pattern in the chamber were considered to be possible contributing factors to localization of the cavitation erosion. Recommendations included adopting inspection procedures to ensure that the specified properties of aluminum alloy 6061-T6 were obtained and that the combustion chamber and adjacent components were aligned within specified tolerances. In a similar situation, consideration should also be given to raising the pressure in the coolant in order to suppress the formation of cavitation bubbles.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001851
EISBN: 978-1-62708-241-9
... bearings machine fault misalignment structural materials vibration wear vibration analysis stiffness damping coefficient inertia steel (steel, general) Introduction A spinning system serves as a model for many rotating machinery elements. It is generally composed of a flexible shaft...
Abstract
Shaft misalignment and rotor unbalance contribute to the premature failure of many machine components. To understand how these failures occur and quantify the effects, investigators developed a model of a rotating assembly, including a motor, flexible coupling, driveshaft, and bearings. Equations of motion accounting for misalignment and unbalance were then derived using finite elements. A spectral method for resolving these equations was also developed, making it possible to obtain and analyze dynamic system response and identify misalignment and unbalance conditions.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0048169
EISBN: 978-1-62708-233-4
... to have originated in the 0.38-mm radius fillet between the tab and the body of the washer. It was interpreted from the analysis of the compound fracture that it was composed of fatigue fractures caused by the formed tab being loaded so as to compress the spring along the axis of its centerline...
Abstract
A valve-seat retainer spring (made of 0.23 mm thick 17-7 PH stainless steel) from a fuel control on an aircraft engine was found to be broken after 3980 h of service. The two inner tabs were found to be broken off. The part was revealed to be in relative rotation against its contacting member by the radial wear marks on the convex surface. Beach marks indicating that fatigue fracture had been initiated at the convex surface of the washer and had propagated across to the concave surface were revealed by examination of the fractured surfaces of the washer. The cracks were revealed to have originated in the 0.38-mm radius fillet between the tab and the body of the washer. It was interpreted from the analysis of the compound fracture that it was composed of fatigue fractures caused by the formed tab being loaded so as to compress the spring along the axis of its centerline and produce torsional vibrations. It was concluded that the two inner tabs had broken in fatigue as the result of cyclic loading that compressed and torsionally vibrated the spring. The fillets were replaced with slots to minimize stress concentration at the corners as a corrective measure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047059
EISBN: 978-1-62708-217-4
...). Considerable vibration was created in the installation because of the design of the mechanical device used to transmit power to the governor. The pins were permitted to slide axially a small distance. Analysis (visual inspection, microscopic examination, and ductility measurements) supported the conclusion...
Abstract
The governor on an aircraft engine failed and upon disassembly of the unit, it was discovered that the retainer for the flyweight pivot pins was broken. The channel-shaped retainer was made of 0.8 mm (0.030 in.) thick 1018 or 1020 steel. The part was plated with copper, which acted as a stop-off during carburizing of the offset, circular thrust-bearing surface surrounding the 16-mm (0.637-in.) diam hole. The bearing surface was case hardened to a depth of 0.05 to 0.1 mm (0.002 to 0.005 in.), then austempered to obtain a minimum hardness of 600 Knoop (1-kg, or 2.2-lb, load). Considerable vibration was created in the installation because of the design of the mechanical device used to transmit power to the governor. The pins were permitted to slide axially a small distance. Analysis (visual inspection, microscopic examination, and ductility measurements) supported the conclusion that failure of the retainer was the result of fatigue caused by vibration in the flyweight assembly. Impact of the pivot pins on the retainer also contributed to failure. Recommendations included redesign of the flyweight assembly, and replacement of the channel-shaped retainer with a spring-clip type of pin retainer.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001842
EISBN: 978-1-62708-241-9
... Abstract A felt guide roll fractured in-service on a paper manufacturing machine, damaging the belt as well as multiple dryer rolls, nearby felt guide rolls, and the frame of the machine. The investigation included visual and stereoscopic examination, chemical and microstructural analysis...
Abstract
A felt guide roll fractured in-service on a paper manufacturing machine, damaging the belt as well as multiple dryer rolls, nearby felt guide rolls, and the frame of the machine. The investigation included visual and stereoscopic examination, chemical and microstructural analysis, microhardness and tensile testing, stress calculations, and vibration measurements. Based on the results, the roll fracture was attributed to high-cycle fatigue associated with a plug weld over one of the five threaded fasteners added to secure a balance weight inside the roll. The balance weight was installed to compensate for variations in wall thickness (i.e., weight distribution) of the pipe product used to make the roll. According to the investigation, resonance and vibration, which were initially considered, did not cause the failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0046242
EISBN: 978-1-62708-236-5
... Abstract An integral coupling and gear (Cr-Mo steel), used on a turbine-driven main boiler-feed pump, was removed from service after one year of operation because of excessive vibration. Spectrographic analysis and metallographic examination revealed the fact that gritty material in the gear...
Abstract
An integral coupling and gear (Cr-Mo steel), used on a turbine-driven main boiler-feed pump, was removed from service after one year of operation because of excessive vibration. Spectrographic analysis and metallographic examination revealed the fact that gritty material in the gear teeth (found at visual inspection) was composed of the same material as the metal in the coupling. Beach marks and evidence of cold work, typical of fatigue failure, were found on the fracture surface. Chips remaining in the analysis cut were difficult to remove, indicating a strong magnetic field in the part. Evidence found supports the conclusions that failure of the coupling was by fatigue and that incomplete demagnetization of the coupling following magnetic-particle inspection caused retention of metal chips in the roots of the teeth. Improper lubrication caused gear teeth to overheat and spall, producing chips that eventually overstressed the gear, causing failure. Because the oil circulation system was not operating properly, metal chips were not removed from the coupling. Recommendations included checking the replacement coupling for residual magnetism and changing or filtering the pump oil to remove any debris.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001828
EISBN: 978-1-62708-241-9
..., centrifugal stresses, and stresses due to vibrations imposed during operation. A finite-element (FE) stress analysis was carried out using a three-dimensional cuboid element to establish the stresses induced in the journal due to the following conditions. Shrink Fit and Centrifugal Stresses...
Abstract
A heat transport pump in a heavy water reactor failed (exhibiting excessive vibration) during a restart following a brief interruption in coolant flow due to a faulty valve. The pump had developed a large crack across the entire length of a bearing journal. An investigation to establish the root cause of the failure included chemical and metallurgical analysis, scanning electron fractography, mechanical property testing, finite element analysis of the shrink fitted journal, and a design review of the assembly fits. The journal failure was attributed to corrosion fatigue. Corrective actions to make the journals less susceptible to future failures were implemented and the process by which they were developed is described.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001139
EISBN: 978-1-62708-221-1
... to minimize the number of accidents and lessen the number of lawsuits? A company can do the following: Pay careful attention to detail design, Conduct a thorough design analysis, stress analysis, fatigue and fracture analysis, vibration analysis, etc., Conduct appropriate tests, Conduct...
Abstract
A truck-mounted hydraulic crane had a horizontal thrust bearing with one race attached to the truck and the other to the rotating crane. The outside race of the bearing was driven by a pinion gear, and it is through this mechanism that the crane body rotated about a vertical axis. The manufacturer welded the inner race to the carrier in a single pass. After several years of service, the attachment weld between the bearing inner race and the turntable failed in the area adjacent to the heat-affected zone. The fracture zone where there was the greatest tension was heavily oxidized. In the zone where the bearing was in compression, there was a clean surface indicating recent fracture. Finally, there were areas where the weld did not meet AWS specifications for convexity or concavity. These areas were weak enough to allow fatigue cracks to initiate. Recommendations to prevent reoccurrence of the failure include the use of bolts in lieu of welding, a welding schedule that reduces the propensity of lamellar tearing, and the use of an alloy that precludes lamellar tearing. However, if abuse of the crane was the primary cause of failure, none of these recommendations would have prevented deterioration of the machine to an extent that would have rendered the failure improbable.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001162
EISBN: 978-1-62708-220-4
... such as electrolytic and hand polishing and the vibration method resulted in poor edge and crack edge definition due to material thickness. Etching experiments involved a grain surface attack and hence produced a rather strong surface relief from which the grain boundary cracks could again not clearly...
Abstract
Some 99.90 pure tin tubes (0.15 mm thick) used for packaging a chemical compound cracked on bending and underwent brittle fracture prior to filling, while others remained ductile and showed no sign of failure. Examination showed that specimens prepared by mechanical methods such as electrolytic and hand polishing and the vibration method resulted in poor edge and crack edge definition due to material thickness. Etching experiments involved a grain surface attack and hence produced a rather strong surface relief from which the grain boundary cracks could again not clearly be differentiated. The sections were therefore examined unetched in polarized light. The microstructure of the cracked tubes was shown to have much smaller grains than the ductile and showed cracks from the surface down along the grain boundaries. Material hardness also differed between the unusable tubes and the ductile, and chemical analysis showed a higher level of aluminum in the brittle specimens. Failure obviously occurred due to the high material aluminum content that increased hardness which then caused embrittlement at the surface which led to cracks or fracture on bending. Since no explanation of how the aluminum entered the tin was available, no recommendations could be made.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001767
EISBN: 978-1-62708-241-9
... using optical and scanning electron microscopy, Fourier transform infrared spectroscopy (FTIR), and thermogravimetric analysis (TGA). The exterior surfaces of all six brackets were alike and shared similar features, including witness marks, discoloration, mechanical deformation, and secondary cracking...
Abstract
Six transformer brackets failed in service, sending a group of three pole-mounted transformers to the ground below. The brackets were made from acrylonitrile-butadiene-styrene (ABS) resin and had been in service for more than 30 years. Remnants of the fractured brackets were analyzed using optical and scanning electron microscopy, Fourier transform infrared spectroscopy (FTIR), and thermogravimetric analysis (TGA). The exterior surfaces of all six brackets were alike and shared similar features, including witness marks, discoloration, mechanical deformation, and secondary cracking, along with crack networks. Both FTIR and TGA analyses indicated that the surface material was in a highly degraded state, likely due to weathering and thermal and ultraviolet exposure. This, in turn, led to the formation of cracks that propagated under the cyclic forces of vibration and wind. As the cracks grew larger, the weight of the transformer eventually overloaded the brackets, resulting in failure.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001028
EISBN: 978-1-62708-214-3
... Abstract Several AISI type 321 stainless steel welded oil tank assemblies used on helicopter engine systems began to leak in service. One failure, a fracture on the aft side of a spot weld, was submitted for analysis. SEM fractography examination revealed fatigue failure. The failure initiated...
Abstract
Several AISI type 321 stainless steel welded oil tank assemblies used on helicopter engine systems began to leak in service. One failure, a fracture on the aft side of a spot weld, was submitted for analysis. SEM fractography examination revealed fatigue failure. The failure initiated at an overload fracture near the root of the weld and was followed by mode III fatigue crack propagation (tearing) around the periphery of the weld. The initial overload fracture was caused by a high external load, which produced a concentrated stress and fracture at the weld root. The subsequent fatigue fracture was caused by engine vibrations during operation of the aircraft. Fracture characteristics indicated that the fatigue would not have occurred if the initial damage had not taken place.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001052
EISBN: 978-1-62708-214-3
... Abstract A failure analysis was conducted to determine the cause of recurring failure of flexible bellows in an exhaust hose assembly. The bellows were made of type 321 stainless steel. Visual examination showed that cracks followed a path along the seam weld in the bellows. Most of the cracks...
Abstract
A failure analysis was conducted to determine the cause of recurring failure of flexible bellows in an exhaust hose assembly. The bellows were made of type 321 stainless steel. Visual examination showed that cracks followed a path along the seam weld in the bellows. Most of the cracks followed a multidirectional/circular pattern, occasionally chipping off the convolutions, an indication of high-resonance fatigue-type cracking. Scanning electron fractography showed fatigue striations throughout the fracture surface. The microstructure consisted of relatively large grains and an abnormal degree of titanium-base stringers. Wall thickness was about 0.15 mm (0.006 in.) underside. It was concluded that the high vane pass frequency excited the natural vibration of the bellows to a higher resonance and cracked the bellows after a relatively short service period. The assembly was redesigned, and no further cracking occurred.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001082
EISBN: 978-1-62708-214-3
... that the natural frequency of the impeller was coincident with the vortex-shedding frequency of the impeller by virtue of its design. The vibration of the impeller caused fluctuating fatigue loads. Computer analysis revealed that the highest stressed area of the impeller was at the leading edge of the impeller...
Abstract
Several large-diameter type 304L stainless steel impeller/propeller blades in a circulating water pump failed after approximately 8 months of operation. The impeller was a single casting that had been modified with a fillet weld buildup at the blade root. Visual examination indicated that the fracture originated near the blade-to-hub attachment in the area of the weld buildup. Specimens from four failed castings and from an impeller that had developed cracks prior to design modification were subjected to a complete analysis. A number of finite-element-method computer models were also constructed. It was determined that the blades failed by fatigue that had been accelerated by stress-corrosion cracking. The mechanism of failure was flow-induced vibration, in which the vortex-shedding frequencies of the blades were attuned to the natural frequency of the blade/hub configuration. A number of solutions involving material selection and impeller redesign were recommended.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001091
EISBN: 978-1-62708-214-3
... source would be torsional vibration caused by power surges during service. The presence of vibrational stresses, a high-frequency source, would explain the short service life of the shaft. Selected References Selected References • Wulpi D.J. , Failures of Shafts , Failure Analysis...
Abstract
An ASTM A193-83a grade B7 (AISI 4140) steel turbine impeller shaft fractured after 2 months of service. Failure had initiated at three separate points around the periphery of the shaft, each associated with one of three keyways. SEM fractography, metallography, and chemical analysis indicated that the mechanism of fracture initiation was torsional fatigue. Intermittent deceleration and acceleration resulting from power surges during operation of the turbine caused torsional vibration and was considered the most probable source of the required cyclic stress. Final failure took place by torsional shear.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001366
EISBN: 978-1-62708-215-0
... analysis indicated that the fatigue loading probably had been caused by forced excitation, resulting in the impeller vibrating at its resonant frequency. It was recommended that the impeller design, control systems, and material of construction be changed. Airfoils Turbines Vanes 7075-T6 AMS 4126...
Abstract
An AMS 4126 (7075-T6) aluminum alloy impeller from a radial inflow turbine fractured during commissioning. Initial examination showed that two adjacent vanes had fractured through airfoils in the vicinity of the vane leading edges, and one vane fractured through an airfoil near the hub in the vicinity of the vane trailing edge. Some remaining vanes exhibited radial and transverse cracks in similar locations. Binocular and scanning electron microscope examinations showed that the cracks had been caused by high-cycle fatigue and had progressed from multiple origins on the vane surface. Structural analysis indicated that the fatigue loading probably had been caused by forced excitation, resulting in the impeller vibrating at its resonant frequency. It was recommended that the impeller design, control systems, and material of construction be changed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001545
EISBN: 978-1-62708-236-5
.... A more thorough analysis showed failure was caused by tube vibration. In a third case, a type 304 stainless steel bellows in a test loop was thought to have failed because of chloride stress corrosion. The report concluded with a recommendation that carbon steel be used as an alternative bellows material...
Abstract
The presence of secondary, branching intergranular stress-corrosion cracking in a type 440C stainless bearing caused the analyst to overlook the real culprit, which was a mechanically-initiated, primary transgranular crack that propagated through the steel's hard chromium carbide. Failure was actually caused by overload. Had the original conclusion been accepted, a relatively exotic alloy would have been specified. In another case, brass heat exchanger tube failure was automatically attributed to attack by an acidic cleaner, and a decision was made to stop using the solution. A more thorough analysis showed failure was caused by tube vibration. In a third case, a type 304 stainless steel bellows in a test loop was thought to have failed because of chloride stress corrosion. The report concluded with a recommendation that carbon steel be used as an alternative bellows material. Caustic, not chloride, stress corrosion was the culprit. Had material substitutions been made on the original premise of countering chloride stress corrosion, most of the loop's highly stressed components would have eventually failed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001617
EISBN: 978-1-62708-227-3
... Abstract Failures of various types of hydraulic couplings used to connect pipes in a naval vessel are described and used to illustrate some of the general procedures for failure analysis. Cracking of couplings, which were manufactured from nickel-aluminum- bronze extruded bar, occurred in both...
Abstract
Failures of various types of hydraulic couplings used to connect pipes in a naval vessel are described and used to illustrate some of the general procedures for failure analysis. Cracking of couplings, which were manufactured from nickel-aluminum- bronze extruded bar, occurred in both seawater and air environments. Cracks initiated at an unusually wide variety of sites and propagated in either longitudinal or circumferential directions with respect to the axis of the couplings. Fracture surfaces were intergranular and exhibited little or no sign of corrosion (for couplings cracked in air), and there was very limited plasticity. Macroscopic progression markings were observed on fracture surfaces of several couplings but were not generally evident. At very high magnifications, numerous slip lines, progression markings, and striations were observed. In a few cases, where complete separation had occurred in service, small areas of dimpled overload fracture were observed. It was concluded from these observations, and from comparisons of cracks produced in service with cracks produced by laboratory testing under various conditions, that cracking had occurred by fatigue. The primary cause of failure was probably the unanticipated presence of high-frequency stress cycles with very low amplitudes, possibly due to vibration, resonance, or acoustic waves transmitted through the hydraulic fluid. Secondary causes of failure included the presence of high tensile residual stresses in one type of coupling, undue stress concentrations at some of the crack-initiation sites, and overtorquing of some couplings during installation. Recommendations on ways to prevent further failures based on these causes are discussed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0046371
EISBN: 978-1-62708-234-1
... any stainless steel from the spacer. Other items for investigation were the nature of the bond between the galled spot and the inner cone and any evidence of overtempering or rehardening resulting from localized overheating. Analysis (visual inspection, electron probe x-ray microanalysis, microscopic...
Abstract
When a roller-bearing assembly was removed from an aircraft for inspection after a short time in service, several areas of apparent galling were noticed around the inside surface of the inner cone of the bearing. These areas were roughly circular spots of built-up metal. The bearing had not seized, and there was no evidence of heat discoloration in the galled areas. The inner cone, made of modified 4720 steel and carburized for wear resistance, rode on an AISI type 630 (17-4 PH) stainless steel spacer. Consequently, it was desirable to determine whether the galled spots contained any stainless steel from the spacer. Other items for investigation were the nature of the bond between the galled spot and the inner cone and any evidence of overtempering or rehardening resulting from localized overheating. Analysis (visual inspection, electron probe x-ray microanalysis, microscopic examination, and hardness testing) supported the conclusions that galling had been caused by a combination of local overload and abnormal vibration of mating parts of the roller-bearing assembly. No recommendations were made.
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