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UNS S43100

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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0091475
EISBN: 978-1-62708-225-9
... (visual inspection and 2400x/6600x TEM analysis) supported the conclusion that failure was caused by hydrogen embrittlement, not SCC as might have been suspected. No recommendations were made. Cleavage Fractographs Stress corrosion cracking 431 UNS S43100 Hydrogen damage and embrittlement...
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0048616
EISBN: 978-1-62708-217-4
... Intergranular precipitation Shot peening 431 UNS S43100 Stress-corrosion cracking The T-bolt shown in Fig. 1(a) was part of the coupling for a bleed air duct of a jet engine on a transport plane. Specifications required that the 4.8-mm ( 3 16 -in.) diam T-bolt be made of AISI type 431...