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UNS S30900
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046915
EISBN: 978-1-62708-232-7
... metals Strip mills 309 UNS S30900 High-temperature corrosion and oxidation Intergranular corrosion Severe reduction of wall thickness was encountered at the liquid line of a lead-bath pan ( Fig. 1 ) that was used in a continuous strip or wire oil-tempering unit. Replacement of the pan...
Abstract
Severely reduced wall thickness was encountered at the liquid line of a lead-bath pan that was used in a continuous strip or wire oil-tempering unit. Replacement of the pan was necessary after six months of service. The pan, 6.9 m (22.5 ft) long, 0.6 m (2 ft) wide, and 38 cm (15 in.) deep with a 2.5-cm (1-in.) wall thickness, was a type 309 stainless steel weldment. Operating temperatures of the lead bath in the pan ranged from 805 deg C (1480 deg F) at the entry end to 845 deg C (1550 deg F) at the exit end. Analysis (visual inspection. metallographic analysis, moisture testing, and etched micrographs using Murakami's reagent) supported the conclusions that thinning of the pan walls at the surface of the molten lead resulted from using coke of high moisture content and from the low fluctuating coke level. Recommendations included reducing the supply of oxygen attacking the grain boundaries and the hydrogen that readily promoted decarburization with the use of dry (2 to 3% moisture content) coke. Maintaining a thick layer of coke over the entire surface of molten lead in the pan would exclude atmospheric oxygen from the grain boundaries.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001049
EISBN: 978-1-62708-214-3
.... Deep corrosion fissures then developed at hot crack sites as a result of crevice corrosion. Use of the appropriate overlay material was recommended. Claddings, corrosion Wood products 309 UNS S30900 Crevice corrosion Surface treatment related failures Background Routine inspections...
Abstract
Routine inspections of a carbon steel wood pulp digester revealed a sharply increasing number of cracks in the overlay metal on the internal surface of the digester after 1 and 2 years of service. The weld overlay was composed of type 309 stainless steel on the top fourth of the digester and of a proprietary high-nickel material on the bottom three-fourths. Examination revealed three distinct modes of deterioration. General corrosion was linked to the use of unspecified overlay metal. Cracking resulted during installation from the use of a material susceptible to hot cracking. Deep corrosion fissures then developed at hot crack sites as a result of crevice corrosion. Use of the appropriate overlay material was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001046
EISBN: 978-1-62708-214-3
... UNS S30900 Incoloy 800 UNS N08800 Inconel 625 UNS N06625 Inconel 600 UNS N06600 Inconel C-276 UNS N10276 High-temperature corrosion and oxidation Background The thin plates within a type 309 stainless steel chlorinated solvent combustion preheater/heat exchanger showed severe...
Abstract
The thin plates within a type 309 stainless steel chlorinated solvent combustion preheater/heat exchanger designed to process fumes from a solvent coating process showed severe corrosion within 6 months of service. Within a year corrosion had produced holes in the plates, allowing gases to shunt across the preheater/exchanger. Metallographic examination of the plates showed that accelerated internal oxidation had been the cause of failure. Corrosion racks of candidate alloys (types 304, 309, and 316 stainless steels, Inconel 600, Inconel 625, Incoloy 800, Incoloy 825, and Inco alloy C-276) were placed directly in the hot gas stream, containing HCl and Cl2, for in situ testing. Results of this investigation showed that nickel-chromium corrosion-resistant alloys, such as Inconel 600, Inconel 625, and Inco alloy C-276, performed well in this environment. Laboratory testing of the same alloys, along with Inconel alloys 601, 617, and 690 and stainless steel type 347 was also conducted in a simulated waste incinerator nitrogen atmosphere containing 10% Co2, 9% O2, 4% HCl, 130 ppm HBr and 100 ppm SO2 at 595, 705, 815, and 925 deg C (1100, 1300,1500, and 1700 deg F). The tests confirmed the suitability of the nickel-chromium alloys for such an environment. Inconel 625 was selected for fabrication of a new preheater/exchanger.