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UNS R56406
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c9001573
EISBN: 978-1-62708-226-6
.... Arcing Pitting (wear) Surgical implants Wire Ti-6Al-4V Titanium nitride coating UNS R56406 Surface treatment related failures (Other, miscellaneous, or unspecified) wear Background The TiN coated back surgery wires were made of Ti6A14V. The reported failure was the presence of pits...
Abstract
TiN coated back surgery wires were made of Ti-6Al-4V. The reported failure was the presence of pits located in the uncoated area of the wires. The uncoated area of the wire is where the wire is fixtured in the coating chamber during coating. Examination and analysis of the pits using SEM/EDX detection unit revealed significant peaks of B, O, Zr and Fe. Moreover, the shape of the pits was similar to an arc crater. The formation of pits in the wire was caused during coating due to microarcing. A contaminated fixture used during the coating most likely caused the microarcing.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0047681
EISBN: 978-1-62708-229-7
... current to reduce the temperature, by an increase in the electrode force, or both. Compressors Gas turbine engines Welding parameters Ti-6Al-4V UNS R56406 Joining-related failures Fatigue fracture A fluorescent liquid-penetrant inspection of an experimental stator vane of a first-stage...
Abstract
A fluorescent liquid-penetrant inspection of an experimental stator vane of a first-stage axial compressor revealed the presence of a longitudinal crack over 50 mm (2 in.) long at the edge of a resistance seam weld. The vane was made of titanium alloy Ti-6Al-4V (AMS 4911). The crack was opened by fracturing the vane. The crack surface displayed fatigue beach marks emanating from the seam-weld interface. Both the leading-edge and trailing-edge seam welds exhibited weld-metal expulsions up to 3.6 mm (0.14 in.) in length. Metallographic examination confirmed that metal expulsion from the resistance welds was generally present. The stator vane failed by a fatigue crack that initiated at internal surface discontinuities caused by metal expulsion from the resistance seam weld used in fabricating the vane. Expulsion of metal from seam welds should be eliminated by a slight reduction in welding current to reduce the temperature, by an increase in the electrode force, or both.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047641
EISBN: 978-1-62708-235-8
... contamination. Contaminants Gas tungsten arc welding Heat affected zone Oxygen Stress concentration Thermal stresses Ti-6Al-4V UNS R56406 Joining-related failures A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The pressure vessel...
Abstract
A Ti-6Al-4V alloy pressure vessel failed during a proof-pressure test, fracturing along the center girth weld. The girth joints were welded with the automatic gas tungsten arc process utilizing an auxiliary trailing shield attached to the welding torch to provide inert-gas shielding for the exterior surface of the weld. A segmented backup ring with a gas channel was used inside the vessel to shield the weld root. The pressure vessel failed due to contamination of the fusion zone by oxygen, which resulted when the gas shielding the root face of the weld was diluted by air that leaked into the gas channel. Thermal stresses cracked the embrittled weld, exposing the crack surfaces to oxidation before cooling. One of these cracks caused a stress concentration so severe that failure of the vessel wall during the proof test was inevitable. A sealing system at the split-line region of the segmented backup ring was provided, and a fine-mesh stainless steel screen diffuser was incorporated in the channel section of the backup ring to prevent air from leaking in. A titanium alloy color chart was furnished to permit correlation of weld-zone discoloration with the degree of atmospheric contamination.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091726
EISBN: 978-1-62708-217-4
.... Recommendations included revising the specification to require a minimum NO content of 0.6%. Nitrogen dioxide Pressure vessels Propellant tanks Ti-6Al-4V UNS R56406 Stress-corrosion cracking Nitrogen tetroxide, a storable hypergolic oxidizer, was used in the service propulsion system (SPS...
Abstract
In January 1965, a Reaction Control System (RCS) pressure vessel (titanium alloy Ti-6Al-4V) on an Apollo spacecraft cracked in six adjacent locations. It used N2O4 for vehicle attitude control through roll, pitch, and yaw engines, and was protected from the N2O4 by a Teflon positive expulsion bladder. Investigation (visual inspection, pressure testing of 10 similar vessels, and chemical testing of the N2O4) supported the conclusion that the failure was due to stress corrosion from the N2O4, and specifically from a specification change in the military specification MIL-P-26539. Recommendations included revising the specification to require a minimum NO content of 0.6%.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091727
EISBN: 978-1-62708-217-4
... in the imposition of a control specification (MF0004-018) for all fluids that contact titanium for existing and future space designs. Pressure Vessels Propellant tanks Surface pretreatments Ti-6Al-4V UNS R56406 Stress-corrosion cracking The storable hypergolic fuel used for the SPS on the Apollo...
Abstract
During an acceptance test of the Apollo spacecraft 101 service module prior to delivery, an SPS fuel pressure vessel (SN054) (titanium Ti-6Al-4V, approximately 1.2 m (4 ft) in diam and 3 m (10 ft) long) containing methanol developed cracks adjacent to the welds. The test was stopped. This acceptance test had been run 38 times on similar pressure vessels without problems. The methanol was a safe-fluid replacement for the storable hypergolic fuels (blend of 50% hydrazine and 50% unsymmetrical dimethyl hydrazine). Investigation (visual inspection and 65X images) showed similarities to stress-corrosion resulting from contamination during misprocessing of the vessels. However, another vessel underwent a more severe testing procedure and failed catastrophically. Further investigation supported the conclusion that the failure cause was SCC of titanium in methanol. Attack is promoted by crazing of the protective oxide film. It was learned that minor changes in the testing procedures could inhibit or accelerate the reaction. Recommendations included replacing the methanol with a suitable alternate fluid. Isopropyl alcohol was chosen after considerable testing. This incident further resulted in the imposition of a control specification (MF0004-018) for all fluids that contact titanium for existing and future space designs.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001782
EISBN: 978-1-62708-241-9
... club fracture atmospheric contamination titanium alloy cracking concentric grooves SEM/EDS analysis grain size Ti6Al4V (titanium-aluminum-vanadium alloy) UNS R56406 Introduction The relative low density, high strength, and corrosion resistance of titanium alloys make them well-suited...
Abstract
The head on a golf club driver developed multiple cracks during normal use. The head was a hollow shell construction made from a titanium alloy. Analysis and additional investigation revealed a progressive failure that initiated on the interior surface of the face plate along a deep, concentric groove created during a press forming operation. It was also determined that atmospheric contamination occurred during the welding of the head, causing embrittlement, which may have also contributed to the failure. Recommendations were made addressing the problems that were observed.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001030
EISBN: 978-1-62708-214-3
...). Control of machining parameters to prevent formation of brittle martensite, use of galvanically compatible fasteners, and use of an alternate lubricant were recommended. Airframes, corrosion Fasteners Jet planes Marine environments Military planes Solid lubricants Ti-6Al-4V UNS R56406 Stress...
Abstract
Cracks were discovered between interference-fit fasteners (MoS2-coated Ti-6Al-4V) that had been incorporated into a fighter aircraft primary structural frame (D6ac steel) to enhance structural fatigue life. Examination of sections cut from the cracked frame established that the cracks propagated by stress-corrosion cracking. The cause of cracking was twofold: use of interference-fit fasteners exposed to moisture intrusion from a marine environment and poor hole quality. Failure was intensified by dissimilar-metal contact in the presence of weak acidic electrolyte (dissociated MoS2). Control of machining parameters to prevent formation of brittle martensite, use of galvanically compatible fasteners, and use of an alternate lubricant were recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001649
EISBN: 978-1-62708-234-1
... at the time of re-torque and at the time of initial torque application several years earlier. Aerospace fasteners Fractography Ti-6Al-4V UNS R56406 Ductile fracture As in many industries, aerospace systems and components are subject to time-dependent degradation. The ongoing structural...
Abstract
Two titanium alloy wing attachment bolts from a commercial jetliner failed during the course of a routine service operation. Failure of the bolts occurred during the re-torque process as the wing was being reattached. Metallurgical failure analysis indicated that the fracture mechanism was ductile overload and that the mechanical properties of the bolts were consistent with exemplar bolts that had been supplied. After eliminating other sources of excessive load application, the most probable cause of failure was ascribed to variances between the frictional characteristics of the bolt at the time of re-torque and at the time of initial torque application several years earlier.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001660
EISBN: 978-1-62708-236-5
... are discussed along with potential methods to eliminate these microstructural in homogeneities. Shear bands Threaded fasteners Ti-6Al-4V UNS R56406 Ductile fracture Threaded Ti-6Al-4V fasteners are used extensively by the aerospace industry for joining structural components. One popular type...
Abstract
Failure analysis was performed on threaded Ti-6Al-4V fasteners that had fractured in the threads during installation. Scanning electron microscopy (SEM) and optical metallography revealed that the fractures initiated in circumferential shear bands present at the thread roots. The fractures propagated by microvoid coalescence typical of that observed in notched tensile specimen fractures of the same material. For comparison, Ti-6Al-4V fasteners from various commercial sources were tested to failure in uniaxial tension and examined in the SEM. In all cases, the fracture appearances were similar to that exhibited by the fasteners that failed during installation. In addition, results of optical microscopy indicated that the geometry and extent of the shear bands appeared to depend on the fabrication process employed by the individual manufacturers. Causes of shear band formation are discussed along with potential methods to eliminate these microstructural in homogeneities.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001803
EISBN: 978-1-62708-241-9
.... orthopedic implant devices fracture corrosion inclusions and stress gaps medical materials cracking fretting pitting fractography fracture toughness Ti6Al4V (titanium-aluminum-vanadium alloy) UNS R56406 316L stainless steel (austenitic wrought stainless steel) UNS S31603 Introduction...
Abstract
Metallurgical SEM analysis provides many insights into the failure of biomedical materials and devices. The results of several such investigations are reported here, including findings and conclusions from the examination a total hip prosthesis, stainless steel and titanium compression plates, and hollow spinal rods. Some of the failure mechanisms that were identified include corrosive attack, corrosion plus erosion-corrosion, inclusions and stress gaps, production impurities, design flaws, and manufacturing defects. Failure prevention and mitigation strategies are also discussed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001636
EISBN: 978-1-62708-217-4
... history could have been more severe than anticipated. This possibility was subsequently supported by a separate investigation of the assumed and actual fatigue loads and stresses. Rotor blade Ti-6Al-4V UNS R56406 Fatigue fracture Introduction On 10 November 1998, a Royal Netherlands Navy...
Abstract
A Lynx helicopter from the Royal Netherlands Navy lost a rotor blade during preparation for take-off. The blade loss was due to failure of a rotor hub arm by fatigue. The arm was integral to the titanium alloy rotor hub. An extensive material based failure analysis covered the hub manufacture, service damage, and estimates of service stresses. There was no evidence for failure due to poor material properties. However, fractographic and fracture mechanics analyses of the service failure, a full scale test failure, and specimen test failures indicated that the service fatigue stress history could have been more severe than anticipated. This possibility was subsequently supported by a separate investigation of the assumed and actual fatigue loads and stresses.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c9001690
EISBN: 978-1-62708-226-6
.... Corrosion Fracture mechanisms Metallic surgical implants Retrieval analysis Ti-6Al-4V UNS R56406 316L UNS S31603 ISO 5832-2 grade 1 Nitinol (Other, general, or unspecified) corrosion (Other, general, or unspecified) fracture Worldwide data indicate that approximately 100 million metallic...
Abstract
This paper summarizes several cases of metallurgical failure analysis of surgical implants conducted at the Laboratory of Failure Analysis of IPT, in Brazil. Investigation revealed that most of the samples were not in accordance with ISO standards and presented evidence of corrosion assisted fracture. Additionally, some components were found to contain fabrication/processing defects that contributed to premature failure. The implant of nonbiocompatible materials results in immeasurable damage to patients as well as losses for the public investment. It is proposed that local sanitary regulation agencies create mechanisms to avoid commercialization of surgical implants that are not in accordance with standards and adopt the practice of retrieval analysis of failed implants. This would protect the public health by identifying and preventing the main causes of failure in surgical implants.