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UNS K03006
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089734
EISBN: 978-1-62708-235-8
.... Fillet welds Flanges Headers Pipe fitting Stress concentration Superheaters Thermal stresses Weld defects ASTM A106 grade B UNS K03006 ASTM A105 grade 2 Fatigue fracture Joining-related failures A system of carbon steel headers, handling superheated water of 188 °C (370 °F) at 2 MPa (300...
Abstract
A system of carbon steel headers, handling superheated water of 188 deg C (370 deg F) at 2 MPa (300 psi) for automobile-tire curing presses, developed a number of leaks within about four months after two to three years of leak-free service. All the leaks were in shielded metal arc butt welds joining 200 mm (8 in.) diam 90 deg elbows and pipe to 200 mm (8 in.) diam welding-neck flanges. A flange-elbow-flange assembly and a flange-pipe assembly that had leaked were removed for examination. Investigation (visual inspection, hardness testing, chemical analysis, magnetic-particle testing, radiographic inspection, and 2% nital etched 1.7x views) showed varying IDs on the assemblies and supported the conclusions that the failures of the butt welds were the result of fatigue cracks caused by cyclic thermal stresses that initiated at stress-concentrating notches at the toes of the interior fillet welds on the surfaces of the flanges. Recommendations included using ultrasonic testing to identify the appropriate joints and then replacing them. Special attention to accuracy of fit-up in the replacement joints was also recommended to achieve smooth, notch-free contours on the interior surfaces.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001701
EISBN: 978-1-62708-219-8
... by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system. Water chemistry Water heaters Water pipelines Water treatment ASTM A106 UNS K03006 Crevice corrosion...
Abstract
A closed-loop hot water heating system at a museum in South Carolina was the subject of failure evaluation. The system consisted of plain carbon steel pipes (Schedule 40) made of ASTM A 106 or A 53 (ERW or seamless). The supply and return lines were made of the same materials. The fittings were mechanically threaded assemblies. Temperatures ranged from 150 to 155 deg F (65.6 to 68.3 deg C). Leaks in the system had reportedly initiated immediately after the building had been placed in service. The cause of corrosion inside the steel pipes was attributed to tuberculation caused by oxygen concentration cells and oxygen-pitting related corrosion. Both types of corrosion are due to the poor quality of the water and the lack of corrosion control in the water system.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001325
EISBN: 978-1-62708-215-0
... quality. Hydrogen sulfide Weld metal Welded joints UNS K03005 UNS K03504 UNS K03006 ASTM A53 grade B ASTM A105 ASTM A234 grade WPB Uniform corrosion High-temperature corrosion and oxidation Background Application This cross-tee was located in piping which conveyed concentrated H...
Abstract
A carbon steel piping cross-tee assembly which conveyed hydrogen sulfide (H7S) process gas at 150 to 275 deg C (300 to 585 deg F) with a maximum allowable operating pressure of 3 MPa (450 psig) ruptured at the toe of one of the welds at the cross after several years of service. The failure was initially thought to be the result of thermal fatigue, and the internal surfaces exhibited the “elephant hide” pattern characteristic of thermal fatigue. However metallographic failure analysis found that this pattern was the result of corrosion rather than thermal fatigue. Corrosion caused failure at this location because the weld was abnormally thin as fabricated. Thus, failure resulted from inadequate deposition of weld metal and subsequent wall thinning from internal corrosion. It was recommended that the cross-tee be replaced with a like component, with more careful attention to weld quality.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001534
EISBN: 978-1-62708-220-4
... startup, culminating in catastrophic failure as soon as the crack exceeded critical length. Ammonia Condenser tubes Refrigerating machinery Weld defects Welded joints API 5L B ASTM A234 grade WPB UNS K03006 Joining-related failures Intergranular fracture Hydrogen damage and embrittlement...
Abstract
A detailed failure analysis was conducted on an ammonia refrigerant condenser tube component that failed catastrophically during its initial hours of operation. Evidence collected clearly demonstrated that the weld between a pipe and a dished end contained a sharp unfused region at its root (lack of penetration). Component failure had started from this weld defect. The hydrogen absorbed during welding facilitated crack initiation from this weld defect during storage of the component after welding. Poor weld toughness at the low operating temperature facilitated crack growth during startup, culminating in catastrophic failure as soon as the crack exceeded critical length.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001065
EISBN: 978-1-62708-214-3
..., corrosion Pipe, corrosion Pumps Water supply ASTM A106 grade B UNS K03006 Erosion - corrosion Background A 460 mm (18 in.) diam suction line to the main feedwater pump for a nuclear power plant failed in a catastrophic manner. The failure was so violent that large section ofpipe was found...
Abstract
A 460 mm (18 in.) diam suction line to the main feed water pump for a nuclear power plant failed in a violent, catastrophic manner. Samples of pipe, elbow, and weld materials (ASTM A106 grade B carbon steel, ASTM A234 grade WPB carbon steel, and E7018 carbon steel electrode, respectively) from the suction line were analyzed. Evidence of overall thinning of the elbow and pipe material and ductile tearing of fractures indicated that the feed water pipe failed as a result of an erosion corrosion mechanism, which thinned the wall sufficiently to cause rapid, ductile tearing of the material after its design stress had been exceeded. It was recommended that steel with a higher chromium content be used to mitigate the erosion corrosion potential in the lines and that more rigorous nondestructive (ultrasonic) examinations be performed.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001314
EISBN: 978-1-62708-215-0
... Overheating Transgranular fracture Vaporizers ASTM A106 grade B UNS K03006 Thermal fatigue fracture Background A vaporizer installed in a foodstuffs industry processing plant failed three times in attempts to bring the system on line. A schematic flow chart illustrates the location...
Abstract
A gas-fired, ASTM A-106 Grade B carbon steel vaporizer failed on three different occasions during attempts to bring the vaporizer on line. Dye penetrant examination indicated the presence of multiple packets of ductile cracks on the inside of the coil radius at the bottom of the horizontal axis coils. Visual examination of the inside of the tubing indicated the presence of a carbonaceous deposit resulting from decomposition of the heat-exchanging fluid. Subsequent metallographic examination and microhardness testing indicated that the steel was heated to a temperature above the allowable operating temperature for the fluid. The probable cause for failure is thermal fatigue due to the localized overheating. Flow conditions inside the tubing should be reexamined to ensure suitable conditions for annular fluid flow.