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T.L. da Silveira, I. Le May
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P.G. Caceres, K. Habib
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UNS J94224
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Search Results for UNS J94224
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Book Chapter
Creep Damage in Welds of Reformer Furnace Tubing
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001735
EISBN: 978-1-62708-220-4
... showed the welds to be inadequate, and to have a strength and creep resistance below those of the base metal. Reformer furnaces Tubine Welded joints HK-40 UNS J94224 Creep fracture/stress rupture A sample tube was removed from a reformer furnace for life assessment after 69,000 h...
Abstract
A sample tube was removed from a reformer furnace for life assessment after 69,000 h of service. Sections were cut from the tube, which was a spindle cast A297 Grade HK 40 (25 Cr, 20 Ni, 0.4 C) austenitic steel of 122.5 mm OD and 10.5 mm nominal wall thickness. They were examined metallographically on transverse sections and on longitudinal sections through the butt welds joining the separate cast segments of the tube. Creep damage was mainly concentrated within the inner one third of the wall thickness. The use of damage assessment parameters in evaluating the reformer tube remaining life showed the welds to be inadequate, and to have a strength and creep resistance below those of the base metal.
Book Chapter
Failure Analysis of a Steam Reformer Tube
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001687
EISBN: 978-1-62708-220-4
... properties. Grain boundary sliding and dislocation motion were enhanced, causing a local increase in the steady state strain rate and the premature failure of the tube. Grain boundary sliding Plastic deformation Spalling Voids HK UNS J94224 Creep fracture/stress rupture The petrochemical...
Abstract
Microstructural examinations on transverse cross sections of a steam reformer tube, showed the presence of large macrovoids elongated in the radial direction and emanating from the internal surface of the tube. The macrovoids were located at the interdendritic regions, and were partially filled by a Mn-Fe bearing chromium oxide film. The areas adjacent to the oxide film were chemically depleted in C, Cr and Mn and rich in Fe and Ni. Associated with this depletion were a large concentration of microvoids. It was suggested that the dissolution of carbides in areas surrounding the macrovoids and the concentration of stresses at their tips, caused extensive localized plastic deformation which led to the formation of microvoids and subsequently to the spalling of the oxide film. The non-protective character of the film induced a progressive deterioration of the grain boundaries properties. Grain boundary sliding and dislocation motion were enhanced, causing a local increase in the steady state strain rate and the premature failure of the tube.