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UNS G10300
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.matlhand.c0048073
EISBN: 978-1-62708-224-2
...-radius fillet was machined at the change in section. Pinions Radii Stress concentration 1030 UNS G10300 Fatigue fracture A drum pinion shaft, part of the hoisting gear of an 18,140-kg (20-ton) capacity crane operating in a blooming mill, broke while the crane was lifting a 9070-kg (10-ton...
Abstract
A drum pinion shaft (1030 steel) which was part of the hoisting gear of a crane (capacity 18,140-kg) operating in a blooming mill failed while lifting a 9070 kg load. Chatter marks, rough-machining marks, and sharp corner radii were revealed in the keyway which extended into a shoulder at a change in diam. A circular recess below the keyway surface was revealed at each end of the keyway. A sharp corner at the end of the keyway was revealed by examination to be the origin of fracture. Beach marks were found radiating from the origin over a large portion of the fracture surface which confirmed failure of the shaft by fatigue fracture. As a corrective measure the shaft was replaced with one made of 4140 steel, quenched and tempered to a hardness of 286 to 319 HRB. The keyway was moved away from the change in section and was machined with a 1.6-mm radius in the bottom corners and a larger-radius fillet was machined at the change in section.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001779
EISBN: 978-1-62708-241-9
... steel shrinkage pits and voids scanning electron microscopy cavitation resistance C30 (low-carbon steel alloy) UNS G10300 ...
Abstract
Material samples collected from failed booster pumps were analyzed to determine the cause of failure and assess the adequacy of the materials used in the design. The pumps had been in service at a power plant, transporting feedwater from a deaerator to a main turbine boiler. Samples from critical areas of the pump were examined using optical and scanning electron microscopy, electrochemical analysis, and tensile testing. Based on microstructure and morphology, estimated corrosion rates, and particle concentrations in the feedwater, it was concluded that cavitation and erosion were the dominant failure mechanisms and that the materials and processes used to make the pumps were largely unsuited for the application.