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UNS A97075
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001541
EISBN: 978-1-62708-235-8
... proved the crack to be a forging defect called a cold shut. Because defects of this type are usually detected when the raw forging is inspected, this occurrence was considered to be an isolated instance. Cold shuts Cracking (fracturing) Forgings 7075-T6 UNS A97075 Metalworking-related failures...
Abstract
A forging of 7075-T6 aluminum alloy, which formed a support for the cylinder of a cargo door, cracked at an attachment hole. Fluorescent penetrant inspection showed the crack ran above and below the hole out onto the machined flat surface of the flange. A 6500x electron fractograph proved the crack to be a forging defect called a cold shut. Because defects of this type are usually detected when the raw forging is inspected, this occurrence was considered to be an isolated instance.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0091809
EISBN: 978-1-62708-217-4
... weeks. No recommendations were made. Bacterial corrosion Microbial induced corrosion 7075 UNS A97075 Biological corrosion An early case of MIC on aluminum was identified in aircraft wing tank failures in the 1950s. In this case, water condensed into the fuel tanks during flight led...
Abstract
Aluminum 7075 aircraft wing tanks failed in the 1950s. Investigation (visual inspection, biological analysis, and chemical analysis) supported the conclusion that MIC was the cause of the failures. Water condensed into the fuel tanks during flight led to microbial growth on the jet fuel. Pitting attack occurred under microbial deposits on the metal surface in the water phase or at the water-fuel interface. Previously, exposure of aluminum 7075 to cultures of various isolates showed that 27 bacterial isolates and 3 fungi could seriously corrode the aluminum alloy over several weeks. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006413
EISBN: 978-1-62708-217-4
... cracks which were present before the landing. It was recommended that an inspection for SCC be made of all pylon struts with a similar service life. Landing gear Scanning electron microscopy Stresses 7075 UNS A97075 Stress-corrosion cracking A pylon strut was submitted for failure...
Abstract
Examination of a 7075-T6 aluminum alloy pylon strut revealed cracks in two locations on the ears of the strut. Because the part was still intact, the cracks had to be forced open so that the fractures could be examined. Scanning electron microscopy (SEM) of the opened cracks showed that the crack surfaces were covered with a mud crack pattern suggestive of stress-corrosion cracking (SCC). The T6 temper is susceptible to SCC. It was concluded that cracking of the strut could have been aggravated by the hard landing experienced by the aircraft. The strut, however, contained stress-corrosion cracks which were present before the landing. It was recommended that an inspection for SCC be made of all pylon struts with a similar service life.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006387
EISBN: 978-1-62708-217-4
.... Accessories Aircraft components Scanning electron microscopy Swivels 7075 UNS A97075 Intergranular corrosion Stress-corrosion cracking A routine examination on a seat ejection system found that the catapult attachment swivel contained cracks on opposite sides of the part. This swivel, or bath tub...
Abstract
A routine examination on a seat ejection system found that the catapult attachment swivel fabricated from 7075-T651 aluminum alloy plate contained cracks on opposite sides of the part. This swivel, or bath tub, does not experience extreme loads prior to activation of the catapult system. Some loads could be absorbed however, when the aircraft is subjected to G loads. Visual examination of the part revealed that cracks through the wall thickness initiated on the inner walls of the fixture. Scanning electron microscopy (SEM) and electron optical examination revealed that the cracking pattern initiated and progressed by an intergranular failure mechanism. It was concluded that failure of the catapult attachment swivel fixture occurred by SCC. It was recommended that the 7075 aluminum ejection seat fixture be supplied in the T-73 temper to minimize susceptibility to SCC.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046146
EISBN: 978-1-62708-217-4
.... Aircraft components Forgings Landing gear 7075-T73 UNS A97075 Fatigue fracture The torque-arm assembly for an aircraft nose landing gear ( Fig. 1a ) failed after 22,779 simulated flights. The part, made from an aluminum alloy 7075-T73 forging, had an expected life of 100,000 simulated flights...
Abstract
The torque-arm assembly (aluminum alloy 7075-T73) for an aircraft nose landing gear failed after 22,779 simulated flights. The part, made from an aluminum alloy 7075-T73 forging, had an expected life of 100,000 simulated flights. Initial study of the fracture surfaces indicated that the primary fracture initiated from multiple origins on both sides of a lubrication hole that extended from the outer surface to the bore of a lug in two cadmium-plated flanged bushings made of copper alloy C63000 (aluminum bronze) that were press-fitted into each bored hole in the lug. Sectioning and 2x metallographic analysis showed small fatigue-type cracks in the hole adjacent to the origin of primary fracture. Hardness and electrical conductivity were typical for aluminum alloy 7075. This evidence supported the conclusion that the arm failed in fatigue cracking that initiated on each side of the lubrication hole since no material defects were found at the failure origin. Recommendations included redesign of the lubrication hole, shot peeing of the faces of the lug for added resistance to fatigue failure, and changing of the forging material to aluminum alloy 7175-T736 for its higher mechanical properties.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006402
EISBN: 978-1-62708-217-4
... (aircrafts) 7075 UNS A97075 Intergranular corrosion New aircraft wing panels extruded from 7075-T6 aluminum were reported to be discolored, exhibiting an unusual pattern of circular black interrupted lines ( Fig. 1a ). The black marks were coherent with the metal and could not be removed by scouring...
Abstract
New aircraft wing panels extruded from 7075-T6 aluminum exhibited an unusual pattern of circular black interrupted lines, which could not be removed by scouring or light sanding. The panels, subsequent to profiling and machining, were required to be penetrated inspected, shot peened, H2SO4 anodized, and coated with MIL-C-27725 integral fuel tank coating on the rib side. Scanning electron microscopy and microprobe analysis (both conventional energy-dispersive and Auger analyzers) showed that the anodic coating was applied over an improperly cleaned and contaminated surface. The expanding corrosion product had cracked and, in some places, had flaked away the anodized coating. The corrodent had penetrated the base aluminum in the form of subsurface intergranular attack to a depth of 0.035 mm (0.0014 in.). It was recommended that a vapor degreaser be used during cleaning prior to anodizing. A hot inhibited alkaline cleaner was also recommended during cleaning prior to anodizing. The panels should be dichromate sealed after anodizing. The use of deionized water was also recommended during the dichromate sealing operation. In addition, the use of an epoxy primer prior to shipment of the panels was endorsed. Most importantly, surveillance of the anodizing process itself was emphasized.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001298
EISBN: 978-1-62708-215-0
... by acid etching. Post-plating baking operations subsequently reduced the fatigue strength of the spar. Chemical etching Fatigue strength Mechanical properties Rotor blades 7075-T7351 UNS A97075 Pitting corrosion Fatigue fracture Surface treatment related failures Background...
Abstract
A helicopter tail rotor blade spar failed in fatigue, allowing the outer section of the blade to separate in flight. The 7075-T7351 aluminum alloy blade had fiberglass pockets. The blade spar was a hollow “D” shape, and corrosion pits were present on the inner surface of the hollow spar A single corrosion pit, 0.38 mm (0.015 in.) deep, led to a fatigue failure of the spar The failure initiated on the pylon side of the blade. Dimensional analysis of the spar near the failure revealed measurements within engineering drawing tolerances. Though corrosion pitting was present, there was an absence of significant amounts of corrosion product and all of the pits were filled with corrosion-preventative primer. This indicated that the pitting occurred during spar manufacture, prior to the application of the primer The pitting resulted from multiple nickel plating and defective plating removal by acid etching. Post-plating baking operations subsequently reduced the fatigue strength of the spar.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001366
EISBN: 978-1-62708-215-0
... UNS A97075 Fatigue fracture Background An AMS 4126 (7075-T6) aluminum alloy impeller from a radial inflow turbine fractured during commissioning. Applications The turbine is used to derive power at a natural gas letdown station. A finite-element model of the impeller is shown in Fig...
Abstract
An AMS 4126 (7075-T6) aluminum alloy impeller from a radial inflow turbine fractured during commissioning. Initial examination showed that two adjacent vanes had fractured through airfoils in the vicinity of the vane leading edges, and one vane fractured through an airfoil near the hub in the vicinity of the vane trailing edge. Some remaining vanes exhibited radial and transverse cracks in similar locations. Binocular and scanning electron microscope examinations showed that the cracks had been caused by high-cycle fatigue and had progressed from multiple origins on the vane surface. Structural analysis indicated that the fatigue loading probably had been caused by forced excitation, resulting in the impeller vibrating at its resonant frequency. It was recommended that the impeller design, control systems, and material of construction be changed.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047199
EISBN: 978-1-62708-234-1
... to an elevated-temperature quench to minimize exfoliation for 7075 forgings in the T6 temper. Forgings Grain structure Weapons 7075-T6 UNS A97075 Exfoliation corrosion Heat treating-related failures The lower receiver of the M16 rifle is an anodized forging of aluminum alloy 7075-T6. Degradation...
Abstract
The lower receiver of the M16 rifle is an anodized forging of aluminum alloy 7075-T6. Degradation of the receivers was observed after three years of service in a hot, humid atmosphere. The affected areas were those in frequent contact with the user's hands. There was no question that the material failed as a result of exfoliation corrosion, so an investigation was undertaken, centered around the study of thermal treatments that would increase the exfoliation resistance and still develop the required 448 MPa (65 ksi) yield strength. The results of the study concluded that rolled bar stock should be preferred to extruded bar stock. Differences in grain structure of the forgings, as induced by differences in thermal-mechanical history of the forged material, can have a significant effect on susceptibility to exfoliation corrosion. Regarding thermal treatment, the results show conclusively that large changes in strength and exfoliation characteristics of 7075 forgings can be induced by changes in temperature or time of thermal treatment. With regard to the effect of quenching rate on exfoliation characteristics, a cold-water quench below 25 deg C (75 deg F) would appear to be far superior to an elevated-temperature quench to minimize exfoliation for 7075 forgings in the T6 temper.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001600
EISBN: 978-1-62708-217-4
... be controlled especially at the critical areas of the web, to assure complete coverage and proper compressive residual stresses. Shot peening 7075 UNS A97075 Fatigue fracture Background Four helicopter main support bridges were shipped to the Army Research Lab (ARL) for analysis. The parts had...
Abstract
This paper summarizes the results of a failure analysis investigation of a fractured main support bridge made of 7075 aluminum alloy from an army helicopter. The part, manufactured by “Contractor IT,” failed component fatigue testing while those of the original equipment manufacturer (OEM) passed. Metallurgical data collected during this investigation indicated that the difference in fatigue life between the components fabricated by IT and by OEM may be attributable to a difference in dimensions at the web where fatigue crack initiation occurred. The webs of the two OEM parts examined had cross-sectional thicknesses significantly larger than the web cross-sectional thicknesses of the IT components. Recommendations included changing the web reference dimension of 0.38 in. to include a tolerance range based upon a fracture mechanics model. Also, the shot peening process should be controlled especially at the critical areas of the web, to assure complete coverage and proper compressive residual stresses.