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Luther M. Gammon, Michael V. Hyatt, G. Hari Narayanan, Henry J. Oberson, Harcayal B. Singh
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UNS A92024
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1-6 of 6 Search Results for
UNS A92024
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047677
EISBN: 978-1-62708-217-4
... nuggets that were the result of shunting caused by poor fit-up. The forming procedures were revised to achieve a precise fit between the stiffener and the tank wall. Also, an increase in welding current was suggested. Aircraft components Fitting Fuel tanks 2024-T8511 UNS A92024 Joining-related...
Abstract
Resistance spot welds joining aluminum alloy 2024-T8511 stiffeners to the aluminum alloy 6061-T62 skin of an aircraft drop tank failed during slosh and vibration testing. Visual examination of the fracture surfaces showed that the failure was by tensile or bending overload. Measurements of the fractured spot welds established that all welds were below specification size. Review of the assembly procedures revealed that there had been poor fit-up between the stiffeners and the tank skin, which resulted in weak, undersize weld nuggets. The spot welds failed because of undersize nuggets that were the result of shunting caused by poor fit-up. The forming procedures were revised to achieve a precise fit between the stiffener and the tank wall. Also, an increase in welding current was suggested.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047673
EISBN: 978-1-62708-217-4
... positioning. The problem could be solved by better forming procedures to provide an accurate fit-up that would not interfere with electrode alignment. Aircraft components Fuel tanks Welding parameters 2024-T62 UNS A92024 Joining-related failures A series of resistance spot welds joining Z...
Abstract
A series of resistance spot welds joining Z-shape and C-shape members of an aircraft drop-tank structure failed during ejection testing. The members were fabricated of alclad aluminum alloy 2024-T62. The back surface of the C-shape members showed severe electrode-indentation marks off to one side of the spot weld, suggesting improper electrode contact. Visual examination of the weld fractures showed that the weld nuggets varied considerably in size, some being very small and three exhibiting an HAZ but no weld. Of 28 welds, only nine had acceptable nugget diameters and fusion-zone widths. The weld deficiencies were traced to problems in forming and fit-up of the C-shape members and to difficulties in alignment and positioning of the weld tooling. The failure of the resistance spot welds was attributed to poor weld quality caused by unfavorable fit-up and lack of proper weld-tool positioning. The problem could be solved by better forming procedures to provide an accurate fit-up that would not interfere with electrode alignment.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001529
EISBN: 978-1-62708-217-4
... Melting Overheating 1230 UNS A91230 2024-T3 UNS A92024 (Other, miscellaneous, or unspecified) failure During a Seattle thunderstorm the evening of 16 July 1999, a Boeing 737–800 on final approach for landing sustained a major lightning strike. Based on the pattern of physical damage...
Abstract
On 16 July 1999, a Boeing 737-800 on final approach for landing sustained a major lightning strike. Damage to the fuselage structure primarily was in the form of melting or partial melting of widely-separated rivets and adjacent Alclad 2024-T3 fuselage skin. The damage was confined to a 0.25-in. (6.4-mm) radii around the affected rivets. The repair process involved removal of the locally-affected material and addition of a skin doubler to restore the aircraft structure to the originally designed condition. Damage features are described briefly.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006409
EISBN: 978-1-62708-217-4
... if pipe threads were to be used. A determination of proper torque values for tightening the connectors was suggested also. Aircraft components Scanning electron microscopy Stresses Tapping (threads) Wall thickness 2024 UNS A92024 Intergranular fracture Stress-corrosion cracking...
Abstract
Pitostatic system connectors were being found cracked on several aircraft. Two of the cracked connectors made of 2024-T351 aluminum alloy were submitted for failure analysis. The connectors had cut pipelike threads that were sealed with Teflon-type tape when installed. Longitudinal cracks were located near the opening of the female ends of each connector. A cross section showed intergranular cracking with multiple branching in one connector. Scanning electron microscopy (SEM) showed intergranular cracking and separation of elongated grains. A cross section of connector threads showed an incomplete thread form resulting from improper tapping. It was concluded that the pitostatic system connectors failed by SCC. The stress was caused by forcing the improperly threaded female nut over its fully threaded male counterpart to effect a seal. The one connector tested for chemical composition was not made of 2024 aluminum alloy as reported but of 2017 aluminum. It was recommended that the pitostatic system connector manufacturing process be revised to produce full-depth threads rather than pseudo pipe threads. Wall thickness should be increased to increase the hoop stress bearing area if pipe threads were to be used. A determination of proper torque values for tightening the connectors was suggested also.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047072
EISBN: 978-1-62708-217-4
... to the T6 temper after forming. Aircraft components Gas turbine engines Spot welds 2024-T42 UNS A92024 6061-T6 UNS A96061 Joining-related failures Fatigue fracture Heat treating-related failures Postflight inspection of a gas-turbine aircraft engine that had experienced compressor stall...
Abstract
Postflight inspection of a gas-turbine aircraft engine that had experienced compressor stall revealed that the engine air-intake bullet assembly had dislodged and was seated against the engine-inlet guide vanes at the 3 o'clock position. The bullet assembly consisted of an outer aerodynamic shell and an inner stiffener shell, both of 1.3 mm (0.050 in.) thick aluminum alloy 6061-T6, and four attachment clips of 1 mm (0.040 in.) thick alclad aluminum alloy 2024-T42. Each clip was joined to the outer shell by 12 spot welds and was also joined to the stiffener. Analysis (visual inspection, dye-penetrant inspection, and 10x/150x micrographs of sections etched with Keller's reagent) supports the conclusion that the outer shell of the bullet assembly separated from the stiffener because the four attachment clips fractured through the shell-to-clip spot welds. Fracture occurred by fatigue that initiated at the notch created by the intersection of the faying surfaces of the clip and shell with the spot weld nuggets. The 6061 aluminum alloy shell and stiffener were in the annealed (O) temper rather than T6, as specified. Recommendations included heat treating the shell and stiffener to the T6 temper after forming.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001546
EISBN: 978-1-62708-217-4
... microcracks between adjacent discontinuities supported a hydrogen blistering diagnosis. Adhesive joints Blistering Chemical milling Extrusions Microcracking Pitting (corrosion) 2024-T3 2024-T4 UNS A92024 Hydrogen damage and embrittlement Fatigue fracture Fatigue Microcracking in Alclad 2024...
Abstract
A longeron assembly constructed of Alclad 2024, some parts being in the T3 condition, others in the T42 condition, failed at a rivet hole. Plastic deformation at the crack site was found, but no plastic deformation was found in similar failed components. It was concluded that the numerous hairline cracks in the Alclad layer adjacent to the main fracture were fatigue cracks. In another case, bonded samples of 2024-T3 sheet were fatigue tested at various stress levels. Failures could be separated into three groups: those that failed in the adhesive bond, those that failed in the base material, and those that exhibited a dual failure. The last category failed in the adhesive bond and also showed a type of pitting on one face of the base material. In a third case, a 2024-T4 extrusion section was found to exhibit blistering after chemical milling. The presence of interconnecting microcracks between adjacent discontinuities supported a hydrogen blistering diagnosis.