Skip Nav Destination
Close Modal
By
Luther M. Gammon, Michael V. Hyatt, G. Hari Narayanan, Henry J. Oberson, Harcayal B. Singh
Search Results for
UNS A91230
Update search
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
Filter
- Title
- Authors
- Author Affiliations
- Full Text
- Abstract
- Keywords
- DOI
- ISBN
- EISBN
- Issue
- ISSN
- EISSN
- Volume
- References
NARROW
Format
Topics
Book Series
Date
Availability
1-1 of 1 Search Results for
UNS A91230
Follow your search
Access your saved searches in your account
Would you like to receive an alert when new items match your search?
Sort by
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001529
EISBN: 978-1-62708-217-4
... Melting Overheating 1230 UNS A91230 2024-T3 UNS A92024 (Other, miscellaneous, or unspecified) failure During a Seattle thunderstorm the evening of 16 July 1999, a Boeing 737–800 on final approach for landing sustained a major lightning strike. Based on the pattern of physical damage...
Abstract
On 16 July 1999, a Boeing 737-800 on final approach for landing sustained a major lightning strike. Damage to the fuselage structure primarily was in the form of melting or partial melting of widely-separated rivets and adjacent Alclad 2024-T3 fuselage skin. The damage was confined to a 0.25-in. (6.4-mm) radii around the affected rivets. The repair process involved removal of the locally-affected material and addition of a skin doubler to restore the aircraft structure to the originally designed condition. Damage features are described briefly.